210.1r-94 compendium of case histories on repair of erosion-damaged concrete in hydraulic structures
TRANSCRIPT
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ACI 210.1 R-94
Compendium of Case Histories on Repair ofErosion-Damaged Concrete in Hydraulic Structures
Reported by ACI Committee 210
(Reapproved 1999)
Stephen B. TatroChairman
Patrick J. Creegan Angel E. Herrera
James R. Graham Richard A.Kaden
This report is a companion document to ACI 210R. It contains a series of case histories on hydraulic structures that have been damaged by erosion
fro m various physical mechanical and chemical actions. Many of these structures have been successfully repaired. There were many examples to
select from; however, the committee has selected recent, typical projects,with differing repair techniques, to provide a broad range of current exper-
ience. These case histories cover only damage to the hydraulic surfaces dueto the action of water, waterborne material or chemical attack of concrete
from fluids conveyed along the hydraulic passages. In addition to repairsof the damaged concrete, remedial work frequently includes design modi-
fications that are intended to eliminate or minimize the action that pro-duced the damage. This report does not cover repair of concrete damaged by other environmental factors such as freeze-thaw, expansive aggregate, or corroding reinforcement.
Keywords: abrasion; abrasion resistance; aeration; cavitation; chemical attack;concrete dams; concrete pipes; corrosion; corrosion resistance; deterioration;erosion; grinding (material removal); high-strength concrete hydraulic structures;maintenance; outlet works; penstocks; pipe linings; pipes (tubes); pittings; polymer concrete; renovating; repairs; sewers; spillways; tolerances (mechanics); wear.
CONTENTS
Chapter l-Introduction, p. 210.1R-1
Chapter 2-Cavitation-erosion case histories, p.210.1R-2
Dworshak DamGlen Canyon DamLower Monumental DamLucky Peak DamTerzaghi DamYellowtail Afterbay Dam
Yellowtail DamKeenleyside Dam
ACI Committee Reports, Guides, Standard Practices, andCommentaries are intended for guidance in designing, plan-ning, executing, or inspecting construction and in preparing specifications. References to these documents shall not bemade in the Project Documents. If items found in thesedocuments are desired to be part of the Project Docu-ments, they should be phrased in mandatory language andincorporated into the Project Documents.
James E. McDonaldErnest K. Schrader
Chapter 3-Abrasion-erosion case histories, p. 21O.lR-13
Espinosa Irrigation Diversion DamKinzua Dam
Los Angeles River Channel Nolin Lake DamPine River Watershed, Structure No. 41Pomona DamProvidence-Millville Diversion StructureRed Rock DamSheldon Gulch Siphon
Chapter 4-Chemical attack-erosion case histories, p.210.1R-25
Barceloneta Trunk Sewer Dworshak National Fish HatcheryLos Angeles Sanitary Sewer System and
Hyperion Sewage Treatment FacilityPecos Arroyo Watershed, Site 1
Chapter 5-Project reference List, p.210.1R-32
CHAPTER 1-INTRODUCTION
This compendium of case histories provides informa-tion on damage that has occurred to hydraulic structuresand the various methods of repair that have been used.ACI Committee 210 has prepared this report to help oth-
ers experiencing similar problems in existing work.Knowledge gained from these experiences may help
ACI 210.1R-94 became effective Nov. 1.1994.Copyright 8 1994, American Concrete Institute.Al l rightsreserved including rights of reproduction and use in any formor by
any means, including the making of copies by any photo process, or by any elec-tronic or mechanical device, printed, written, or oral, or recording for sound orvisual reproduction for use in any knowledge or retrieval system or device, unlesspermission in writing is obtained from tbe copyright proprietors.
210.1R-1
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210.1R-2 ACI COMMITTEE REPORT
avoid oversights in design and construction of hydraulicstructures and provide guidance in the treatment of future problems.
Erosion of concrete in hydraulic structures may occur as a result of abrasive action, cavitation, or chemicalattack. Damage may develop rapidly after some unusualevent such as a flood or it may develop gradually during
normal continuous operation or use. In most cases wheredamage has occurred, simply replacing the eroded con-crete will ensure immediate serviceability, but may notensure long-term performance of the structure. There-fore, repair work usually includes replacing erodedconcrete with a more resistant concrete and additionalsurface treatment, modifying the design or operation of the structure to eliminate the mechanism that producedthe damage, or both. A detailed discussion of mechan-isms causing erosion in hydraulic structures, andrecommendations on maintenance and repair, is con-tained in ACI 210R.
When damage does occur to hydraulic structures,
repair work poses some unique problems and is oftenvery costly. Direct access to the damaged area may not be possible, or may be limited by time, or other con-straints. In some cases, such as repair to spillway stilling
basin floors, expensive bulkheads and dewatering arerequired. It may not be possible to completely dry thearea to be repaired or maintain the most desirabletemperature. A great deal of planning and scheduling for repair work are normally required, not only for therepairs and access, but also for control of water releasesand reservoir levels. If time permits, extensive inves-tigation usually precedes planning and scheduling to
determine the nature and extent of damage. Hydraulicmodel studies may also be necessary to evaluate possiblemodifications in the design or operation of the facility.
This compendium provides the history on 21 projectswith hydraulic erosion damage. They vary in size andcover a variety of problems: 8 with cavitation damage, 9with abrasion-erosion damage, and 4 with erosiondamage from chemical attack. Table 1.1 summarizes the
projects. Each repair was slightly different. Each historyincludes background information on the project or facil-ity, the problem of erosion, the selected solution to the
problem, and the performance of the corrective action.Histories also contain references and owner informationif further details are needed.
CHAPTER2-CAVITATION-EROSIONCASE HISTORIES
DWORSHAK DAM North Fork, Clearwater River, Idaho
BACKGROUNDDworshak Dam, operational in 1973, is a straight-axis
concrete gravity dam, 717 ft high, 3287 ft long at the
crest, and contains 6,500,000 cubic yards of concrete. Inaddition to two gated overflow spillways, three regulatingoutlets, 12 ft wide by 17 ft high, are located in the spill-way monoliths. The inlet elevation for each regulatingoutlet is 250 ft below the maximum reservoir elevation.Each outlet jet is capable of a maximum discharge of 14,000 fij/s.
Outlet surfaces are reinforced structural concrete placed concurrently with adjacent lean, large aggregateconcrete. Coatings to the outlet surfaces were appliedduring the original construction. In Outlet 1, the wall andinvert surfaces from the tainter gate to a point 50 ftdownstream are coated with an epoxy mortar having anaverage thickness of in. The same area of Outlet 2 wascoated using an epoxy resin, approximately .05 in. inthickness. Outlet 3 was untreated.
The outlets were operated intermittently at variousgate openings for a period of 4 years between 1971 and1975, resulting in a cumulative discharge duration of approximately 10 months. The three outlets were not
operated symmetrically; outlets 1 and 2 were used pri-marily.
PROBLEM
Inspection in 1973 showed minor concrete scaling of the concrete wall surfaces of Outlets 1 and 2. One year later, in 1974, serious erosion had occurred at wallsurfaces of both outlets immediately downstream of thewall coatings, 50 ft from the tainter gate. Part of this wallarea had eroded to a depth of 22 in., exposing and evenremoving some No. 9 reinforcing bars. In the wall sur-faces downstream of Outlet 1 medium damage, up to 1
in. depth of erosion, also occurred in over 60 squareyards of surface, bordered by lighter erosion. Everyhorizontal lift joint (construction joint) along the path of the jet, showed additional cavitation erosion.
SOLUTIONRepairs were categorized as three types:
l Areas with heavy damage, with erosion greater than2 to 3 in., were delineated by a 3-in. saw cut andthe interior concrete excavated to a minimumdepth of 15 in. (Fig. 2.1 and 2.2). Reinforcementwas reestablished and steel fiber-reinforced con-crete (FRC) was used as the replacement material.
l Areas with medium damage, where the depth of erosion was less than 1 in., were bush-hammered toa depth of to 1 in. and dry-packed with mortar.The mortar, if left untreated, would easily havefailed when subjected to the high velocity discharge.
l Areas with minor damage, surfaces showing a sand- blast texture, were not separately treated prior to polymer impregnation. The entire wall surfaces of Outlet 1 were then treated by polymer impregna-tion from the downstream edge of the existingepoxy mortar coating to a distance 200 ft down-
stream.
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REPAIR OF EROSION DAMAGED HYDRAULIC STRUCTURES 210.1 R-3
TABLE 1.1- SUMMARY TABLE OF PROJ ECTS COMPRISING THIS REPORT
Reference
page
210.1R-2
Year
completed Location Owner Problem Repair type
1974 Gravity dam Idaho Corps of Cavitation Polymer Engineers impregnation
1964 Arch dam Arizona Bureau of Cavitation AerationReclamation
Project name
Dworshak Dam
Glen Canyon Dam 210.1R-5
Lower MonumentalDam
210.1R-61969
1956
1960
1966
Navigation lock washington Corps of Cavitation EpoxyEngineers
Outlet structure Idaho Corps of Cavitation variousEngineers
Outlet structure British Columbia B.C. Hydro Cavitation HydraulicAuthority redesign
Stilling basin Montana Bureau of Cavitation Various overlaysRecIamation
1966
1968
Stilling basin Montana Bureau of Cavitation Aeration andRecIamation overIays
Outlet structure
British Columbia B.C. Hydro
Cavitation High-strength
Authority I concrete
Lucky Peak Dam 210.1R-8
Terzaghi Dam 210.1R-9
Yellowtail AfterbayDam
210.1R-11
Yellowtail Dam 210.1R-11
210.1R-12Keenleyside Dam
Espinosa Irrigation
Diversion Dam
1984 Diversion dam New Mexico
1965 Stilling basin Pennsylvania
Soil Conser-
vation ServiceCorps of Engineers
Abrasion
Abrasion
Steel plate armor
Silica fumeconcrete
210.1R-13
210.1R-15Kinzua Dam
Los Angeles River Channel
210.1R-171940s Channel California
1963 Stilling basin Kentucky
Proposed Channel Colorado
Corps of Engineers
Corps of Engineers
SoiI Conser-vation Service
Abrasion
Abrasion
Abrasion
Siiica fumeconcrete
Hydraulicredesign
High-strengthconcrete
NoIin Lake Dam 210.1R-18
Pine River Watershed,Structure No. 41
210.1R-19
Pomona Dam 1963
1986
1969
1991
1976
1960s
Varies
Stilling basin Kansas
Diversion dam Utah
Stilling basin Iowa
Syphon outlet Wyoming
Pipeline Puerto Rico
Concrete tanks Idaho
Sewerage Californiastructures
Corps of Abrasion variousEngineers
Soil Conser- Abrasion Surface hardener vation Service
Corps of Abrasion Underwater Engineers concrete
Soil Conser- Abrasion Polymer-modifiedvation Service mortar
Puerto Rico Chemical attack PVC liningAqueduct &Sewer Authority
Corps of Chemical attack LiningsEngineers
City of Los Chemical attack Shotcrete andAngeles PVC liners
210.1R-20
210.1R-22Providence-MillvilleDiversion Structure
Red Rock Dam 210.1R-23
Sheldon Gulch Siphon 210.1R-25
210.1R-25
210.1R-26
Barceloneta Trunk Sewer
Dworshak NationalFish Hatchery
Los Angeles SanitarySewer System andHyperion SewageTreatment Facility
Pecos ArroyoWatershed, Site 1
210.1R-27
1988
Outlet conduit
New Mexico Soil Conser-
Chemical attack HDPE liner and
vation Service hydraulic redesign210.1R-30
Damage to the epoxy mortar was minimal and located PERFORMANCEnear the outlet gate. This area was repaired with new
epoxy.The polymer impregnation process involved drying all
the surfaces to a temperature up to 300 F to drive off water and then allowing the surface to cool to 230 F.Monomer was then applied to the surface using a verticalsoaking chamber. Excessive monomer was drained andthe surface was polymerized by the application of approx-imately 150 F water.
Operation of the outlets from the time of repair in1975 until 1982 has been minimal averaging 1400 ft s
per outlet with peak discharges of 3600 ft s per outlet.Durations of usage are not known. After 1982 outlet dis-charges increased, with durations exceeding 50 days.
Inspections performed in 1976, the year after therepairs, showed no additional concrete damage except for some minor surface spalling adjacent to a major pre-existing crack in an area of dry-packed mortar. The
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210.1R-4 ACI COMMlTTEE REPORT
Fig. 2.1-Dworshak Dam. Detail showing depth of erosion behind reinforcing steel
Fig. 2.2-Dworshak Dam. Extent of outlet sur face preparation prior to concrete and mortar placements
spalled area was patched with epoxy paste, except thatthe epoxy paste did not bridge the crack this time. Epoxyresin coating repairs applied to Outlet 2 showed somefailures,
Inspections in 1983 and 1988 showed that epoxy mor-tar coatings in Outlet 1 continued to perform well. Smallareas of damage, typically spalls, are periodically repairedwith a paste epoxy. Epoxy resin coatings in Outlet 2 arerepaired more frequently but are performing adequately.Surfaces repaired with FRC and mortar and subsequently
polymer-impregnated showed negligible damage. Poly-
mer-impregnated parent concrete shows a typical matrixerosion around the coarse aggregate to a depth of 1/4-in.,and lift joints exhibit pitting up to 3/8-in. deep. Surfaces
along lift joints not polymer-impregnated show erosionup to 3/4-in. in depth and a general surface pitting greater than the companion polymer-impregnated surfaces,
DISCUSSIONBecause of variation in the operation of these outlets,
both in flow rate and duration, exact time-rate erosionconclusions are difficult to make. Recent outlet dischargehas fluctuated annually from moderate flows to none. Ingeneral, surfaces that received replacement materials andwere subsequently polymer-impregnated have performed
well. Original concrete and new polymer impregnatedconcrete is showing evidence of deterioration, but at arate that is less than the unimpregnated surfaces. The
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REPAIR OF EROSION DAMAGED HYDRAULIC STRUCTURES 210.1 R-5
best performance was by the original epoxy mortar coat-ing. The epoxy mortar in Outlet 1 continues to display anexcellent surface condition, with no cavitation-generated
pitting. The epoxy resin coating in Outlet 2 displays good performance.
