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Page 1: “Environmental Friendly Techniques in Textile Sector” Conference/Day … · Parameters Conventional Process Bio-Scouring Process Difference Total turns 33 20 - 13 turn Batch time

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“Environmental Friendly Techniques in Textile

Sector”March 20th, 2016

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GIZ - General Facts & Figures

Established: Since January 1st, 2011 GIZ encompasses the

competences and experiences of DED, GTZ and InWEnt.

The former GTZ was established in 1975.

Type of Firm: Company owned by the German Federal Govt.

Main client: German Federal Ministry for Economic Cooperation and

Development (BMZ)

Other clients: Other German federal ministries, partner-country,

governments and international clients such as the ADB,

EC, UN, World Bank as well as private enterprises

GIZ supports the German Government in achieving its objectives in the

field of international cooperation for sustainable development.

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GIZ World Wide

GIZ operates in 130 countries

Head offices in Eschborn und Bonn

GIZ employs some 17,000 staff worldwide, of whom more

than 60% are national personnel.

Additionally there are

- 1,300 development aid workers

- 750 integrated and 324 returning experts (CIM)

- 700 national staff of partner organisations

- 850 weltwärts volunteers 31.03.2016

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GTZ Head Office, Eschborn

GTZ Berlin, Germany

GTZ Bonn, Germany

GTZ local presence

Offices for German development

cooperation

GTZ Brussels, Belgium

GIZ Offices

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Positioning of IGEP

GIZ – India

Sustainable Economic

Development Energy

Environmental Policy, Conservation & Sustainable Use of Natural

Resources

Urban and Industrial Environmental Policy and

Management

Natural Resources Management

Indo-German Environment Partnership

Sanitation

Environment, Economy &

Socio-Economic Development

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Municipal Solid Waste Management

Slum-free Cities

Waste Water Management

Environmentally Friendly Techniques

Urban-industrial Climate Change incl. Disaster Risk

Management

Planning of New Industrial Parks & Investment Zones

Natural Resources Accounting in

Selected Sectors

Environmental Fiscal Reform in the Area of Waste & Waste Water

Resource Efficiency & Sustainable

Consumption

Sustainable Urban Habitat

Sustainable Industrial Development

Policy for Environment and Climate

Core Topics

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“Environment Friendly

Techniques in Textile Sector”

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Objective

Use of environment-friendly technologies and techniques is

promoted in selected industry sectors, particularly from Small

and Medium Enterprises (SMEs).

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To the identified problems of concern, potential solutions

were identified based on:

BREF (best available techniques reference) documents;

Cleaner Production measures implemented in industries;

Solutions available in the market; International Case

Examples & National / Local Case Examples

Identified 18 potential measures as “suggestive

measures”.

Identified 15 potential measures/ techniques that could be

tested in pilots having best practice and policy dimensions

by GIZ.

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“Pilot Measures in Textile Sector”

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Pilot 1: Replacement of alkaline scouring with bio-

scouring enzyme for enzymetic scouring.

Problem:

Scouring produces strongly alkaline effluents (around pH 12.5)

with high organic loads,

High concentrations of Total Dissolved Solids (TDS), oil and

grease in wastewater

Needs caustic boil & chlorine in process

Pilot measure:

Bio-scouring enzyme for enzymatic scouring

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Parameters Conventional Process Bio-Scouring Process Difference

Total turns 33 20 - 13 turn

Batch time 18 Hrs 10 Hrs - 8 Hrs

No. of drains 13 8 - 5 Drains

Water

consumption

3900 lit / batch 2400 lit/ batch - 1500 lit/

batch

Chemical cost 5.88 4.98 - 0.9 Rs./kg

Labor cost 1.05 0.58 - 0.47 Rs./kg

Electricity 0.72 0.36 - 0.36 kW/kg

Steam 1000 500 - 500

kg/batch

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Cost Benefit Analysis:

The processing cost of fabric reduced to Rs. 3.91 per kg of

fabric from Rs. 5.15 per kg of fabric.

