approaches to improve air preheater thermal efficiency by louis bondurant, alstom

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  • 8/13/2019 Approaches to Improve Air PreHeater Thermal Efficiency by Louis Bondurant, Alstom

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    W

    PC

    A

    Worldwide Pollution

    Control Association

    WPCA-Entergy

    Increasing Energy

    Efficiency of Existing

    Units Seminar

    January 22, 2014

    Visit our website at www.wpca.info

    All presentations posted on this website are copyrighted by the Worldwide Pollution

    Control Association (WPCA). Any unauthorized downloading, attempts to modify or to

    incorporate into other presentations, link to other websites, or to obtain copies for any

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    prohibited, unless approved in writing by the WPCA or the original presenter. TheWPCA does not assume any liability for the accuracy or contents of any materials

    contained in this library which were presented and/or created by persons who were

    not employees of the WPCA.

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    Louis Bondurant

    January 22, 2014

    Approaches to ImproveAir Preheater

    Thermal Efficiency

    Alstom Air Preheater

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    ALSTOM 2013. All rights reserved. Information contained in this document is indicative only. No representation or warranty is given or should be relied onthat it is complete or correct or will apply to any particular project. This will depend on the technical and commercial circumstances. It is provided withoutliability and is subject to change without notice. Reproduction, use or disclosure to third parties, without express written authority, is strictly prohibited.

    Presentation title - 23/01/2014 P 2

    LGOT R&D Program(Low Gas Outlet Temperature)

    Objective of the LGOT Program

    Develop the design of the Ljungstrom air preheater for operation at gas outlet temperatures

    down to 220F (105C) on coal fired boiler applications.

    The Potential Benefits of LGOT

    Significant reduction in Dry Gas Loss a key metric in unit heat rate

    Reduced volumetric flow rates for downstream FGD, CO2 capture, etc.

    ESP can benefit from reductions in both volumetric flow and fly ash resistivity

    Potential Issues for LGOT Enhanced risk of air preheater acid dew point fouling problems

    Added potential for low temperature corrosion from halogen acids near the H2O dew point.

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    ALSTOM 2013. All rights reserved. Information contained in this document is indicative only. No representation or warranty is given or should be relied onthat it is complete or correct or will apply to any particular project. This will depend on the technical and commercial circumstances. It is provided withoutliability and is subject to change without notice. Reproduction, use or disclosure to third parties, without express written authority, is strictly prohibited.

    Presentation title - 23/01/2014 P 3

    Bench-Scale Test Apparatus

    Fouling Test Apparatus Soot Blowing Simulator

    Simulated gas flow included controlled amounts of

    SO3

    Water vapor

    Solid particulate

    Cleaning cycle

    Duration of tests mimicked typical sootblowing interval

    Translational movement in the path of the cleaning

    nozzle mimicked rotor rotation

    Tube removal required in order to clean

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    ALSTOM 2013. All rights reserved. Information contained in this document is indicative only. No representation or warranty is given or should be relied onthat it is complete or correct or will apply to any particular project. This will depend on the technical and commercial circumstances. It is provided withoutliability and is subject to change without notice. Reproduction, use or disclosure to third parties, without express written authority, is strictly prohibited.

    Presentation title - 23/01/2014 P 4

    Pilot Scale Test Apparatus

    AirSdeFan

    Tower1

    To atmosphere

    PreheatBurner Natural Gas

    GasSdeFan

    Catalyst SO2

    Part iculate FeederWater

    Flyash

    Soot blower

    Tower2

    Soot blower

    Broken = Gas side flow

    Solid = Air side flow

    To atmosphere

    HeatExchanger

    Baghouse

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    ALSTOM 2013. All rights reserved. Information contained in this document is indicative only. No representation or warranty is given or should be relied onthat it is complete or correct or will apply to any particular project. This will depend on the technical and commercial circumstances. It is provided withoutliability and is subject to change without notice. Reproduction, use or disclosure to third parties, without express written authority, is strictly prohibited.

    Presentation title - 23/01/2014 P 5

    Pilot Scale Test Apparatus

    Gas Inlet Ducting: SO3, H2O,Flyash Injection

    Preheat BurnerSystem

    Instrumentation Panel

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    ALSTOM 2013. All rights reserved. Information contained in this document is indicative only. No representation or warranty is given or should be relied onthat it is complete or correct or will apply to any particular project. This will depend on the technical and commercial circumstances. It is provided withoutliability and is subject to change without notice. Reproduction, use or disclosure to third parties, without express written authority, is strictly prohibited.