In 1988, outlets were modified by adding aeration de-flectors, wedges 27 in. wide by 1.5 in. high, to the sides
and bottom of each outlet. These deflectors were de-signed to increase the aeration of the discharge jet andfurther reduce the cavitation erosion of the outlet sur-faces. Subsequent deterioration of the outlet surfaces hasnot been observed.
The polymer impregnating of the concrete surfaces of the outlets was a very complex system of operations. Suc-cess requires continual evaluation of application condi-tions and flexibility to react to changes in those condi-tions. Issues relating to safety, cost, and field engineeringadd significant challenges to a polymer impregnation pro-
ject. It is doubtful that this process would be attemptedtoday under similar circumstances. It is more likely thatthe aeration deflectors would be the first remedy con-sidered since they provide a positive solution to the
problem without the higher risks of a failure inherent inthe polymer impregnation process.
REFERENCESSchrader, Ernest K., and Kaden, Richard A, “Outlet
Repairs at Dworshak Dam,” The Military Engineer, TheSociety of American Military Engineers, Washington,D.C., May-June 1976, pp. 254-259.
Murray, Myles A, and Schultheis, Vem F., “Polymer-ization of Concrete Fights Cavitation,” Civil Engineering,
V. 47, No. 4, American Society of Civil Engineers, NewYork, April 1977, pp. 67-70.
U.S. Army Engineer District, Walla Walla, “Polymer Impregnation of Concrete at Dworshak Dam,” WallaWalla, WA, July 1976, Reissued April 1977.
U.S. Army Engineer District, Walla Walla, “PeriodicInspection Reports No. 6, 7, and 8, Dworshak Dam andReservoir,” Walla Walla District, Jan. 1985.
CONTACT/OWNER
Walla Walla District, Corps of Engineers
City-County AirportWalla Walla, WA 99362
GLEN CANYON DAM
Colorado River, Northeast Arizona
BACKGROUNDGlen Canyon Dam, operational in 1964, is a concrete
gravity, arch structure, 710 ft high with a crest length of 1560 ft. The dam is flanked on both sides by high-headtunnel spillways, each including an intake structure withtwo 40- by 55-ft radial gates. Each tunnel consists of a
41-ft diameter section inclined at 55 percent, a vertical
bend (elbow), and 985 ft of near horizontal length fol-lowed by a deflector bucket. Water first flowed throughthe spillways in 1980, 16 years after completion of thedam.
PROBLEMIn late May 1983, runoff in the upper reaches of the
Colorado River was steadily increasing due to snowmeltfrom an extremely heavy snowpack. On June 2,1983, theleft tunnel spillway gates were opened to release 10,000ft 3/s. On June 5 the release was increased to 20,000 ft 3/s.On June 6 officials heard loud rumbling noises comingfrom the left spillway. Engineers examined the tunneland found several large holes in the invert of the elbow.This damage was initiated by cavitation, triggered by dis-continuities formed by calcite deposits on the tunnelinvert at the upstream end of the elbow. In spite of thisdamage, continued high runoff required increasing thedischarge in the left spillway tunnel to 23,000 ft 3/s. byJune 23. Flows in the right spillway tunnel were held at6000 ft3/s. to minimize damage from cavitation. Spillwaygates were finally closed July 23, and engineers made athorough inspection of the tunnels.
Extensive damage had occurred in and near the lefttunnel elbow (Fig. 23). Immediately downstream fromthe elbow, a hole (35 ft deep, 134 ft long, and 50 ft wide)had been eroded in the concrete lining and underlyingsandstone foundation. Other smaller holes had beeneroded in the lining in leapfrog fashion upstream fromthe elbow.
SOLUTION
The repair work was accomplished in six phases: 1) re-moving loose and defective concrete lining and founda-tion rock; 2) backfilling large cavities in sandstone foun-dation with concrete; 3) reconstructing tunnel lining; 4)grinding and patching of small defective areas; 5) remov-ing about 500 cubic yards of debris from lower reaches of tunnel and flip bucket; and 6) constructing an aerationdevice in the lining upstream of the vertical elbow.
Sandstone cavities were filled with tremie concrete be-fore the lining was replaced. About 2000 cubic yards of replacement concrete was used. The aeration slot wasmodeled in the Bureau of Reclamation Hydraulic Labor-
atory to ensure that its design would provide the per-formance required.The aeration slot was constructed on the inclined por-
tion of the tunnel approximately 150 ft upstream fromthe start of the elbow. A small 7-in-high ramp was con-structed immediately upstream of the slot. The slot was4 by 4 ft in cross section and extended around the lower three-fourths of the tunnel circumference (Fig. 2.4). Allrepairs and the slot were completed in the summer of 1983.
PERFORMANCEBecause of the moderate runoff in the Colorado River
since completion of the tunnel repairs, it has not been
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210.1R-6 ACI COMMITTEE REPORT
Fig. 2.3-Glen Canyon Dam. Erosion of spillway tunnel invert and sandstone foundationrock downstream of the elbow
necessary to use the large spillway tunnels. However,shortly after completion of the work, another high runoff
period permitted performance of a field verification test.This test lasted 72 hr with a maximum flow during thattime of 50,000 ft 3/S. The test was conducted in two
phases with several interruptions in each for examinationof the tunnel Offsets were intentionally left in place toevaluate whether the aeration slot would indeed preclude
cavitation and attendant concrete damage. The tunnel re- pairs and air slot performed as designed. No sign of cavi-tation damage was evident anywhere in the tunnel. Aera-tion has decreased the flow capacity of the spillwaytunnels by approximately 20 percent of the original flowcapacity.
REFERENCES
Burgi, P.H., and Eckley, M.S., “Repairs at Glen Can-yon Dam,” Concrete International, American ConcreteInstitute, MI, V. 9, No. 3, Mar. 1986, pp. 24-31.
Frizell, K.W., “Glen Canyon Dam Spillway TestsModel - Prototype Comparison,” Hydraulics and Hydro-logy in the Small Computer Age, Proceeding of the Spe-cialty Conference, Lake Buena Vista, Florida, Aug.
12-17, 1985, American Society of Civil Engineers, NewYork, 1985, pp. 1142-1147.
Frizell, K.W., “Spillway Tests at Glen Canyon Dam,”U.S. Bureau of Reclamation, Denver, CO, July 1985.
Pugh, C.A., “Modeling Aeration Devices for GlenCanyon Dam,” Water for Resource Development, Proceed-ings of the Conference, Coeur d’Alene, Idaho, Aug.14-17, 1984, American Society of Cii Engineers, New
York, 1984, pp. 412416.
CONTACT
U.S. Bureau of ReclamationP.O. Box 25007, Denver Federal Center Denver, CO 80225
LOWER MONUMENTAL DAMSnake River, Near Kaloutus, Washington
BACKGROUNDLower Monumental Dam, operational in 1970, consists
of a concrete gravity spillway and dam, earthfii em-
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210.1R-7
Original tunnel surfac
Aeration slot
.I8
SECTION A-A
Fig. 2.4-Glen Canyon Dam. Diagram of new tunnel spillway air slot
bankments, a navigation lock, and a six-unit powerhouse.The 86-ft wide by 675-ft long navigation lock chamber,
with a rise of 100 ft, is filled and emptied by two galleriesor culverts, landside and riverside of the lock structure.
The landside culvert, which supplies five downstream lat-erals, crosses under the navigation lock to discharge intothe river. The riverside culvert supplies and dischargeswater to the upstream five laterals. Each lateral consistsof 10 portal entrances approximately 1.5 ft wide by 3 fthigh. Plow velocities in excess of 120 ft/s occur in severalof the portals entrances. A tie-in gallery exists betweenthe two main culverts, near the downstream gates, thatequalizes the pressure between the two culverts.
PROBLEMInspections as early as 1975 revealed that the ceiling
concrete of the landslide culvert was spalled at somemonolith joints to depths of 9 in. This may have been ini-tiated by differential movement of adjacent monolithswhen the lock chamber was filled and emptied. Damageto the invert, at several locations, was irregular, witherosion a maximum of 18 in. deep at the monolith joint,decreasing to 1 in. at a point 10 ft upstream of the joint.Reinforcing steel was exposed. Other areas of erosion inthe invert and on wall surfaces were observed, measuring2 ft square and 2 in. deep.
Later inspections revealed that portal surfaces nearestthe culverts of the most downstream laterals were show-ing signs of concrete erosion (Fig. 2.5). By 1978, the por-
tal walls, ceiling, and invert had eroded as deep as 3 in.
over an area of 5 square ft, exposing reinforcing steel.All four corners of the tie-in gallery experienced ob-
vious cavitation damage. The damage varied from minor pitting to exposure and undercutting of the 11/2-in. aggre-
gate.
SOLUTIONIn 1978, the navigation lock system was shut down for
two weeks for repairs. The major erosion damage to thelandslide culvert was repaired by mechanically anchoredsteel fiber-reinforced concrete. The smaller areas of damage received a trowel application of a paste epoxy
product. Ceiling damage was backfilled with dry-mixshotcrete. Portal and tie-in gallery surfaces receivedapplication of a paste epoxy, troweled to a feather edgearound the perimeter.
PERFORMANCE
The mechanically anchored fiber-reinforced concretehas performed well to date. No additional erosion has
been observed. Shotcrete patches to the ceiling adjacentto the joints show continued spalling, but to a lesser extent than prior to repairs.
The repairs to the portal surfaces and tie-in gallerysurfaces performed poorly. After 1 year of service, ap-
proximately 40 percent of the epoxy paste had failed; andafter 3 years, nearly 100 percent has failed. Concreteerosion in these areas has subsequently increased todepths of 6 to 8 in. in the tie-in gallery and up to 5 to 6
in. on the two most downstream portal surfaces.
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210.1R-8 ACI COMMITTEE REPORT
DISCUSSIONRecent inspections have shown that the rate of erosion
has decreased. The accumulated erosion of concrete fromcertain surfaces is significant; however, subsequent ero-sion is almost negligible. Consequently, repair schedulesare not critical.
Paste epoxy was applied to the concrete surfaces tran-sitioning to feather edges along the perimeter of the
patches. Cavitation eroded the concrete adjacent to the
feather edges as weIl as eroding the thin epoxy edges(Fig. 2.5). These new voids undermined the new, thicker epoxy, and at some point caused another failure of theleading edge. As the leading edge void increased in size,the failure progressed until little epoxy was left in therepaired area. After erosion of the epoxy patch material,no further concrete erosion has occurred. It appears thatthe eroded configuration of the surface is hydraulicallystable.
Patch-type repair procedures are not sufficient for thisstructure because erosion is initiated at the edge of thenew patch. Eventual repairs will replace larger areas of the concrete flow surfaces and will include substantialanchoring of new materials.
U.S. Army Engineer District, Walla Walla, “PeriodicInspection Report No. 6, Lower Monumental Lock andDam,” Walla Walla, WA, Jan. 1977.
U.S. Army Engineer District, Walla Walla, “PeriodicInspection Report No. 7, Lower Monumental Lock andDam,” Walla Walla, WA, Jan. 1981.
U.S. Army Engineer District, Walla Walla, “PeriodicInspection Report No. 8, Lower Monumental Lock andDam,” Walla Walla, WA, Jan. 1983.
CONTACT/OWNER
Walla Walla District, Corps of EngineersCity-County AirportWalla Walla, WA 99362
LUCKY PEAK DAMBoise River, Near Boise, Idaho
BACKGROUNDLucky Peak Dam, operational in 1955, is 340 ft high
with a crest length of 2340 ft. The dam is an earth androckfill structure with a silt core, graded filters, and rock shells. The ungated spillway is a 6000-ft-long ogee weir discharging into an unlined channel. The outlet worksconsists of a 23-ft-diameter steel conduit that deliverswater to a manifold structure with six outlets. Each outletis controlled by a 5.25-ft by 10-ft slide gate. Individual
flip lips were constructed downstream from each slidegate. Downstream of the flip lips is the plunge pool, ex-cavated into the basalt rock, with bottom areal dimen-sions of 150 by 150 ft. The outlet alignment and designwere determined by hydraulic modeling. The sir outletsoperated under a maximum head of 228 ft with a designdischarge of 30,500 ft3/S and a maximum discharge vel-ocity ranging between 88 ft/s and 124 ft/s.
PROBLEMThe steel manifold gates have a long history of cavi-
tation erosion problems. The original bronze gate seals
were seriously damaged by cavitation after initial use.Flow rates across the manifold gate frames in excess of 150 ft/s for many days were common. The gate seals werereplaced with new seals made of stainless steel andaluminum-bronze. The cast-steel gate frames requiredcontinual repair of cavitated areas. In 1975 alone, over 2000 pounds of stainless steel welding rod was manuallywelded into the eroded areas and ground smooth. Neatcement grout was pumped behind the gate frames to re-establish full bearing of the gate frames with the concretestructure.