There is no capital cost only replacement of chemical (although

10 % additional cost compared to existing chemicals in some

cases)

Total savings Rs. 50,22,000 per annum.

When & Where Implemented:

M/s Mangal Textile, Ahmedabad & M/s Komal Texfeb, Ahmedabad

replaced the alkaline scouring with bio scouring in 2013.

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Pilot 2: Caustic Soda Recovery System.

Problem:

In mercerization process, fabric is washed with water to remove

un-reacted caustic soda (98 to 99 % of unreacted caustic)

Wash water contains substantial amount of caustic soda which

is resource loss

Generates pollution in the wastewater (higher COD, TDS, TSS,

alkalinity etc).

Pilot measure:

Caustic Soda Recovery System

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Cost Benefit Analysis:

Capital cost was Rs. 92,40,000

Operating costs of Rs. 48,21,000 per annum

Total savings of Rs. 1,42,00,000

Payback period of 12 months.

When & Where Implemented:

M/s Shyam Corporation, Ahmedabad installed the caustic recovery

plant in 2013.

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Pilot 3: Recycle/reuse of cooling water and condensate

water as boiler feed water.

Problem:

Jet dyeing machines equipped with common heat exchangers

used for both heating and cooling

Cooling & Condensate water is drained with other effluent

Increasing fresh water consumption as well as effluent quantity

& load at ETP.

Pilot measure:

Cooling water from jet dyeing machines is reused as process hot

wash water on soft flow dyeing machines, RFD (Ready For

Dyeing) machines, etc.

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Cost Benefit Analysis:

Capital cost was Rs. 11,00,000

Operating cost (10 HP pump operation)

to Rs. 1,96,000 per annum

Resulted in saving of Rs. 12,12,000 (Rs.

5,94,750 fuel cost + Rs. 6,17,760 fresh

water pumping cost) per annum

Payback period of 13 months

When & Where Implemented:

M/s Komal Texfab, Ahmedabad installed the

recovery system plant in 2013.

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Problem:

Problems associated with manual methods of preparing

solutions are following:

Errors in manually calculating amount of dyestuff, auxiliary and

water.

Manually weighing of precise amount of required dye takes time

and skill, risk of mistakes in a busy production environment is

high.

Manually dispensing auxiliaries and water accurately is very

time consuming.

Variations in water temperature can affect the stability and

accuracy of solutions for certain dyestuffs.

Pilot 4: Auto Colour Dispensing through

Spectrophotometer & Chemical Dispensing System.

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Pilot measure:

An infrared exhaust laboratory-dyeing machine with a fully

automated dosing system.

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Cost Benefit Analysis:

Capital cost was Rs. 2,00,00,000,

Minimum operating and maintenance cost

Total savings is Rs. 62,64,000 per annum

Simple payback of 3.5 years.

When & Where Implemented:

M/s Komal Texfab, Ahmedabad Auto Dispensing System (Aral,

Israel), Spectrophotometer (gretagmacbeth) and IR dyer

(Copower) were installed by industry in year 2011.

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Pilot 5: Low Liquor Ratio Jet Dyeing Machines.

Problem:

Current Jet dyeing machines operate at a liquor ratio of 10:1

Resulting in excess water consumption and excess waste water

generation

Pilot measure:

Machines of newer designs operate at a liquor ratio of 7:1

These machines usually incorporate low-friction Teflon internal

coatings and advanced spray systems to speed rinsing.

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Cost Benefit Analysis:

Capital cost of 900 kg/hr machine was Rs. 1.25 crore,

Reduced operating cost than conventional jet dyeing machines

Total savings was Rs. 18,90,000 per annum

Payback period of 80 months (Excluding cost of chemicals

saving & waste water treatment & disposal cost).

When & Where Implemented:

M/s Komal Texfab, Ahmedabad installed low liquor ratio machines

in 2009.

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Pilot 6: Reuse of Treated Water for Washing at Printing

Machines.

Problem:

Screen are washed on every change of pattern & colour.

Frames also need washing on change overs.

Printing machine requires 1500 lit/hr for continuous cleaning of

the blanket and screens

Wash water generated is treated in ETP.