    Presentation title - 23/01/2014 P 6

    Simulated URS SBS InjectionTechnologyFull Mitigation (5ppmv SO3+ Na2SO4By-Product)

    Stable Pressure Drop Response for ~ 2 Months

    Tower 1 Gas Side Pressure Drops

    0.0

    0.5

    1.0

    1.5

    2.0

    2.5

    3.0

    3.5

    4.0

    4.5

    0 200 400 600 800 1000 1200 1400 1600 1800 2000

    Elapsed Operating Time (hrs)

    PressureDro

    p

    (inwg)

    2000

    2100

    2200

    2300

    2400

    2500

    2600

    2700

    2800

    2900

    FlueGasFlo

    w(

    lb/hr)

    Total Cold End Flue Gas Flow

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    ALSTOM 2013. All rights reserved. Information contained in this document is indicative only. No representation or warranty is given or should be relied onthat it is complete or correct or will apply to any particular project. This will depend on the technical and commercial circumstances. It is provided withoutliability and is subject to change without notice. Reproduction, use or disclosure to third parties, without express written authority, is strictly prohibited.

    Presentation title - 23/01/2014 P 7

    Simulated URS SBS InjectionTechnologyFull Mitigation (5ppmv SO3+ Na2SO4By-Product)

    No Significant Deposit Thickness Was Found

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    ALSTOM 2013. All rights reserved. Information contained in this document is indicative only. No representation or warranty is given or should be relied onthat it is complete or correct or will apply to any particular project. This will depend on the technical and commercial circumstances. It is provided withoutliability and is subject to change without notice. Reproduction, use or disclosure to third parties, without express written authority, is strictly prohibited.

    Presentation title - 23/01/2014 P 8

    Conclusions from Pilot Scale TestingSimulated URS SBS Injection Technology

    With SO3levels reduced to 5 ppmv

    Cold layer pressure drop did not increase

    No significant deposit thickness was found

    With SO3levels at 10 ppmv

    Rapid increases in cold layer pressure drop occurred

    Significant sodium bi-sulfate deposit was found

    Note: Sodium based SO3mitigation must reduce SO3concentrations to 5ppmv or less entering the air preheater

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    ALSTOM 2013. All rights reserved. Information contained in this document is indicative only. No representation or warranty is given or should be relied onthat it is complete or correct or will apply to any particular project. This will depend on the technical and commercial circumstances. It is provided withoutliability and is subject to change without notice. Reproduction, use or disclosure to third parties, without express written authority, is strictly prohibited.

    Presentation title - 23/01/2014 P 9

    RGOT Vs LGOT Operation(Reduced Gas Outlet Temperature)

    Simple modifications to an existing air heater typically cannot achieve a

    220F gas outlet temperature

    An increase in airflow can provide a significant reduction in gas temperature.

    Co-benefit, if this this incremental hot air can be used elsewhere in the plant.

    Reduced gas outlet temperature (> 220F) can be pursued in lieu of LGOT.

    Basic benefits retained, implementation cost lowered significantly.

    Reduced potential for corrosion, but need to stay above H2O dewpoint

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    ALSTOM 2013. All rights reserved. Information contained in this document is indicative only. No representation or warranty is given or should be relied onthat it is complete or correct or will apply to any particular project. This will depend on the technical and commercial circumstances. It is provided withoutliability and is subject to change without notice. Reproduction, use or disclosure to third parties, without express written authority, is strictly prohibited.

    Presentation title - 23/01/2014 P 10

    RGOT OperationMeans to Accomplish

    Fill empty voids in APH rotor with additionalbasket layers

    Utilize special basket designs to maximize

    useable space for heat transfer surface

    Consolidate shallow basket layers into

    single deeper layers

    Modify APH rotor to more efficiently support

    basket layers

    Switch to more efficient types of heat

    transfer surface

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    ALSTOM 2013. All rights reserved. Information contained in this document is indicative only. No representation or warranty is given or should be relied onthat it is complete or correct or will apply to any particular project. This will depend on the technical and commercial circumstances. It is provided withoutliability and is subject to change without notice. Reproduction, use or disclosure to third parties, without express written authority, is strictly prohibited.

    Presentation title - 23/01/2014 P 11

    RGOT OperationConsiderations

    Fuel compatibility

    Thermodynamic limitation

    Available space within the existing APH rotor

    Load bearing limits on rotor bearings, rotor drive and APH structure

    Ability of draft fans to accommodate expected pressure drop levels

    Ability of APH sealing system and structure to operate at higher

    pressure levels

    Ability to maintain temperature levels above H2O dew point at all loadand ambient conditions

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    ALSTOM 2013. All rights reserved. Information contained in this document is indicative only. No representation or warranty is given or should be relied onthat it is complete or correct or will apply to any particular project. This will depend on the technical and commercial circumstances. It is provided withoutliability and is subject to change without notice. Reproduction, use or disclosure to third parties, without express written authority, is strictly prohibited.

    Presentation title - 23/01/2014 P 12

    Benefits Derived from RGOT

    Reduced coal consumption (potentially as much as 3%)

    Significant reduction in activated carbon required for mercury capture

    Enhanced ESP performance (due to fly ash resistivity)

    Reduced O&M costs associated with steam coil air preheaters

    Reduced CO2 emissions resulting from improved boiler efficiency

    Co-benefit if additional hot air can be used elsewhere on site

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