The concrete invert and side piers, which separate
each of the six flip lips suffered extensive erosion soonafter the start of operations in 1955 (Fig. 2.6). 3/4-in.-thick steel plates were anchored to the piers and invert areas
just downstream of the manifold gates. These steel wall plates became severely pitted, as did the downstreamconcrete flip lip invert surfaces. In 1968, the damaged
plates were again repaired by filling the eroded areaswith stainless steel welding, and grouting behind the plates Deteriorated concrete on the flip lips was re-moved and additional steel plates were installed over those areas. This also failed and repairs commencedagain. Deep areas of cavitation damage in the invert and
piers were filled with concrete. New 1/2-in.-thick plates
were installed. These were stiffened with steel beams,welded on 5-ft centers in each direction. Deep anchor
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REPAIR OF EROSlON DAMAGED HYDRAULIC STRUCTURES 210.1R-9
bars were welded to the plate material to hold them in place. Again, the voids under the plates were grouted.But during the next two years, these repairs also failed.
In 1974, it was recommended that the outlet be re-studied hydraulically. That year, remaining plate materialwas removed. Cavities were found penetrating the invertand through the piers and into the adjacent outlet invert.
These voids were crudely filled with FRC in a “fieldexpedient” manner. Much of this FRC was placed instanding water with little quality control, while adjacent
bays were discharging.
SOLUTIONThe side piers were redesigned and replaced to pro-
vide vents that would introduce air to the underside of the jet just downstream of the gates. This modificationwas intended to prevent additional invert erosion. How-ever, major modifications to the gates and gate frameswere necessary if cavitation erosion was to be eliminated
These modifications were not made since future power-house construction would reduce and nearly eliminatethe need to use the outlet, reserving the structure for emergency and special operations use only. Steel liningon the piers was strengthened and replaced. Stiffenedsteel plates, 11/4-in. thick, were installed on the piers andinvert. Mortar backfill was pumped behind the invert
plates and new concrete placed between pier plates.
PERFORMANCEAfter one year of above average usage on bays 3 and
4, cavitation was again observed. The side piers just
downstream of the gates showed areas of 1 to 2 squareft that had eroded through the steel plate and into theconcrete about 6 in. No erosion of the invert plates or the “field expedient” FRC occurred. Use of these bayshas almost stopped since the new powerhouse becameoperational.
DISCUSSIONThe introduction of air beneath the jet appears to
have cushioned the effects of cavitation on the flip lipinvert. However, pier walls continue to erode at an extra-ordinary rate. The cause lies with the design of the gates
and gate frame. It is evident that satisfactory perfor-mance of the structure can never be achieved until thegates and frames are redesigned and reconstructed toeliminate the conditions that cause cavitation.
REFERENCESU.S. Army Engineer District, Walla Walla, “Lucky
Peak Lake, Idaho, Design Memorandum 12, Flip BucketModifications,” Supplement No. 1, Outlet Works, SlideGate Repair and Modification, Walla Walla, WA, July1986.
U.S. Army Engineer District, Walla Walla, “PeriodicInspection Report No. 6, Lucky Peak Lake,” WallaWalla, WA, Jan. 1985.
U.S. Army Engineer District, Walla Walla, “Periodic
Fig. 2.6-Lucky Peak Dam. Cavitation erosion of flip lip surface
Inspection Report No. 7, Lucky Peak Lake,” WallaWalla, WA, Jan. 1989.
CONTACT/OWNER
Walla Walla District, Corps of EngineersCity-County AirportWalla Walla, WA 99362
TERZAGHI DAMBridge River Near Lillooet, British Columbia, Canada
BACKGROUND
Terzaghi Dam, operational in 1960, is 197 ft high witha crest length of 1200 ft. The earth and rockfill embank-ment consisting of an upstream impervious fill, clay blan-ket, sheet pile cutoff, and multiline grout curtain, isfounded on sands and gravels infilling a deep river chan-nel. The dam impounds Bridge River flow to form theCarpenter Lake reservoir, from which water is drawnthrough two tunnels to Bridge River generating stations1 and 2, located at Shalalth, B.C., on Seton Lake.
Terzaghi Dam discharge facilities are composed of asurface spillway consisting of a 345 ft long free overflowsection; and a gated section with two 25 ft wide by 35 fthigh gates. Two rectangular low level outlets (LLO), each
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210.1R-10 ACI COMMITTEE REPORT
Fig. 2.7-Terzaghi Dam. Downstream detail of constrictor
ring
8 ft wide by 16 ft high are subject to a maximum heat of 169 ft. These outlets were constructed in the top half of the concrete plug in the 32 ft, horseshoe-shaped diversiontunnel.
PROBLEMThe LLOs were operated in 1963 for about 23 days to
draw down Carpenter Lake to permit low-level embank-ment repairs. Severe cavitation erosion of the concretewall and ceiling surfaces downstream of bulkhead gateslots was observed in the north LLO after the water re-lease.
Dam safety investigations in 1985 identified that theLLOs were required to permit emergency drawdown of Carpenter Lake for dam inspection and repair, and to
provide additional discharge capacity during large floods.
SOLUTIONThe repair consisted of three main categories of work
-
repair of damage, improvement to reduce cavitation potential, and refurbishing gates and equipment.Repair of cavitation damage in the north LLO in-
cluded repair of the walls, crown, and gate slots.Improvements to reduce cavitation potential included
1) installing 9-in. deep rectangular constrictor frames(Fig. 2.7) immediately downstream of the operating gatesto increase pressures in the previously cavitated area, 2)
backfilling old bulkhead gate slots and streamlining theexisting LLO invert entrances, and 3) installing piezo-meters in the north LLO to provide information on flowcharacteristics of the streamlined LLO during dischargetesting.
Refurbishing gates and equipment included 1) re- placing leaking gate seals on closure gates; 2) sand- blasting and repainting gates, guides, head covers, and air shafts, 3) cleaning gate lifting rods and replacing bonnet
packings; 4) replacing ballast concrete in north LLOgates and installing ballast cover plates on all gates; and5) refurbishing hydraulic lifting mechanisms of gates.
Repair concrete was designed to fully bond withexisting concrete. Surface preparation included; saw
cutting around the perimeter of the damage, chipping toexpose rebar, and installation of grouted dowels. Latex-modified concrete was used for all repair work, with steelfiber reinforcement for the cavitation-damaged areas.
A total of 26 cubic yards of 3000 psi ready-mixed con-crete was placed by pumping. Maximum aggregate sizesof 3/8-in. and 3/4-in. were used for general repair and in-vert entrance backfill, respectively.
The constrictor frames were made from 1/2-in. and3/4-in. steel plate. They were installed in the LLOs bymeans of the following: 1) bolting the constrictor frameto the existing concrete with a double row of l-in.
diameter adhesive anchors at 12-in. spacing 2) keying theconstrictor infill concrete into the existing concrete; 3)welding the constrictor frame to the existing gate metal-work in the walls and soffit; and 4) embedding the con-strictor sill shear bar into the existing concrete invert(Fig. 2.7).
PERFORMANCEA test with a full reservoir and a peak discharge of
7000 ft3/S, with both gates opened 7 ft, verified that theconstrictor frames and concrete repairs, downstream of the closure gates, performed as designed No cavitation
erosion of the wall and ceiling surfaces was observed.
DISCUSSIONPiezometer readings confirmed that the constrictor
frames in the LLOs helped maintain pressures above at-mospheric, indicating that cavitation should not be a
problem in the future.
REFERENCESB.C. Hydro, “Terzaghi Dam, Low Level Outlet Re-
pairs-Memorandum on Construction,” Report No. EP6,
Vancouver, B.C., Dec. 1986.B.C. Hydro, “Terzaghi Dam, Low Level Outlet Tests,” Report No. H1902, Vancouver, B.C., Mar. 1987.
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REPAIR OF EROSION DAMAGED HYDRAULIC STRUCTURES 210.1R-11
CONTACT/OWNER
British Columbia HydroHydrotechnical Department, HED6911 Southpoint DriveBurnaby, British Columbia, Canada V3N 4X8
YELLOWTAIL AFTERBAY DAMBighorn River, Montana
BACKGROUNDYellowtail Afterbay Dam, operational in 1966, is a
33-ft-high concrete gravity diversion type structure, 300ft long, located about 1 mile downstream from YellowtailDam. In 1967 following a heavy winter/spring snowpack in the upstream drainage basin, flood flows passedthrough both Yellowtail Dam and the Afterbay Dam.
PROBLEMDivers examined the Afterbay Dam sluiceway and still-
ing basin after the flood flows had passed. They foundcavitation damage on the dentates (baffle blocks) andadjacent floor and wall areas in the spillway stilling basin.Although the cavitation damage was moderate, repairswere necessary to lessen the likelihood that futurecavitation damage would occur.
Damage to the dentates and floor in the sluiceway wascaused by abrasion. The relatively low sill at the down-stream end of the sluiceway was permitting downstreamgravel and sand to be drawn into the stilling area, wherea ball mill-type action ground away the concrete surfaces.
In the stilling basin downstream of the reverse ogeesection, cavitation severely eroded the sides of the den-tates and the adjacent floor areas. A similar conditiondeveloped in the sluiceway except that it was caused byabrasion erosion. Since the damage from the two causesoccurred essentially side by side, the situation graphicallyillustrated the dissimilar types of erosion resulting fromcavitation and abrasion.
SOLUTIONFollowing the flood, low flows at the dam could be
maintained for only one month. That situation required
that all repairs be completed quickly and concurrently. Inaddition to repairing damaged areas, the downstream sillin the sluiceway was raised about 3 ft to stop river gravels from being drawn into the sluiceway. Repairswere completed using a combination of bonded concrete,epoxy-bonded concrete and epoxy-bonded epoxy mortar,depending upon thickness of the repair. Epoxy used inthis repair was a polysulfide-type material. After repairedmaterials had been placed and cured, they were groundto provide a smooth, cavitation-resistant surface.
PERFORMANCE
The dam has now been in service about 23 years sincethe repairs were made. With the exception of a minor
number of spalls, the performance of the repairs has been excellent.
REFERENCESGraham, J.R., “Spillway Stilling Basin Repair Using
Bonded Concrete and Epoxy Mortar,” Proceedings, Irri-gation and Drainage Specialty Conference, Lincoln, NE,
Oct. 1971, pp. 185-204.Graham, J.R., and Rutenbeck, T.E., “Repair of Cavita-tion Damaged Concrete, a Discussion of Bureau of Reclamation Techniques and Experiences,” Proceedings,International Conference on Wear of Materials, St.Louis, MO, April 1977, pp. 439-445.
CONTACT
Bureau of ReclamationP.O. Box 25007, Denver Federal Center Denver, CO 80225
YELLOWTAIL DAMBighorn River, Montana
BACKGROUNDThe dam, operational in 1966, is a concrete arch struc-
ture 525 ft high with a crest length of 1480 ft. Normalflow through the dam occurs in two 84-in. outlet pipesand through the turbines of the powerhouse. Flows ex-ceeding the capacity of these facilities are routed througha high-head spillway located in the left abutment. At thisspillway, water enters through a radial-gated intake struc-
ture, then passes into an inclined section of tunnel vary-ing in diameter from 40.5 ft at the upper end to 32 ft atthe beginning of the vertical elbow. Thereafter, flow fol-lows the 32-ft-diameter tunnel through the elbow and1200 ft of near horizontal tunnel, exiting into a combina-tion stilling basin-flip bucket, then into the river.
During the spring of 1967, heavy rains in the water-shed area of the Bighorn River resulted in high inflowsinto Bighorn Lake behind Yellowtail Dam. A total of 650,000 acre-ft of flood waters was released through thespillway over a period of 30 days. Maximum flow was18,000 ft3/S.
PROBLEMDuring the 1967 spill, severe damage occurred to the
concrete tunnel lining and underlying rock in the elbow,as well as upstream and downstream. After the flows intothe river had subsided sufficiently for a temporary shut-down of the tunnel, divers made an examination. Major damage was found in the near-horizontal section of thetunnel lining and in the elbow. Failure occurred alongthe tunnel invert in a leapfrog fashion, typical of cavi-tation damage. The largest cavity was about 100 ft long,20 ft wide and 6 to 8 ft deep. After the tunnel was de-watered, it was found that a small concrete patch placedduring construction had failed. therebv causing the dis-
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210.1R-12 ACI COMMlTTEE REPORT
continuity in the flow that triggered the cavitation.
SOLUTIONThe tunnel liner was repaired using several systems
depending on the size and depth of the damage. Areaswhere the damage extended through the lining into thefoundation rock were repaired with high quality replace-
ment concrete. Major areas of damage where the erosiondid not penetrate through the concrete lining wererepaired with bonded concrete. Shallow-damaged con-crete was repaired with epoxy-bonded concrete andepoxy-bonded epoxy mortar. Surfaces were ground wherenecessary to bring tolerances into conformance withspecifications requirements. Finally, tunnel surfaces
below spring line were painted with an epoxy-phenolic paint, to help seal the surface and bond any aggregate particles that may have been loosened
In order to avoid recurring damage, an aeration devicewas model tested in the laboratory and then constructed
in the tunnel a few ft upstream of the point of curvatureof the vertical elbow. This aeration slot measured 3 ftwide and 3 ft deep and extended around the lower threequarters of the tunnel circumference. It was designed toentrain air in the flow for all discharges up to 92,000ft3/S, without the slot filling with water. A 27-in-longramp was constructed upstream of the slot which raisedthe upstream face of the slot 3 in. at the tunnel invert.Under most flow conditions the bottom of the jet wasforced away from the tunnel floor surface. The jet re-mained free for a considerable distance downstream, allthe while drawing air into the jet from the aeration slot.Aeration has reduced the discharge capacity by approxi-
mately 20 percent.