Pilot measure:

ETP plant treated water is recycled for its use in cleaning

process of screen & frames

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Cost Benefit Analysis:

Capital cost was Rs. 3,00,000,

Operating cost (7.5 HP pump running) of Rs 86,000 per annum

Total savings of Rs 2,58,000

Payback period of 21 months

When & Where Implemented:

M/s Komal Texfab, Ahmedabad started reusing ETP treated water

for washing in 2013.

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Pilot 7 (A): Recycle/reuse of cooling water and

condensate water as boiler feed water.

Problem:

Jet dyeing machines equipped with common heat exchangers

used for both heating and cooling

Cooling & Condensate water is drained with other effluent

Increasing fresh water consumption as well as effluent quantity

& load at ETP.

Pilot measure:

Cooling water and the condensate is recovered completely from

jet dyeing machines and reused as boiler feed water

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Cost Benefit Analysis:

Capital costs was Rs. 3,00,000

Operating cost (10 HP pump operation) to Rs. 3,13,000 per

annum

Resulted in saving of Rs. 33,00,000 per annum

Payback period of 3 months

When & Where Implemented:

M/s Rinkoo Processors, Ahmedabad installed the recovery system

plant in 2010.

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Pilot 7 (B): Reuse of Treated Water for Washing at

Printing Machines.

Problem:

Screen are washed on every change of pattern & colour.

Frames also need washing on change overs.

Printing machine requires 1500 lit/hr for continuous cleaning of

the blanket and screens

Wash water generated is treated in ETP.

Pilot measure:

ETP plant treated water is recycled for its use in cleaning

process of screen & frames

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Cost Benefit Analysis:

Capital cost was Rs. 1,00,000,

Operating cost (6 HP pump running) of Rs 1,69,000 per annum

Total savings of Rs 3,46,500

Payback period of 10 months

When & Where Implemented:

M/s Rinkoo Processors, Ahmedabad started reusing ETP treated

water for washing in 2010.

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Pilot 8: Batch Washing in Place of Continuous Washing

in Jet Dyeing Machine.

Problem:

In Jet Dyeing Machine continuous washing is carried out with

fresh water to remove the unexhausted dyes and chemicals

5000 litre / batch of water is consumed without any real

requirement and as a normal practice.

Pilot measure:

Batch / Intermittent washing is applied with fresh water intake of

three cycles in batch manner instead of continuous flow of water

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Cost Benefit Analysis:

The reduction in water consumption was approx. 39600 KL per

annum on 11 nos. machine

Without any capital cost or operating costs

Saving of Rs. 3,05,000 per annum (pumping cost only)

Immediate Payback.

When & Where Implemented:

M/s Rinkoo Processors, Ahmedabad started the batch washing in

2010.

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Pilot 9: Reuse of Alkaline Stream from Mercerising.

Problem:

In mercerising process, fabric is treated with caustic soda

(NaOH) solution

The alternate to recover caustic is caustic recovery plant

Requires high capital investment and running cost in form of

steam and manpower

Pilot measure:

Alkaline stream is collected in underground tanks

50O caustic stream is reused for next batch

20O caustic stream is pumped to overhead tank and is supplied

to individual jigger machines for use in dyeing (alkaline stream

is used for boiling and bleaching of fabrics)

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Cost Benefit Analysis:

Capital cost was Rs. 5,00,000

Negligible operating cost

Total savings of Rs. 5,40,000 per annum

Payback period of 12 months.

When & Where Implemented:

M/s Rinkoo Processors, Ahmedabad started reusing alkaline

stream for dyeing in 2010.

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Pilot 11: Installation of Variable Frequency Drive in Jet

Dyeing Machine.

Problem:

In Jet Dyeing higher pressure of 3.5 kg/cm2 is required to

ensure uniform dyeing

Lower pressure of 1.5 kg/cm2 is required for creating movement

of the fabric

Pump is made to operate on much more than the required

pressure or is throttled to get the required pressure

Electricity is wasted

Pilot measure:

Retro fitment of a VFD armed with PLC based control gear to

the Jet Dyeing Machine

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Cost Benefit Analysis:

Capital cost of one 12.5 HP VFD is Rs. 30,000,

Operating costs is negligible

Total savings of Rs. 55,000 per annum

Payback period of 7 months.