PERFORMANCEIt has now been 23 years since the tunnel was repaired
and the aeration slot installed, but flows in the river havenever been sufficient to require use of the spillway. How-ever, a controlled prototype test with flows to 16,000 ft3/swas conducted in 1969 and 1970. As a result of this test,less than one percent of the concrete repairs failed andno cavitation damage was observed, even in areas down-stream from discontinuities. To ensure that the tunnelwill always be ready for the next flow, there is a regular
maintenance program to repair ice damage and removecalcium carbonate buildups.
REFERENCESBorden, R.C., et al., “Documentation of Operation,
Damage, Repair, and Testing of Yellowtail Dam Spill-way,” Report No. REC-ERC-71-23, Bureau of Reclama-tion, Denver, CO, May 1971.
Colgate, D., and Legas, J., “Aeration MitigatesCavitation in Spillway Tunnel,” Meeting Preprint 1635, National Water Resources Engineering Meeting, Jan.
24-28, 1972, Atlanta, GA, American Society of CivilEngineers, New York, NY, 29 pp.
CONTACT
U.S. Bureau of ReclamationDenver Office, Code D-3700P.O. Box 25007, Denver Federal Center Denver, CO 80225
KEENLEYSIDE DAMColumbia River, near Castlegar, B.C., Canada
BACKGROUNDThe dam, operational in 1968, consists of an earthfill
embankment 1400 ft long and about 171 ft high and aconcrete gravity section about 1180 ft long and 190 fthigh. The concrete section contains four 55 ft widesluiceways, eight 20 by 24 ft high low level ports, and anavigation lock.
The sluiceway downstream of the gate slot has an ogeesection designed very conservatively for 65 percent of the
design head. Upstream of the gate sill the profile is afairly broad three-radius compound curve. Accordingly,no negative pressures should occur anywhere on the crestunder free discharge operation.
PROBLEMCavitation damage has occurred on the sluiceway crest
near the gate slots on all four bays. The damage ex-tended from inside the upstream portion of the gate slotto a point about 4 ft downstream, extending at an angleof about 30 degrees to the direction of flow (Fig. 2.8).
All attempts to repair the eroded concrete with epoxymixtures and steel fiber-reinforced concrete (FRC) in
1973, 1975, and 1977 were unsuccessful. Continued cav-itation soon pitted the repaired areas which later pro-gressed to development of major voids. By 1980 approxi-mately 80 percent of the previous repair had eroded.During a high water inspection in 1986, sluiceway No. 2was flow tested for 4 hr at gate openings of 4, 8, 12 and16 ft and full opening. Characteristic noises of cavitation
bubble collapse could be heard intermittently at all gatesettings. The highest rate of cavitation activity wasobserved to be with gate openings from 4 to 12 ft.
The deepest erosion usually occurred just outside thegate slot with depths ranging from about 8 to 14 in.
Downstream of the badly eroded area, the concrete atthe invert was observed to be roughened for another 2 ft.The maximum width of the eroded area varied from 18to 24 in.
The cavitation erosion at the foot of the gate slotdamaged not only the concrete invert but also the lower
part of the steel liner within the gate slot and an area of the wall immediately downstream of the liner. The 1986study concluded that the severe concrete erosion at and
just downstream of the gate slots was due to 1) cavitationcaused by vortices originating in the upstream corners of the gate slots at small, part-gate operation; and 2) lack of
rounding and lack of offset of downstream edge of gateslot.
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REPAIR OF EROSION DAMAGED HYDRAULIC STRUCTURES 210.1R-13
SOLUTION
Initially, it was recommended that 1) eroded areasshould be filled with concrete and armored with steel
plates, and; 2) field tests should be conducted to identifycavitation zones. Later, the recommendation was changedto backfill cavitated areas with aggregate, highstrength (6000 psi) concrete. The bond between the back-
fill and the original sluiceway concretes was enhanced byepoxy bonding agent. The top surface of the new patchand the surrounding original concrete were coated withan acrylic latex selected through an extensive laboratoryscreening process.The work was carried out in the sum-mer of 1990.
PERFORMANCE
In order to test the effectiveness of the repairs, duringthe following year it was decided to operate the sluicegates mostly in the worst range. A year later, the re- paired and coated surfaces began to show signs of pitting.
The performance of the repair still did not appear satis-factory. It became obvious that besides repairing theeroded areas other initiatives were needed to alleviaterecurrence of the problem.
DISCUSSIONBased on the observations of the effect of gate open-
ing on cavitation, it was decided to limit gate operationto that outside of the destructive range. Gate operatingorders were rewritten to require “passing over” the roughzones as quickly as possible without any sustainedoperation in those zones.
REFERENCESB.C. Hydro, Hydroelectric Engineering Division,
“Hugh Keenleyside Dam, Cavitation Damage on Spill-way,” Report No. H1922, Vancouver, B.C., Mar. 1987.
B.C. Hydro, Hydroelectric Engineering Division,“Keenleyside Dam, Comprehensive Inspection and Re-view 1986,” Report No. H1894, Vancouver, B.C., May1987.
B.C. Hydro, Hydroelectric Engineering Division,“Hugh Keenleyside Dam, Cavitation Damage on Spillway,Field Investigation of Cavitation Noise and Proposed
Gate Operating Schedules,” Report No. 2305, Vancouver,B.C., June 1992.
CONTACT/OWNER
British Columbia Hydro Structural DepartmentHED6911 Southpoint DriveBumaby, British Columbia, Canada V3N4X8
CHAPTER 3-ABRASION-EROSION
CASE HISTORIES
ESPINOSA IRRIGATION DIVERSION DAMEspBnola, New Mexico, on the Santa Cruz River
Fig. 2.8-Keenleyside Dam. Cavitation erosion of concreteinvert and adjacent damage to steel liner. Maximum depthapproximately 9 in.
BACKGROUND
The diversion dam is a reinforced concrete structurethat is capable of diverting up to 13 f in the EspinosaDitch for irrigation purposes. A 50-ft-long reinforced rec-tangular concrete channel, sediment trap, and sluice gatestructures were constructed between the headgate and
the ditch heading. A sidewall weir notch is provided inthe rectangular ditch lining to allow emergency dischargeof flood flows back to the river. A 24-in.-round sluicegate at the right side of the dam was placed at the slabinvert elevation, to sluice sand and cobbles through thedam and to prevent these materials from entering the ir-rigation ditch head gate. The dam is tied back into theriverbanks on either side with small earthen dikes that
protect theft3/s or less.
surrounding land against flood flows of 1000
PROBLEMDebris plugged the sluice gate, preventing the diver-
sion of the bedload from the irrigation ditch. The struc-ture experienced severe erosion damage to the apron and
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ACI COMMITTEE REPORT
Fig. 3.1-Espinosa Irrigation Diversion Dam. Erosion damage to the floor blocks
Fig. 3.2-Espinosa Irrigation Diversion Dam. Steel plate protection added to floor
blocks and endsill
floor blocks (Fig. 3.1) due to impact and abrasion by the bedload. The bedload consists of gravels and bouldersranging up to 24 in. in diameter. The concrete in the
apron in the impact area was abraded to a depth of 6 in.Except for very low flows and flows diverted for irri-gation, the bedload is carried over the weir.
SOLUTIONRepairs were made by extensive structural modifica-
tions. These modifications included the following (Fig.
3.2): 1) removing and replacing the top layer of rein-forcement in the apron; 2) removing and replacing thetop 6 in. of concrete; 3) protecting the apron with a ? n.
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REPAIR OF EROSION DAMAGED HYDRAULIC STRUCTURES 210.1R-15
steel plate; and 4) replacing the 24-in-round sluice gatewith a 36-in. square sluice gate.
PERFORMANCE
The structure has been operating satisfactorily sincerehabilitation in 1982.
DISCUSSIONFive alternatives were evaluated for the placement of
the diversion dam back into service. The ones notselected as the solution are as follows:
1. Install a reinforced concrete lining inside the wallsand apron of the existing structure.
2. Protect the apron with a 1/2-in. steel plate.3. Remove the entire apron of the structure and re-
place it with one that is adequately reinforced. Addthe liner inside the structure.
4. Remove the entire structure and replace it with anew one.
REFERENCES
U.S. Department of Agriculture, “Espinosa DiversionDam, Report of Investigation of Structural Failure,” SoilConservation Service, Albuquerque, NM, Nov. 1980.
U.S. Department of Agriculture, “Espinosa DiversionDam, Design Engineer’s Report," USDA, Soil Conserva-tion Service, Albuquerque, NM, Sept. 1982.
CONTACT/OWNER
State Conservation Engineer U.S. Department of Agriculture Soil Conservation
Service517 Gold Avenue, SW, Room 3301Albuquerque, NM 87102
KINZUA DAM
Allegheny River, Warren County, Pennsylvania
BACKGROUND
Kinzua Dam became operational in 1965. The stilling basin consists of a horizontal apron, 160 ft long and 204ft wide. It contains nine 7-ft-high by l0-ft-wide baffles,
located 56 ft upstream from the end sill. The vertical-faced end sill is 10 ft high and 6 ft wide. The basin slabwas constructed of concrete with a 28-day compressivestrength of 3000 psi.
The outlet works consists of two high-level and sixlow-level sluices. A maximum conservation flow of about3600 ft3/s is supplied by the high-level sluices. The low-level sluices with flared exists containing tetrahedraldeflectors are located 26 ft above the stilling basin slab.Bank-full capacity, 25,000 ft3/s, can be discharged throughthese sluices at reservoir elevation 1325. The maximum24,800-ft3/s record discharge was discharged through thesluices in 1972. The maximum velocity at the sluice exit
was 88 ft/s.
PROBLEM
Because of the proximity of a pumped-storage power- plant on the left abutment and problems from spray,especially during the winter months, the right side sluiceswere used most of the time. Use of these sluices causededdy currents that carried debris into the stilling basin.The end sill was below streambed level and contributed
to the deposition of debris in the basin.Divers reported erosion damage to the basin floor asearly as 1969. Also, piles of rock, gravel, and other debrisin the basin were reported. About 50 cubic yards of gravel and rock, ranging up to 8 in. in diameter, wereremoved from the basin in 1972. Abrasion-erosion dam-age reached a depth of 3.5 ft in some areas before initialrepairs were made in 1973 and 1974.
These repairs were made with steel fiber-reinforcedconcrete. Approximately 1400 cubic yards of fiber con-crete was required to overlay the basin floor. From thetoe of the dam to a point near the baffles, the overlaywas placed to an elevation 1 ft higher than the originalfloor.
In April 1975, divers reported several areas of abra-sion-erosion damage in the fiber concrete. Maximumdepths ranged from 5 to 17 in. Approximately 45 cubicyards of debris were removed from the stilling basin.Additional erosion was reported in May 1975, andanother 60 cubic yards of debris were removed from the
basin. At this point, symmetrical operation of the lower sluices was initiated to minimize eddy currents down-stream of the dam. After this change, the amount of debris removed each year from the basin was drasticallyreduced and the rate of abrasion declined. However,
nearly 10 years after the repair, the erosion damage had progressed to the same degree that existed prior to therepair.
SOLUTION
A materials investigation was initiated prior to thesecond repair, to evaluate the abrasion-erosion resistanceof potential repair materials. Test results indicated thatthe erosion resistance of conventional concrete contain-ing a locally available limestone aggregate was not accep-table (Fig. 3.3). However, concrete containing this same
aggregate with the addition of silica fume and a high-range, water-reducing admixture exhibited high compres-sive strengths (approximately 14,000 psi at 28 days’ age)and very good resistance to abrasion erosion. Therefore,approximately 2000 cubic yards of silica-fume concretewere used in a 12-in. minimum thickness overlay whenthe stilling basin was repaired in 1983 (Fig. 3.4).
Construction of a debris trap immediately downstreamof the stilling basin end sill was also included in therepair contract. Hydraulic model studies showed thatsuch a trap would be beneficial in preventing downstreamdebris from entering the stilling basin. The trap was 25 ftlong with a 10-ft-high end sill that spanned the entire
width of the basin.
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210.1R-16 ACI COMMlTTEE REPORT
10.0
9.0
8 . 0
2 . 0
1.0
0 A -STE EL FI B ER RE INF OR CE D CO NC RET E
REMOVED FROM THE KINZUA DAM STILL-
ING BASIN.
0B -CONVENTIONAL CONCRETE, PENN-SYLVANIA LIMESTONE AGGREGATE, 5710
PSI (39 MPa)
0C -CONVENTIONAL CONCRETE, LOS AN-
GELES AGGREGATE, 7470 PSI (52MPa).
0D -SILICA-FUME CONCRETE, LOS AN-
GELES AGGREGATE, 11,500 PSI (79MPa)
0E -S IL ICA-FUME CONCRETE, PENNSYL-
VANIA LIMESTONE AGGREGATE, 13,850P S I (95 MPa)
0 12 2 4 3 6 4 8 6 0 7 2
TEST TIME, HR
Fig 3.3-Kinzua Dam. Abrasion-erosion performance of 5 materials tested using the underwater abrasion-erosion test method
PERFORMANCE deep.In August 1984, after periods of discharge through the
upper and lower sluices, abrasion-erosion along somecracks and joints was reported by divers. The maximumdepth of erosion was about in. The divers also dis-
covered two pieces of steel plating that had been em- bedded in the concrete around the intake of one of the
lower sluices. Because of concern about further damageto the intake, the use of this sluice in discharging flowswas discontinued. This nonsymmetrical operation of thestructure resulted in the development of eddy currents.
Sluice repairs were completed in late 1984, and sym-metrical operation of the structure was resumed A diver inspection in May 1985 indicated that the condition of the stilling basin was essentially unchanged from the pre-ceding inspection. A diver inspection approximately 3 1/2
yr after the repair indicated that the maximum depth of
erosion, located along joints and cracks, was about 1 in.
REFERENCES
The next inspection, in late August 1984, found ap- proximately 100 cubic yards of debris in the basin. InSeptember 1984, a total of about 500 cubic yards of debris was removed from the basin, the debris trap, andthe area immediately downstream of the trap. The rock debris in the basin ranged from sand sized particles toover 12 in. in diameter. Despite these adverse conditions,the silica-fume concrete continued to exhibit excellentresistance to abrasion. Erosion along some joints ap-
peared to be wider but remained approximately 1/2-in.
Fenwick, W.B., “Kinzua Dam, Allegheny River, Penn-sylvania and New York; Hydraulic Model Investigation,”Technical Report HL-89-17, U.S. Army Engineer Water-ways Experiment Station, Vicksburg, MS, Aug. 1989.
Holland, T.C., “Abrasion-Erosion Evaluation of Con-crete Mixtures for Stilling Basin Repairs, Kinzua Dam,Pennsylvania,” Miscellaneous Paper SL-83-16, U.S. ArmyEngineer Waterways Experiment Station, Vicksburg, MS,Sept. 1983.
Holland, T.C., “Abrasion-Erosion Evaluation of Con-
crete Mixtures for Stilling Basin Repairs, Kinzua Dam,
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REPAIR OF EROSION DAMAGED HYDRAULIC STRUCTURES 210.1R-17
Fig. 3.4-Kinzua Dam. Typical silica-fume concrete placement operation for a stilling basin slab
Pennsylvania," Miscellaneous Paper SL-86-14, U.S. ArmyEngineer Waterways Experiment Station, Vicksburg, MS,Sept. 1986.
Holland, T.C.; Krysa, A; Luther, M.D.; and Liu, T.C.,“Use of Silica-Fume Concrete to Repair Abrasion-Ero-sion Damage in the Kinzua Dam Stilling Basin,” Fly Ash,Silica Fume, SIag, and Natural Pozzolans in Concrete,SP-91, V. 2, American Concrete Institute, Detroit, MI,1986, pp. 841-863.
McDonald, J.E., “Maintenance and Preservation of Concrete Structures, Report 2, Repair of Erosion-Damaged Structures,” Technical Report No. G78-4, U.S.Army Engineer Waterways Experiment Station, Vicks- burg, MS, April 1980.
CONTACT/OWNER
U.S. Army Engineer DistrictPittsburgh William S. Moorhead Federal Building1000 Liberty AvenuePittsburgh, PA 15222
LOS ANGELES RIVER CHANNELLos Angeles River, California
BACKGROUNDThe Los Angeles River Channel is an improved struc-
tural channel that drains a watershed of 753 squaremiles. The majority of the channel was constructed in the
1940s. In the invert of the concrete-lined main channel isa reinforced concrete low-flow channel, This low-flowchannel is approximately 12 miles long and was originally
constructed with an invert thickness of 12 in. Water vel-ocities in that channel range from 20 to 30 ft/s.
PROBLEM
Over the years abrasion erosion has occurred to vary-ing degrees along the low-flow channel, In some reaches,erosion had progressed completely through the concrete
by the early 1980s. This erosion was the result of a com- bination of abrasion by waterborne sediment and debris passing over the concrete, and chemical attack.
SOLUTION
Prior to repair, laboratory studies were conducted toevaluate the abrasion-erosion resistance of concretes con-taining locally available aggregates. Typically, these ag-gregates exhibit a relatively high abrasion loss testedaccording to ASTM C 131, using the Los Angeles mach-ine. Results of the laboratory tests indicated that con-crete with a high cement content, a silica fume contentof 15 percent by mass of portland cement, and a lowwater-cement ratio would provide excellent abrasion-erosion resistance, even when produced with aggregatesthat might be marginal in durability.
Beginning in 1983, the existing concrete in the approx-imately Yknile reach of most severe damage was re-moved and replaced with reinforced, silica-fume concrete(Fig. 35). The thickness of the replacement concrete was
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210.1R-18 ACI COMMITTEE REPORT
Fig. 3.5-Los Angeles River Channel. Concrete for a fu ll depth replacement was placed with a conveyor and finished with a specially shaped vibratory screed
12 in. Subsequent rehabilitation of the remaining channelduring 1984 and 1985 was accomplished by either full-
depth slab replacement or an overlay on the existing con-crete. Full-depth repairs consisted of a new, reinforced
base slab of conventional concrete and 6-in. overlay of
silica-fume concrete. Overlays on the existing concretewere 4- to 6-in-thick sections of silica-fume concrete.Various mixture proportions were used with compressivestrengths ranging from 8000 to 10,500 psi. Approximately27,500 cubic yards of silica-fume concrete were requiredto complete the rehabilitation. The unit costs for thesilica-fume concrete decreased with time as bidders be-came more familiar with the material. The unit cost for the 1985 project was $154/cubic yard, which was slightlyless than twice the unit cost of conventional concrete.
PERFORMANCE
Scour gauges were installed to monitor long-term wear of the silica-fume concrete. Because of the nature of themechanism causing abrasion-erosion, an evaluation of
performance will require an extended period of time.However, the abrasion resistance of the silica-fumeconcrete, according to the laboratory tests, should be twoto four times better than the conventional concrete pre-viously used Visual inspections of the channel surfacesindicate little or no erosion of the concrete has occurredin the 8 years following repair.
REFERENCES
Holland, T.C., “Abrasion-Erosion Evaluation of Con-crete Mixtures for Repair of Low-Flow Channel, LosAngeles River,” Miscellaneous Paper SL-86-12, U.S. Army
Engineer Waterways Experiment Station, Vicksburg, MS,Sept. 1986.
Holland, T.C., and Gutschow, R.A., “Erosion Resis-tance with Silica-Fume Concrete,” Concrete International,V. 9, No. 3, Detroit, MI, March 1987, pp. 32-40.
CONTACT/OWNER
U.S. Army Engineer District, Los Angeles300 North Los Angeles StreetLos Angeles, CA 90012
NOLIN LAKE DAM Nolin River, Edmonson County, Kentucky
BACKGROUND
Nolin Lake Dam became operational in 1963. Thestilling basin is 40 ft wide, 174 ft long with a 7-ft-high endsill and 35-ft-high sidewalls. The basin contains a para-
bolic section with an 8.4-ft drop in elevation from theoutlet tunnel invert to the horizontal floor slab. Thedesign discharge is 12,000 ft3/s with an average velocityof 61 ft/s entering the basin. The structure was built of reinforced concrete with a design compressive strength of 3000 psi.
PROBLEMThe conduit and stilling basin at Nolin were dewatered
for inspection in 1974, following approximately 11 yearsof operation. Erosion was reported in the lower portionof the parabolic section, the stilling basin floor, the lower
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REPAIR OF EROSION DAMAGED HYDRAULIC STRUCTURES 210.1R-19
part of the baffles, and along the top of the end sill. Themost severe erosion was in the area between the wall baf-fles and the end sill, where holes 2 to 3 ft deep had beeneroded into the stilling basin floor along the sidewalls.
SOLUTIONThe stilling basin was dewatered and repaired in 1975.
Conventional concrete designed for 5000 psi compressivestrength was used to restore the basin slab to an eleva-tion 9 in. above the original grade. A hydraulic modelstudy of the existing basin was not conducted, but thestructure was modified in an attempt to reduce theamount of debris entering the basin. New work includedraising the end sill 12 in., adding end walls at the end of the stilling basin, and paving a 50-ft-long channel section.
PERFORMANCEA diver inspection in 1976 indicated approximately 4
tons of rock was in the stilling basin. The rock, piled upto 15 in. deep, ranged up to 12 in. in diameter. Also,
l8-in.-deep rock piles were found on the slab down-stream from the stilling basin. Erosion, up to 8 in. deep,was reported for concrete surfaces that were sufficientlyclear of debris to be inspected.
In August 1977, approximately 1 to 11/2 tons of large,limestone rock all with angular edges, was reported inthe stilling basin. No small or rounded rock was found.Since the basin had been cleaned during the previous in-spection, this rock was thought to have been thrown intothe basin by visitors. When the stilling basin was de-watered for inspection in October 1977, no rock or debriswas found inside the basin. Apparently, the large amount
of rock discovered in the August inspection had beenflushed from the basin during the lake drawdown, whenthe discharge reached a maximum of 7340 ft3/s.
Significant erosion damage was reported when thestilling basin was dewatered for inspection in 1984. Themost severe erosion was located behind the wall baffles,similar to that prior to repair in 1975. Each scour holecontained well-rounded debris ranging from marble sizeto approximately 12-in. diameter. Temporary repairs in-cluded removal of debris from the scour holes and fillingthem with conventional concrete. Also, the half bafflesattached to each wall of the stilling basin were removed.
A hydraulic model of the stilling basin was constructedto investigate potential modifications to the basin to min-imize chances of debris entering the basin and causingsubsequent erosion damage to the concrete. Results of this study were incorporated into a permanent repair in1987. Modifications included rebuilding the parabolic sec-tion in the shape of a whale’s back, overlaying the basinfloor, adding a sloping face to the end sill, raising the
basin walls 2 ft, paving an additional 100 ft of the retreatchannel, slush grouting all derrick stone in the retreatchannel, and adding new slush-grouted riprap beside the basin.
The condition of the concrete was described as good
with no significant defects when the basin was dewatered
for inspection in August 1988. The maximum dischargeto that point had been 5050 ft3/s for a period of 13 days.
REFERENCESMcDonald, J.E., “Maintenance and Preservation of
Concrete Structures, Report 2, Repair of Erosion-Damaged Structures,” Technical Report No. C-784, U.S.
Army Engineer Waterways Experiment Station, Vicks- burg, MS, April 1980.
McDonald, J.E., and Liu, T.C., “Repair of Abrasion-Erosion Damage to Stilling Basins,” Concrete Interna-tional, V. 9, No. 3, American Concrete Institute, Detroit,MI, March 1987, pp. 55-61.
CONTACT/OWNER
U.S. Army Engineer District, LouisvilleP.O. Box 59Louisville, KY 40201-0059
PINE RIVER WATERSHED, STRUCTURE NO. 41La Plata and Archuleta Counties, Colorado
BACKGROUND
Structure No. 41 is a high velocity reinforced concretechute spillway with a St. Anthony Falls (SAF) stilling
basin. The SAF stilling basin is a design developed by theAgricultural Research Service at the St. Anthony FallsHydraulic Laboratory of the University of Minnesota.The design includes chute and floor blocks with an endsill sized by hydraulic modeling for maximum energy dis-
sipation. The floor of the basin in Structure No. 41 isdepressed about 4.6 ft below the downstream channelgrade. The design wall thickness is 8 in. and the designfloor thickness is 9 in. The reinforcement is a single matof steel centered in the floor and walls.
PROBLEMFrom 1974 to 1984 the structure had displayed signifi-
cant erosion of the concrete. The most severe erosionhad occurred at the lower end of the SAF stilling basin.The stilling blocks, end sill, and reinforcement was com- pletely deteriorated. The reinforcing steel was exposed inthe floor, sidewalls (Fig. 3.6), and wingwalls from immed-iately upstream of the end sill downstream through thestructure. The exposed reinforcement showed consider-able wear.
Erosion in the floor of the chute was limited to about in. This erosion appeared constant throughout thelength of the chute.
During a 1984 investigation, it was concluded that thedamage exhibited the characteristics of erosion and abra-sion damage by the ball mill effect, as described on pages14 and 15 of Chapter 1 of the Bureau of ReclamationConcrete Manual. The major damage to the structure isattributed to gravel and larger sized material being intro-
duced into the stilling basin from the outlet channel
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210.1 R-20 ACI COMMITTEE REPORT
Fig. 3.6-Pine River Watershed, Structure No. 41. Erosion of sidewall,exposing reinforcing steel
slope protection rock.The SAF outlet channel was designed and constructed
with a 3 to 1 adverse grade from the top of the end sillto the canal invert elevation, approximately 4 ft abovethe end sill. It has a bottom width of 10 ft with 2 to 1side slopes. The entire section is lined with loose rock riprap. The rock is rounded to subrounded and is easilydislodged. Much of the rock on the adverse slope ap-
pears to have been displaced and the slope eroded, sothat it is considerably steeper than originally constructed.Hydraulic transport of the smaller rock into the basinappears to be the method of debris introduction.
SOLUTIONThe investigating team made the following recommen-
dations:1. Study the hydraulics of the outlet and design an
outlet basin to fit most favorably with those pre-dicted by model studies. Minimize use of rock riprap but, if needed, grout to prevent movement.
2. Replace concrete end sill, floor blocks, and chute blocks using high-strength concrete. The effect onhydraulic performance will need to be studied.
A model study was conducted in 1984 to determinethe design for a preshaped, riprapped energy dissipation
pool. The design was recommended for the repair andrehabilitation of the structure and was also consideredappropriate information for use in the design of similar
pools.