When & Where Implemented:

M/s Rinkoo Processors, Ahmedabad installed VFDs on 11 nos. of

Jet Dyeing machines in 2010.

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Pilot 12: Water Consumption Optimisation at Jigger

Machines.

Problem:

In overflow rinsing, clean water is drained through an overflow

weir usually set near a normal running level.

Overflow rinsing is inefficient in terms of water use

3 times (1200 litre/batch) higher flow rate of overflow water

required.

Pilot measure:

Installed two separate water lines for jigger machines

For water filling (1.5 inch) with auto timer based controller to fill

required quantity of water

For overflow (0.5 inch) line with auto timer controller which

allows only 400 litre per 20 minutes and stops the water flow

after one turn.

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Cost Benefit Analysis:

Capital cost was Rs. 2,00,000 per jigger

Water saving of 360 KL/yr.

Although the fresh water cost is not significant, the payback in

this case is not fast considering the fresh water cost only.

When & Where Implemented:

M/s Mukesh Industries, Ahmedabad started the Jigger water

optimisation in 2010.

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Pilot 13: Optimisation of Heat Energy in Jigger Machines.

Problem:

High heat quantity is required to raise the water temperature in

Jigger

Steam pressure (3 kg/cm2) leads to higher velocity through the

water bath, which escapes to atmosphere without delivering the

heat and increase the steam consumption

Average specific steam consumption at jigger machine is 1.5 to

2 kg of steam per kg of fabric.

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Pilot measure:

Water supplied to the jigger is from condenser cooling water

(soft water) of caustic recovery plant at 50 0C

Water is preheated and will need steam only to raise

temperature from 50 0C to average 85 0C.

Hot water is further heated in closed tank with direct steam

injection at 1 kg/cm2g pressure only to utilise the full heat

content of the steam

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Cost Benefit Analysis:

Capital cost of various modifications was Rs. 13,50,000

Total savings of Rs. 8,70,000,

Negligible operating cost

Payback period of 18 months

When & Where Implemented:

M/s Mukesh Industries, Ahmedabad done the modification in 2011.

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Pilot 14: Flash Steam Recovery of Drying Range to

Preheat Boiler Feed Water.

Problem:

A typical 16 cylinder dryer requires 110 kg steam input per hour

for 2400 m/hr fabric running rate

Steam after condensation comes out of the dryer cylinder at

approx. 2 kg/cm2g pressure collected in an open tank, flash

steam generates due to sudden change in pressure.

Flash steam goes into atmosphere as waste.

The industry is having 4 nos. of drying ranges with average 45

KL/day condensate generation from each range.

Pilot measure:

Industry designed a simple system to recover this flash steam

and raise the temperature of boiler feed water

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Cost Benefit Analysis:

Capital cost for modification was Rs. 1,00,000

Savings due to reduction in fuel consumption of Rs. 35,67,000

per annum

Negligible operating cost

Payback period of 10 days.

When & Where Implemented:

M/s Mukesh Industries, Ahmedabad installed the system for heat

content utilisation from flash steam in 2012

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Pilot 15: Heat losses optimisation at cylinder drying

range.

Problem:

A typical 16 cylinder dryer requires 110 kg steam input per hour

for 2400 m/hr fabric running rate

The side plates of cylinders, are not insulated and losses heat to

the surrounding area.

Major challenges for insulating the side plates of a cylinder dryer

are :

Cylinder dryers rotates at 50-60 rpm

Normally industries insulate with glass/mineral wool

Water resistance of mineral wool is very low and thus gaining

moisture by insulation makes it conductive to heat loss

Normally insulation peel off within 2-3 month of installation

Due to low moisture resistance and holding of moisture within

insulation promotes corrosion

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Pilot measure:

Side plates of drying range are insulated with more durable (life

& properties) mineral/rock wool, which can result in reduction of

steam consumption.