PERFORMANCE No permanent work has been completed on the repair
of the structure to date. Options for repair are beingconsidered at this time.
REFERENCESBureau of Reclamation, Concrete Manual, 8th Edition,
U.S. Department of the Interior, 1981.Rice, C.E., and Blaisdell, F.W., “Energy Dissipation
Pool for a SAF Stilling Basin,” Applied Engineering in Agriculture, V. 3, No. 1, USDA-ARS, Stillwater, Okla-homa, 1987, pp. 52-56.
CONTACT/OWNER
State Conservation Engineer U.S. Department of Agriculture, Soil Conservation
ServiceSixth Avenue Central, 655 Parfet Street, Room E200C
Lakewood, CO 80215-5517
POMONA DAMHundred Ten Mile Creek, Vassar, KS
BACKGROUNDThe stilling basin at Pomona Dam, operational in
1963, is 35 ft wide and 80 ft long. The reinforced con-crete transition and horizontal basin floor have a designdischarge velocity of 58 ft/s. Two staggered rows of baf-fles, 3 ft wide and 5 ft high, are spaced at 7 ft on centers.A two-step, vertical-faced end sill is 4 ft high. Fill con-crete was placed the width of the basin for a distance of 20 ft downstream from the end sill.
PROBLEMThe initial dewatering of the basin in February 1968
revealed erosion damage at the downstream end of thetransition slab and on the upstream one-third of the
basin slab. This erosion, caused by the abrasive action of
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REPAIR OF EROSION DAMAGED HYDRAULIC STRUCTURES 210.1R-21
Fig. 3.7-Pomona Dam. Stilling basin condition several years after
completion of repairs
rocks and other debris, had exposed reinforcing steelalong the left wall of the basin. An inspection in October 1970 revealed significant additional erosion and extensiveexposure of reinforcing steel. The major damage was at-tributed to flow conditions at relatively low discharges,since approxima500 ft3/s or less.
tely 97 percent of the releases had been
SOLUTIONHydraulic model tests confirmed that severe separa-
tion of flow from one sidewall, together with eddy actionstrong enough to circulate stone in the model, occurredwithin the basin for discharges and tailwaters common tothe project. Various modifications including raising theapron, installing chute blocks, constructing interior side-
walls with reduced flare, and providing a hump down-stream of the outlet portal were model tested to evaluate
their effectiveness in eliminating the undesirable sepa-ration of flow and eddy action within the basin.
Based on the model study, it was recommended thatthe most practical solution was to provide a 3-ft-thick overlay of the basin slab upstream of the first row of
baffles, a l?&ft overlay between the two rows of baffles,and 1 to 1 sloped face to the existing end sill. Thissolution provided a wearing surface for the area of greatest erosion and provided a depression at the down-stream end of the basin for trapping debris. However,flow separation and eddy action were not eliminated bythis modification. Therefore, it was recommended that afairly large discharge, sufficient to create a good hy-draulic jump without eddy action, be released periodicallyto flush debris from the basin.
The final design for the repair included 1) a minimumY n.-thick epoxy mortar topping applied to approxi-
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210.1 R-22 ACI COMMITTEE REPORT
mately one-half of the transition slab; 2) an epoxy mortar applied to the upstream face of the right three upstream
baffles; 3) a 2-ft-thick concrete overlay slab placed on theupstream 70 percent of the basin slab; and 4) a slopedconcrete end sill. The reinforced concrete overlay was re-cessed into the original transition slab and anchored tothe original basin slab. The coarse aggregate used in the
repair concrete was Iron Mountain trap rock, an abra-sion-resistant aggregate. The average compressivestrength of the repair concrete was 6790 psi at 28 days.
PERFORMANCEThe stilling basin was dewatered for inspection five
years after repair (Fig. 3.7). The depression at the down-stream end of the overlay slab appeared to have func-tioned as desired. Most of the debris, approximately 1cubic yard of rocks, was found in the trap adjacent to theoverlay slab. The concrete overlay had suffered onlyminor damage, with general erosion of about -in. andmaximum depths of l -in. The location of the erosioncoincided with that occurring prior to the repair. Appar-ently, debris is still being circulated at some dischargerate. Based on a comparison of discharge rates and slaberosion, before and after the repair, it was concludedthat the repair had definitely reduced the rate of erosion.The debris trap and the abrasion-resistant concrete wereconsidered significant factors in this reduction.
The next inspection, in April 1982, indicated thestilling basin floor slab remained in good condition withessentially no damage since the previous inspection. Ap-
proximately 5 cubic yards of debris, mostly rocks, wereremoved from the debris trap at the downstream end of
the basin.
REFERENCESMcDonald, J.E., “Maintenance and Preservation of
Concrete Structures, Report 2, Repair of Erosion-Dam-aged Structures,” Technical Report No. C-784, U.S. ArmyEngineer Waterways Experiment Station, Vicksburg, MS,April 1980.
Oswalt, N.R., “Pomona Dam Outlet Stilling BasinModifications,” Memorandum Report, U.S. Army Engi-neer Waterways Experiment Station, Vicksburg, MS,1971.
CONTACT
U.S. Army Engineer District, Kansas City601 E. 12th StreetKansas City, MO 64106
PROVIDENCE-MILLVILLE DIVERSION STRUCTURE Near Logan, Utah
BACKGROUNDThe Providence-Millville Diversion Structure is a rein-
forced 60-ft-wide concrete drop structure, with a drop of
4 ft, a weir height of 4 ft, an apron length of 10 ft, anda sill height of 15 in. Two 4-by 4-ft slide gates in the rightabutment headwall direct flow from Blacksmith Fork intothe irrigation canal.
A considerable number of reinforced concrete diver-sion structures have been constructed in mountainstreams in the Western United States. These streams are
usually on a steep gradient and generally transport aheavy bedload of sands, gravels, and cobbles. Frequently permanent drops are incorporated in the diversion to provide the necessary head for diverting the irrigationflow, sluicing the bedload, and stabilizing the streamgradient.
PROBLEMIn spite of engineering practices such as providing
sluiceways, using grated inlet devices, and special en-trance configuration, the transported sediment causesabrasion to the exposed concrete in the diversions. Attimes of flood flows or above normal high water, exces-sive bedload (quantity and size of particles) also impartssevere impact to the surfaces of stilling basins or apronsof drop structures. This impact as well as the grindingaction of highly abrasive aggregate causes loss of con-crete, exposure of steel reinforcement, and, if unchecked,loss of the structure.
The bedload of sand, gravel, and boulder materials inBlacksmith Fork has caused erosion of the concrete inthe apron and walls of the Providence-Millville diversionstructure and consequent exposure of the reinforcingsteel (Fig. 3.8).
SOLUTIONFollowing the extreme flooding years of 1983 and
1984, the SCS (Soil Conservation Service) in Utah wasfaced with repairing or replacing a multitude of irrigationstructures that had been damaged or lost. The decisionwas made to make the repairs or replacements, usingsome of the proprietary concrete products available toenhance durability under high bedload conditions.
The new Providence-Millville structure was one of fivein which field trials were conducted for the evaluation of defensive measures available. The product selected for this site was a metallic aggregate topping. This product
consists of premixed metallic floor topping composed of iron aggregate, high-early portland cement, and water-reducing admixtures. A surface treatment was applied tothe hardened surface.
l-in-thick metallic aggregate topping was placed over a new concrete structure substrata following applicationof an epoxy or latex bonding aid. A proprietary sealer,recommended by the topping supplier, was applied to theoverlay surface to reduce permeability.
The cost for 604 square ft of surface treated was$ll.00/square ft (1986 price level.)
PERFORMANCEHigh water preventssclose inspection of the treated
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REPAIR OF EROSION DAMAGED HYDRAULIC STRUCTURES 210.1 R-23
Fig. 3.8-Providence-Millville Diversion Structure. Erosion of the surface of theconcrete apron and sidewalls
areas. Inspections since the installation indicate theoverlay is still intact. High water conditions and theaccompanying abrasive bedload have been only moderatesince the repairs in September 1986.
DISCUSSIONThis metallic floor topping hardener is supplied in pre packaged 55-lb bags, which is enough to apply a l-in.layer to a 18- to 20-square ft area. Installation must be inaccordance with the manufacturer’s directions.
The floor topping develops approximately 13,000 psicompressive strength in 3 days and is especially suited for
building floor slabs subjected to impact loads. While notspecifically marketed for use on hydraulic structures, itsabrasion-resistant properties are attractive. Performancein drop structures with heavy sediment bedloads has been
positive to date.
REFERENCESU.S. Department of Agriculture, “Memorandum,
Dated April 17, 1990, to Francis T. Holt, StateConservationist, SCS, Salt Lake City, UT, from RobertA. Middlecamp, Construction Engineer, SCS, West National Technical Center, Portland, OR.
CONTACT/OWNER
State Conservation Engineer Soil Conservation Service, U.S. Department of
AgricultureP.O. Box 11350Salt Lake City, UT 84147-0350
RED ROCK DAMDes Moines River, Iowa
BACKGROUND
Red Rock Dam, operational in 1969, is 6200 ft longand 95 ft high. The two rolled earth embankment sec-
tions of the dam are separated by a concrete section thatserves as the outlet works and spillway. The spillway hasan ogee crest with five 41-ft-wide by 49-ft-high tainter gates. The outlet works has fourteen 5- by 9-ft conduitsthrough the ogee section. Discharge from the spillwayand the outlet works passes into a 240-ft-wide by214-ft-long stilling basin, which has two rows of baffles.A minimum flow through the basin is 300 ft3/s, even indry seasons.
PROBLEMA diver inspection in 1982 detected several small areas
of eroded concrete and bedrock along the end sill Heavy precipitation during 1983 and 1984 resulted in large dis-charges ranging up to 40,000 ft3/s compared to normaldischarges of about 3000 ft3/s. Based on the finding of the diver inspection and because of subsequent high dis-charges, plans for repair were initiated.
Until recently, repairs of this type generally requireddewatering of the stilling basin. Dewatering costs can ex-ceed $1 million and have averaged 40 percent of the totalrepair cost in previous repairs. Since the damage to theend sill was not very severe, the high cost of dewateringthe basin for repair was considered inappropriate.
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210.1R-24
SOLUTION
ACI COMMlTTEE REPORT
CONCRETE WlTH
ANTI-WASHOUT ADMIXTURE
GROUT FILLED BAGS
#8 ANCHORS 8’ ONCENTERS
CEMENTITIOUS NONSHRINK GROUT
Fig. 3.9-Red Rock Dam. Diagram of concrete repair of stilling basin endsill
Results of laboratory tests indicated that cohesive,flowable, and abrasion-resistant concrete could be placedunder water by available methods without use of the tre-mie seal and withminimal loss of fines if proper mater-ials were used and precautions taken. Concrete contain-ing AWA (antiwashout admixture) and a water-reducingadmixture placed at the point of use sustained only arelatively small loss of fines and bonded well to in-place
hardened concrete. Consequently, underwater concretingwas selected as the most cost effective method for repair of the stilling basin.
Immediately prior to the repair in August 1988, a finalunderwater inspection of the basin indicated larger areasof erosion than in 1982, most occurring in the bedrock
just downstream of the end sill. The eroded areas ex-tended about 18 ft downstream from the end sill and hada maximum depth of 5 ft.
Construction requirements included removing looserock and debris, installing anchors and reinforcing,
positioning grout-filled bags to define the placement
area, and placing concrete by a diving contractor. Theminimum flow of 300 ft3/s was discharged through thedam during the repair (Fig. 3.9).
A concrete pump with a 4-in.-diameter line was usedfor underwater placement of the concrete. A diver con-trolled the end of the pumpline, keeping it embedded inthe mass of newly discharged concrete and moving itaround to completely fill the repair area. Approximately100 cubic yards of concrete were placed in about 4 hours.
The effects of the AWA were apparent; even thoughthe concrete had a slump of about 9 in., it was very co-hesive. The concrete pumped very well and, according tothe diver, self-leveled within a few minutes following
placement. The diver also reported that the concrete re-
mained cohesive and exhibited very little loss of fines onthe few occasions when the end of the pumpline kickedout of the concrete.
The total cost of the repair was $128,000 (1988 pricelevels). In comparison, estimated costs to dewater alonein a conventional repair ranged from $500,000 to$750,000.
PERFORMANCE
Although additional time will be required to evaluate performance, all indications are that the repair is an eco-nomical and durable solution to the problem.
REFERENCESMcDonald, J.E., “Maintenance and Preservation of
Concrete Structures, Report 2, Repair of Erosion-Dam-aged Structures,” Technical Report No. C-78-4, U.S. ArmyEngineer Waterways Experiment Station, Vicksburg, MS,April 1980.
Neeley, B.D., “Evaluation of Concrete Mixtures for
Use in Underwater Repairs,” Technical Report No.REMR-CS-18, U.S. Army Engineer Waterways Experi-
ment Station, Vicksburg, MS, April 1988. Neeley, B.D., and Wickersham, J., “Repair of Red
Rock Dam,” Concrete International, V. 11, No. 10, Amer-ican Concrete Institute, Detroit, MI, Oct. 1989, pp. 36-39.
CONTACT/OWNER
U.S. Army Engineer District, Rock IslandClock Tower BuildingP.O. Box 2004
Rock Island, IL 61204-2004
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REPAIR OF EROSION DAMAGED HYDRAULIC STRUCTURES 210.1R-25
SHELDON GULCH SIPHONBig Horn County, Wyoming
BACKGROUNDThe siphon consists of 1770 ft of 27-in-diameter
reinforced concrete pipe with a flared reinforced con-crete box outlet. The siphon replaces approximately two
miles of eroding, steep gradient, canal. A wasteway, usedto discharge excess water or provide for upline systemdrainage, was established at the inlet, discharging into theabandoned canal. Rock riprap was placed at the siphoninlet by the canal company after completion of the pro-
ject.
PROBLEMThe reinforced concrete basin experienced severe ero-
sion damage to the apron and wall. The damage appearsto have been caused by the introduction of rock from theriprap protection upstream from the structure. The abra-sion has the characteristics of erosion and abrasiondamage by the ball mill effect, as described by theBureau of Reclamation Concrete Manual (see refer-ences).
SOLUTIONRepairs of the apron and sidewalls were made by re-
placing the damaged area with polymer-modified port-land cement, two-component, fast-setting patchingmortar. Existing concrete in the abraded area of theapron and sidewalls was removed in accordance with pro-cedures detailed in Chapter VII of Reclamation’s Con-
crete Manual. The exposed area was prepared and the
mortar applied as directed in the manufacturer’s productsheet.
Riprap was stabilized by placing concrete over therock riprap at the siphon inlet and outlet to preventfurther rock removal and subsequent transport into thesiphon.
PERFORMANCEThe repairs were made prior to the 1991 irrigation
season. No opportunity has occurred for an inspection of the repairs to date.
DISCUSSIONAn alternate repair method, considered for this pro-
ject, was to apply a thin layer of patching mortar in areaswhere concrete erosion was greater than 1 in. This alter-native was more economical but considered inferior tothe selected method because of the laminations createdin the concrete section.
REFERENCESBureau of Reclamation Concrete Manual, 8th Edition,
U.S. Department of the Interior, 1981.
CONTACT/OWNER
State Conservation Engineer U.S. Department of Agriculture, Soil Conservation
ServiceFederal Building, Room 3124100 East B Street
Casper, WY 82601
CHAPTER 4-CHEMICAL ATTACK-ROSION CASE HISTORIES
BARCELONETA TRUNK SEWER Municipality of Barceloneta, Puerto Rico
BACKGROUNDThe Barceloneta Trunk Sewer, operational in 1976,
collects sewage from several pharmaceutical plants aswell as local domestic flows. It was built using regular reinforced concrete pipes conforming to ASTM C 76,with cast-in-place reinforced concrete manholes, spacednot farther than 280 ft.
The depth of the pipe invert below ground surfacevaries from a minimum of 5 ft to a maximum of 25 ft.
Flow from pharmaceutical plants is partially treated,mostly to reduce the biological oxygen demand (BOD),and remove larger solids. The pipeline is subject to awide range of pH, temperatures and chemical composi-tion, which varies frequently because of batch productionschedules for each of the pharmaceutical plants.
PROBLEMGround subsidence of the pipeline backfill appeared
along the sewer alignment. When these failures were in-vestigated, it was found that the pipe had seriouslydeteriorated. There were places where the concrete hadalmost completely disappeared.
SOLUTIONSeveral procedures to solve the problem were investi-
gated, including replacing the entire system. Replacingthe entire system was found to be costly and difficult,
because the pipe runs along the shoulder of a major road
that is the access to the pharmaceutical plants. It wasdecided to proceed with the rehabilitation of the systemusing a proprietary pipe-lining process.
This lining process is a method of installing a newsolid lining in an existing pipeline in which pipe segments
between manholes are relined in a single operation. The process consists of cleaning the existing pipe interior surfaces, then installing a flexible plastic-lined fiberglasshose impregnated with a polyester resin. The resin isactivated by circulating hot water through the hose for a
period of time. The hose is installed by filling it withwater under limited pressure. The water pressure alsoserves to expand the hose as required and. place it inintimate contact with the pipe wall.
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210.1 R-26 ACI COMMITTEE REPORT
Fig. 4.1-Dworshak National Fish hatchery. Deteriorationof concrete surface of tank Note repaired area to the left of
the photograph
In order to install the hose it is necessary to tem- porarily divert the flows, bypassing the section under rehabilitation. Waste flows controlled by the bypass sys-tem during rehabilitation averaged 2100 gallons per minute at the larger pipes.
Rehabilitation of over 17,000 ft of various diameter pipeline, ranging from 18-36 in., required 7 months. In
addition 68 manholes were rehabilitated, having diam-eters ranging from 48 to 72 in. and depths from 5 to 25ft.
PERFORMANCEAfter several years of uninterrupted use, the reha-
bilitated sewer is performing well with no evidence of deterioration.
DISCUSSIONThe rehabilitation process represents a cost-effective
and seemingly durable solution to chemical attack to
existing concrete sewer pipes.
CONTACT
Puerto Rico Aqueduct & Sewer AuthorityP.O. Box 7066Bo. Obrero Station SanturcePuerto Rico 00916
DWORSHAK NATIONAL FISH HATCHERYClearwater River, Near Orofino, Idaho
BACKGROUNDThe Dworshak NFH (National Fish Hatchery), opera-
tional in the late 1960s, is located at the confluence of the Clearwater and North Fork Clearwater Rivers, Idaho.A series of modifications and additions has brought thefacility to its present capacity of 470,000 pounds of fish
per year. The hatchery was designed as a reuse water facility, where only a small amount of makeup water isadded to supplement the flow and distribution system.
PROBLEMThe concrete surfaces exposed to hatchery water have
experienced chemical attack and surface removal of port-land cement paste (Fig. 4.1). Particles of sand in the con-crete have become exposed due to erosion of the weak-ened paste. This phenomenon has been previously re-
ported in areas where the concrete is attacked by water containing free CO2, flowing pure water from melting iceor condensation, and water containing little CO,. Thewater dissolves Ca(Ol , thus causing surface erosion.The Dworshak reservoir collects snowmelt from the
drainage basin and releases the pure water during theseasonal incubational and rearing phase of fish hatchery
production. The following table summarizes a typicalwater analysis for Dworshak NFH.
SOLUTIONThe most likely solution was to coat the concrete sur-
faces with some type of surface treatment to preventexposure to the pure water. Epoxy coatings, polymeric,and other coatings protect the hardened portland cement
paste at exposed surfaces. Trial coatings of epoxy mortar and a urethane coating, of approximately 500 square ft
each, were applied to damaged surfaces for evaluation(Fig. 4.1). After two years of exposure, the integrity of the coatings is intact, however, performance of thecoatings adjacent to joints and cracks is poor. An alter-nate solution may be to alter the pH of the water by ap-
propriate chemical additions, such as free lime, if it istolerable to the fish.
Parameter Value Unit
pH 6.5 to 7.4Total Dissolved Solids 28-33 mg/LSpecific Conductivity 23-29 *mhos
Hardness 12-15 mg/L
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REPAIR OF EROSION DAMAGED HYDRAULIC STRUCTURES 210.1R-27
AlkalinityChlorides, Cl-
Sulfates, SOg Nitrates, NO,-Sodium, Na+Potassium, K +
Calcium, Ca++
Magnesium, Mg++
CONTACT/OWNER
15-20 mg/LO-2-0.4 mg/L
2.0 ma0.07 ma1.44 mg/L0.55 mg/L3.75 mg/L
0.70 mg/L
U.S. Fiih & Wildlife ServiceDworshak Kooskia NFH ComplexP.O. Box 18Ahsahka, ID 83520
LOS ANGELES SANITARY SEWER SYSTEM ANDHYPERION SEWAGE TREATMENT FACILITYLos Angeles, California
BACKGROUNDThe sanitary sewerage system of the city of Los An-
geles includes over 6000 miles of sewers that service anarea of over 600 square miles.
There are two upstream water reclamation plants inthe San Fernando Valley. These are the D.C. Tillmanand the Los Angeles-Glendale plants. The sewage atthose plants is treated to advanced secondary standardsand discharged to the Los Angeles River. Their solids arereturned to the sewers for transport to the Hyperionregional treatment plant on the coast of Santa Monica
Bay.All of the remaining sewers of the service area enter
one of four major interceptors for conveyance to theHyperion plant. This 420 Mgal/d (million gallons per day) facility was originally designed for 265 Mgal/d to
provide primary (mechanical) treatment and a high rateactivated sludge secondary (biological) treatment to thesewage, and meet a discharge standard of 70 ppm (par-ticles per million particles) suspended solids and 70 ppm
biological oxygen demand (BOD). In 1957 the processwas modified so that 100 Mgal/d received secondarytreatment and is mixed with 320 Mgal/d that receives
only primary treatment. This mixed plant effluent isdischarged at sea, where dilution and dispersion ulti-mately render it innocuous. The ocean outfall extends 5miles to sea, to a water depth of 235 ft. In 1986 secon-dary treatment was expanded to 200 Mgal/d, and chemi-cals were added to enhance primary treatment.
PROBLEMOver 40 years ago, the pioneer research of Dr. Rich-
ard D. Pomeroy pinpointed the shortened life of the con-crete sanitary sewers in Los Angeles as being due to hy-drogen sulfide (II attack of septic sewage. His was theoriginal research that recognized the phenomenon.
By one definition, septic sewage is sewage that con-tains entrained Hm To be septic, the sewage in a warmclimate need only have an age of a few hours in thesewers. The H, is generated by sulfate-reducing anaer-obic bacteria confined in the slimes that line the con-tinuously wetted perimeter of the sewer, particularly inlow velocity (<2 ft/s) zones of flow. Under conditions of
laminar flow, the H= of septic sewage escapes the water surface at moderate rates, to attack the concrete abovethe waterline. The attack is the result of the H, beingoxidized by bacterial action and combining with water vapor to form H,SO,. So, more accurately, H, attack could be termed sulfuric acid attack on the concretesurfaces above the waterline (compare Fig. 4.2 and 4.3).Under conditions of turbulence, caused by high velocityflow or a plunging of the flow, as in a drop manhole(Fig. 4.4), the escape of H= from the waste-water ismuch more rapid, and the H, attack is much moresevere.
With this as background, the engineering conclusionsdrawn by the city of Los Angeles from their experiencesof the past 45 years will be recited.
SOLUTION-THE SEWER SYSTEMThe problem of H, attack in the sewer system is on-
going, and worsening. The long distances traveled toreach the Hyperion plant account for the plant influenthaving been in the sewers for 24 to 72 hours. That meansthat hundreds of miles of sewers are transporting septicsewage. Current policy is to use acid-resistant vitrifiedclay pipe for all sewers up to 42 in. ID (inside diameter)and PVC (polyvinyl-chloride) lined reinforced concrete
pipe for all diameters above that.The H= attack on the concrete pipe has become more
aggravated in recent years. Engineers have speculatedthat this aggravation is due to point-source control of toxic producers. In conformance with EPA regulations,many industries are required to pretreat their plant ef-fluent so as not to discharge toxins into the sewer systemthat could kiIl the bacteria in the biological reactors of the secondary treatment facilities at Hyperion. The ironyof the situation is that whereas previously the toxicity inthe sewers had tended to keep the growth of the H,-
producing bacteria under some measure of control, now
that lack of toxicity has permitted those bacteria tothrive. Unprotected concrete pipe, subjected to this lowtoxicity effluent, has failed within 5 years due to H,
attack.The City of Los Angeles engineering policy generated
as a result of these experiences is that:1. For all new concrete construction, protect the
inside of manholes and the inside crown of pipesabove the waterline with a sheet of acid-resistantPVC, mechanically anchored to the concrete.
2. For the repair of old concrete construction, restorethe concrete surface and then protect it with an ap-
plied coating or lining. It is at this point that thecity is still in the process of setting policv. There
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ACI COMMlTTEE REPORT
Fig. 4.2-Los Angeles Sanitary Sewer System. Typical new and undeteriorated condition of concrete pipe
Fig. 4.3-Los Angeles Sanitary Sewer System. Deterioration of concrete pipe from acid s attack
have been some bad experiences with spray-on coatings sideration.
(Fig. 4.5), resulting both from pinhole holidays and poor quality control of the constituent materials. Roll-on SOLUTION-THE PRIMARY SETTLING TANKS
plastic sheets have been successful, but the physical There are 12 primary settling tanks at the Hyperionsituation in sewers often precludes their use. Also plant; 4 more are under construction. Each of the tanksdemolition of the damaged structure or pipe and re- is 300 ft long, 56.5 ft wide, and 15 ft deep. Of the existing
placement with PVC-lined new construction is under con- 12 tanks, 8 were constructed in 1950, of unprotected rein-
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REPAIR OF EROSION DAMAGED HYDRAULIC STRUCTURES 210.1R-29
Fig. 4.4-Los Angeles Sanitary Sewer System. Deterioration of reinforced concrete structures from acid attack
Fig. 4.5-Hyperion Sewage Treatment Facility. Reinforced concrete sedimentation tank showing coating failure and corrosion
forced concrete. Four were constructed in 1957 and, under construction will be covered with an aluminum based on the experience of the original eight, were pro- roof.tected against HB attack by a PVC liner, above the HB is stripped as the sewage enters the tanks, throughwaterline, for 75 ft at each end. The first 12 tanks were
a baffle system, and again as it exits over V-notch weirs.covered with a 15-in. reinforced concrete slab, supported by a system of beams and columns. The four currently
These are two regions of turbulence, where the H,
levels are unusually high. In spite of the tranquil flow
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210.1R-30 ACI COMMITTEE REPORT
between these two regions, the tank roofs have sufferedcritically through the years, due to Ha attack. This wasfirst brought to the attention of the engineering com-munity in 1964, when Jack Betz’s paper, “Repair of Cor-roded Concrete in Wastewater Treatment Plant,” was
published in the Journal of the Water Pollution Control Federation. By the early 1960’s, the concrete above the
waterline in the launders (the effluent channel of the primary settling tank), and the soffit of the roof slabs,had been damaged to the point that the reinforcing had
been exposed The City decided to repair the damage bychipping back to sound concrete, anchoring steel meshon to the existing rebar, and applying a new concrete tothe surface. The system only lasted 20 years. By 1983, theconcrete above the waterline was in such bad shape thata second repair was initiated.