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Cost Benefit Analysis:

Capital costs of the insulation Rs. 35,000 for 12 m2 surface area

No operating costs involved

Total saving is Rs. 1,16,000

Payback period of 4 months.

When & Where Implemented:

M/s Mukesh Industries, Ahmedabad insulated the side plates in

2014

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Pilot 16: Optimisation of exhausts by controlling the

exhaust humidity with automation

Problem:

In Cotton Printing, Stenter is used before printing but after pre-

treatment.

In case of Polyester or PC Dyeing, stenter is used twice

Only 5.4% of heat given to stenter is utilized in heating the fabric

in case of Heat Setting.

Heat gained by fabric in any typical stenter operation is 4.6%

only.

It is further evident that approx. 95% stenters is used for the

purpose of moisture evaporation, released to atmosphere or

wasted.

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Pilot measure:

Installing the Stenter exhaust moisture controlling system

(retrofit)

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Cost Benefit Analysis:

Capital costs of the insulation is Rs. 1,65,000,

No operating costs involved,

Estimated saving is Rs. 1,85,000 (@ 5 % savings)

Payback period in 11 months..

When & Where Implemented:

M/s Mukesh Industries, Ahmedabad is installing the device in 2014

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Pilot 17: Efficient Boiler Operation.

Problem:

Highest efficiencies been secured with coal are in the range of

50-82%

Combustion efficiency of the boiler was found to be only 80 %

while of efficient boilers is more than 90 %.

The reasons for low combustion efficiency are:

The heat transfer is poor due to low heat transfer area and short

contact time between flue gas and the water.

The fuel charging door remains more or less open during the

entire operation due to various reasons, mostly human errors

There is no control over fuel firing in combustion chamber

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Pilot measure:

Replaces the existing non-efficient boiler with the efficient 6

TPH capacity boiler with ESP system to take care the air

emissions as well.

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Cost Benefit Analysis:

The capital cost of the boiler is Rs. 85,00,000 (excluding ESP)

Operating cost remains the same while it will reduce due to

consideration of latest technologies and control of the boiler

system,

Total savings of Rs. 50,00,000

Payback period of 21 months

When & Where Implemented:

M/s V R Polyfab, Ahmedabad commissioned the new boiler in

2014

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Pilot Measures Implemented in Ahmedabad

Pilot Benefits Status

Process Development:

Bio- Scouring in place

of Alkaline Scouring

Water consumption reduction:

45.45%

Chemical consumption reduction:

8.65%

Electrical power consumption

reduction: 37.04%

Fuel (coal) consumption reduction:

24.55%

Reduction in boiler emissions

Reduction in waste water

generation (quality & quantity)

Implemented:

Mangal Textile,

Ahmedabad

Komal Texfeb,

Ahmedabad

Trials (Positive

Results)

Vinod Textile,

Ahmedabad

Shyam Textile,

Ahmedabad

Aakash Fashion,

Ahmedabad

Chemical Recovery &

Reuse – Caustic

Chemical (Caustic) consumption

reduction: 93%

Reduction in waste water

generation (quality & quantity)

Implemented:

Shyam Textile,

Ahmedabad

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Pilot Benefits Status

Recycle/reuse of

cooling water and

condensate water as

boiler feed water

The total boiler feed water is being

now catered by recovered

condensate & cooling water

amounting to 50 KL per day.

Boiler feed water consumption

reduction: 100%

Recovery of energy in form of heat

from hot water: 15%

Reduction in boiler emissions

Reduction in waste water generation

(quality & quantity)

Implemented:

Rinkoo

Processors,

Ahmedabad

Komal Texfab,

Ahmedabad

Automated Chemical

Dosing Systems

Reduction in chemical usage: 10%

Reduction of rework by 3 %

Reduction in water consumption

Reduction in energy consumption

Reduction in waste water generation

(quality & quantity)

Pilot:

Komal Texfab,

Ahmedabad

Pilot Measures Implemented in Ahmedabad

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Pilot Benefits Status

Batch Washing in

Place of Continuous

Washing in Jet Dyeing

Machine

Economic savings with reduced

fresh water consumption by 360 KL

per year

Reduction in effluent generation

due to reuse of cooling water.