The 1983-87 repair program involved water blasting back to sound concrete, and restoring the concrete sur-face with shotcrete. This was then sprayed with a polymer coating. The system worked fairly well, but wherever there was a pinpoint holiday in the polymer coating, theH= attack would recur. Additionally, there were caseswhere the polymer failed to stop the reflection of ex-
panding cracks in the substratum. These cracks likewiseexposed the concrete to H, and water vapor.
As a result of the experiences of the design of the 8original primary settling tanks, and the 1963-67 and the1983-87 repairs of the erosion of the first 12 tanks, thecity adopted the following policies with respect to pro-tecting the concrete in the primary settling tanks:
1. For existing concrete above the waterline, remove
damaged concrete back to sound concrete and re-store the surface with shotcrete. Although policy isstill not set, the current practice is to protect thelining with a roll-on sheet plastic cemented to theconcrete. Spray-on coatings are generally not con-sidered to be a long-term solution.
2. For existing concrete and new construction belowthe waterline, protect the concrete with coal-tar epoxy. This is not related to the erosion of concretedue to H, attack, but rather to the issue of block-ing chlorides from penetrating into the perviousconcrete and attacking the reinforcement.
3. For new construction above the waterline, provide100 percent protection using PVC lining systems.
REFERENCESU.S. Environmental Protection Agency, “Process De-
sign Manual for Sulfide Control in Sanitary SewerageSystems,” EPA 625/l-74-005 and NTIS PB/260/479,Washington, DC, Oct. 1974.
American Concrete Pipe Association, Concrete Pipe Handbook, Vienna, VA, 1980.
American Society of Civil Engineers, “Manuals and
Reports on Engineering Practice, No. 60; WPCF, Manual of Practice, No. FD-5.
CONTACT/OWNER
City of Los AngelesHyperion Treatment PlantLos Angeles, CA
PECOS ARROYO WATERSHED, SITE No. 1San Miguel County, New Mexico
BACKGROUNDThe Pecos Arroyo Dam is a floodwater-retarding
structure constructed on C&ton Bonito, 5 miles northof Las Vegas, New Mexico. The dam is earthfill with aclay core and maximum height of 47 ft. It has a 600-ft-wide excavated earth spillway. The outlet consists of 304ft of 36-in-diameter reinforced concrete pipe, with anungated concrete riser inlet structure and a plunge pooloutlet.
PROBLEMThe outlet conduit concrete was severely deteriorated,
believed to be due to galvanic corrosion in combinationwith carbonic acid attack (Fig. 4.6). The apparent sourceof the chemical attack was saline water seeping from thecarbonaceous shale and limestone in the right abutment.Resultant corrosion of reinforcement had been aggra-vated by local galvanic cells at the steel spigot pipe endsin the low resistivity soils. No other apparent damageshad occurred Structural failure had not occurred but aserious safety hazard existed.
SOLUTIONThe existing 36-in. I.D. reinforced concrete pressure
pipe was lined with 304 ft of 32-in. O.D. high-density polyethylene (HDPE) pipe. The annular space betweenthe two pipes was pressure pumped full with 2.3 cubicyards of grout. A cast-in-place cantilever outlet replaced24 ft of existing downstream 36-in. pipe and cantilever support. The downstream outlet channel was enlarged to
prevent submergence of the pipe invert during normalflows. The total cost of the contract for the performanceof this work was $126,000.
Treatment of the abutment was considered unneces-
sary and was not provided.
PERFORMANCEAnnual inspections since installation have shown no
evidence of chemical attack. No flow has been observedin the drain system around the conduit. The length of theHDPE liner has stretched 1 to 2 in. longer than the con-crete conduit. This variation is in accordance with thedesign calculations.
DISCUSSIONTwo alternatives, other than lining the existing con-
duit, were considered in the design. The first was toremove and replace the existing conduit with a reinforced
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REPAIR OF EROSION DAMAGED HYDRAULIC Sl?WCTURES 21 0.1 R-31
Fig. 4.6-Pecos Arroyos Watershed, Site 1. Deterioration of concrete of outlet structure
concrete prestressed cylinder pipe made with Type Vcement. The second alternative was to abandon the exist-ing conduit and install another conduit in an altenativelocation. These alternatives were estimated to be morecostIy than the repair method used.
REFERENCESU.S. Department of the Interior, “Pecos Arroyo
Watershed, Site No. 1, Preliminary Design Report,” Soil
Conservation Service, Nov. 17, 1986.U.S. Department of the Interior, “Pecos ArroyoWatershed, Site No. 1, Final Design Report,” SoilConservation Service, Dec. 4, 1987.
CONTACT/OWNER
State Conservation Engineer U.S. Department of Agriculture, Soil Conservation
Service517 Gold Avenue Southwest, Room 3301Albuquerque, NM 87102
CHAPTER 5-PROJECT REFERENCE LIST
While compiling information on suitable projects toinclude in this compendium of case histories, many casesof erosion damage were reported. Most were not suitablefor inclusion because sufficient information on thedamage and subsequent repair was not readily available.Many other cases were similar to those cases selected for inclusion. Table 5.1 provides a listing of projects reported
to have experienced erosion damage of the type de- _
scribed in this report. It is not clear if repairs have beeninitiated for all the listed projects. Additional informationon specific dams is available in the World Register of
Dams, published by the International Commission onLarge Dams in 1984, 3rd Edition, and in a 1988 FirstUpdating by the same publisher.
1 in.1 ft.1 in2
1 ft.21 in.31 ft.3
1 yd31 lb.1 IbJin.2 (psi)
1 ft./s1 ft?/s1 mi.1m.P
1 Mgal/d
Metric Conversions
25.4 mm0.3048 m645.1 mm2
0.0929 m2
16.39 x 104 mm3
0.0283 m3
0.7646 m3
0.4536 kg6.894 MPa
0305 m/s2832 l/s1609 m2590 km2
43.821 l/s
Temperature‘c = 9 - 32)/l.8
Difference in temperature‘c = tffl.8
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210.1R-32 ACI COMMITTEE REPORT
TABLE 5.1 - REFERENCE LIST OF EROSION AND REPAIR OF CONCRETE STRUCTURES
Project name
Alcova Dam
Alder Dam
Arkabutla Lake
Arthur R. Bowman Dam
Barren River Lake
Belton Dam
Blue Mesa Dam
Blue Ridge Dam
Bonneville Dam
Bratsk Dam
Type of structure
Spillway
Plunge Pool
Type of erosion
Chemical attack
Abrasion
Bull Shoals Lake Dam
Project location
Casper, WY
I
Centrailia, WA
Coldwater, MS
Oregon
Glascow, KY
Belton, TX
Colorado
Toccoa River, GA
Bonneville, WA
IBratsk, Irkutsk, U.S.S.R.
Mountain Home. AR
Stilling basin
Tunnel outlet works
Stilling basin and outlet works
Stilling basin
Diversion tunnel
Spillway and stilling basin
Stilling basin
Spillway Sluices and stilling basin
Abrasion
Cavitation
Abrasion
Abrasion
Abrasion
Abrasion
Abrasion
CavitationI
Abrasion and cavitation
Burfell Dam Selfoss, Arnesssyla, Iceland
Canyon Ferry Dam Townsend, MT
Causey Dam Ogden River, UT
Cave Run Dam Farmer, KY
Center Hill Dam Carthage, TNCherokee Dam Holston River, TN
Chickamauga Dam Hamilton County, TN
Chief Joseph Dam Columbia River, WA
Conchas Dam Tucumcari, NM
Sand sluice Abrasion
Stilling basin and outlet works Abrasion
Stilling basin and outlet works Abrasion and cavitation
Stilling basin Not listed
Stilling basin Abrasion and cavitationSpillway apron and stilling basin Abrasion
Spillway piers, weirs, and stilling Abrasion basin
Stilling basin Abrasion and cavitation
Stilling basin Abrasion
Curwensville Lake Dam
Derbendikhan Dam
Douglas Dam
Curwensville, PA
Sulaymaniya, Iraq
Sevier County, TN
Stilling basin and outlet works
Spillway
Outlet works, sluiceway, and
Abrasion
Cavitation
Abrasion and cavitation
Douglas Dam
Detroit Dam
Sevier Countv. TN
apron
Stilling basin Abrasion and cavitation I
1 Salem. OR Stilling basin and conduit 1 Abrasion and cavitation
Echo Dam
Emigrant Dam
Enid Dam
Folsom Dam
Grand Coulee Dam
Wader River, UT
Emigrant Creek, OR
Grenada, MS
Folsom, CA
Columbia River. WA
Stilling basin
Stilling basin
Stilling basin and outlet works
Stilling basin
Spillwav
Abrasion
Abrasion
Abrasion
Abrasion
Cavitation
Guri Dam
Haystack Dam
Hiwassee Dam
Howard Prairie Dam
Ice Harbor Dam
Itha Solteira Dam
Karoon DamKentucky Dam
Krasnoyarsk Dam
Lac qui Parle Dam
Libby Dam
Iindsay Creek Culverts
Little Goose Dam
Mason Dam
Mayfield Dam
McCloud Dam
McNary Dam
Venezuela
Madras, OR
Hlwassee River, NC
Beaver Creek, OR
Pasco, WA
Parana River, Brazil
Masjed Soliian, IranTennessee River, KY
Krasnoyarsk, U.S.S.R.
Montevideo, MN
Kootenia River, MT
Lewiston, ID
Starbuck, WA
Baker, OR
Mayfield, WA
I
Redding, CA
Umatilla, OR
Spillway and flip bucket
Stilling basin
Outlet works
Cavitation
Abrasion
Cavitation
Stilling basin Abrasion
Stilling basin Abrasion
Stilling basin Abrasion
3 Chute spillway cavitationSpillway and stilling basin Abrasion
Spillway flip bucket Cavitation
Stilling basin Abrasion
Stilling basin and outlet works Abrasion and cavitation
Box culvert Abrasion
Stilling basin and navigation lock Abrasion and cavitation
Conduit cavitation
Plunge pool Abrasion and cavitation
Spillway Abrasion and cavitationt
Stilling basin Abrasion
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REPAIR OF EROSION DAMAGED HYDRAULIC STRUCTURES 210.1R-33
TABLE 5.1 (cont.) - REFERENCE LIST OF EROSION AND REPAIR OF CONCRETE STRUCTURES
Mica Dam British Columbia 3 Bay chute Pitting
Milford Dam Junction City, KS Stilling basin Abrasion
Navajo Dam Farmington, NM Stilling basin and outlet works Abrasion and cavitation
Nimrod Lake Da m Danville, AR Stilling basin Abrasion
Norris Dam Clinch River, TN Stilling basin and outlet works Abrasion and cavitation
Norris Dam Clinch River, TN Spillway apron Abrasion
Nurek Dam Tadjik SSR, U.S.S.R. Tunnel and chute Abrasion
Oologah Lake Dam Tulsa, OK Stilling basin Abrasion
Oxbow Dam Homestead, OR Spillway Abrasion
Painted Rock Dam Ravalli County, MT Outlet works tunnel Abrasion and cavitation
Palisades Dam
Irwin, ED
Outlet works chute Abrasion and cavitation
Perry Dam
Pine Flat Dam
Perry, KSI
Fresno, CA
Redding, CA
Redding, CA
Hermitage, MO
Stilling basin
Spillway
Abrasion
Abrasion
Pit No. 6 Dam
Pit No. 7 Dam
Pomme de terra Dam
Stilling basin and spillway
Stilling basin and spillway
Stilling basin
Abrasion and cavitation
Abrasion and cavitation
Abrasion
Rathbun Dam
Ririe Dam
Ruedi Dam
San Gabriel No. 1 Dam
Table Rock Lake Dam
Tarbela dam
Tiber Dam
Rathbun, IA
Ririe, ID
Colorado
Azusa, CA
Branson, MO
Pakistan
Montana
Stilling basin and outlet works
Stilling basin
Outlet works
Stilling basin
Stilling basin and conduit
Spillway and outlet tunnels
Outlet works
Abrasion
Abrasion and cavitation
Cavitation
Abrasion
Abrasion
Abrasion and cavitation
Abrasion
Tionesta Dam
Tuttle Greek Dam
Tygart Dam
V.I. Lenin Volga Dam
Tionesta, PA
Manhattan, KS
Grafton, WV
U.S.S.R
Stilling basin
Stilling basin and outlet works
Stilling basin
Baffle piers
Abrasion
Abrasion
Abrasion
Cavitation
Walter F. George Dam Fort Gaines, GA Stilling basin I Abrasion
Warsak DamWebbers Falls Dam
Wilson Dam
Wilson Dam
PakistanWebbers Falls, IL
Tennessee River, AL
Tennessee River, AL
Stilling basin and spillway AbrasionStilling basin Abrasion and cavitation
Spillway apron and stilling basin Abrasion
Outlet works cavitation