Reduces the load on ETP and

reduction of CETP charges in

future for the volume of waste

water reduced

Pilot:

Rinkoo

Processors,

Ahmedabad

Water Consumption

Optimisation at Jigger

Machines

Economic savings with reduced

fresh water consumption by 360 KL

per year

Reduction in effluent generation

due to reuse of cooling water.

Reduces the load on ETP and

reduction of CETP charges in

future for the volume of waste

water reduced

Pilot:

Mukesh Industry,

Ahmedabad

Pilot Measures Implemented in Ahmedabad

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Pilot Benefits Status

Low-Liquor-Ratio

Jet Dyeing

Machines

Reduced water consumption: 30%

Reduced electrical power consumption:

20%

Reduced fuel (coal) consumption: 30%

Reduced consumption of chemicals &

auxiliaries.

Reduction in waste water generation

(quality & quantity)

Pilot:

Komal Texfab,

Ahmedabad

Reuse of Treated

Water for Washing

at Printing Machines

Reduced fresh water consumption by 150

KL per day

Reduction of CETP charges in future for

the volume of waste water reduced

Pilot:

Rinkoo

Processors,

Ahmedabad

Komal Texfab,

Ahmedabad

Reuse of Alkaline

Stream from

Mercerising

Reduction of caustic consumption by

15000 kg per year.

Reduction of CETP charges in future for

the volume of waste water reduced

Pilot:

Rinkoo

Processors,

Ahmedabad

Pilot Measures Implemented in Ahmedabad

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Pilot Benefits Status

Installation of

Variable Frequency

Drive in Jet Dyeing

Machine

Reduction in electricity consumption

Better process control

Pilot:

Rinkoo

Processors,

Ahmedabad

Optimisation of

Heat Energy in

Jigger Machines

Reduction in coal consumption by 102 tons

per year.

Reduction in fresh water consumption of

30000 KL per year

Reduction of CETP charges in future for the

volume of waste water reduced

Reduced emissions from boiler

Pilot:

Mukesh

Industry,

Ahmedabad

Flash Steam

Recovery of Drying

Range to Preheat

Boiler Feed Water

Reduction in coal consumption by 510 tons

per year.

Reduction in fresh water consumption of

3375 KL per year due to recovery of flash

steam

Reduced emissions from boiler

Pilot:

Mukesh

Industry,

Ahmedabad

Pilot Measures Implemented in Ahmedabad

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Pilot Benefits Status

Boiler Efficiency

Optimisation

Reduction in coal consumption:

10-30%

Reduction in boiler emissions.

Pilot:

V R Polyfab,

Ahmedabad

Dryer Heat Loss

Reduction

Reduction in steam consumption:

5-10%

Reduction in boiler emissions.

Production area working

conditions will improve

Safety for workers will improve

Pilot:

Mukesh Industry,

Ahmedabad

Installation of Exhaust

Humidity Control

System in Stenters

Reduction in consumption of

electrical power: 5-10%

Reduction in consumption of fuel

(coal): 20%

Reduction in thermic fluid heater

emissions.

Reduction in process time.

Pilot:

Mukesh Industry,

Ahmedabad

(Under Implementation)

Pilot Measures Implemented in Ahmedabad

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Thank You

As a federal enterprise, GIZ supports the German Government in

achieving its objectives in the field of international cooperation for

sustainable development.

Published by

Deutsche Gesellschaft für

Internationale Zusammenarbeit (GIZ) GmbH

Registered offices, Bonn and Eschborn, Germany

Sustainable and Environment-friendly Industrial Production

1st Floor, B 5 / 1, Safdarjung Enclave

New Delhi 110029

T +91 11 49 49 53 53

F +49 11 49 49 53 51

E [email protected]

I www.giz.de, www.igep.in

Responsible

Mr. N. Raghu Babu

Author(s)

Mr. Nitesh Patel

In Cooperation with