automation in burnishing
TRANSCRIPT
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Proceedings of the National conference on Advances in Engineering, Technology and Applied Sciences SPANDAN-13.
AUTOMATION IN OUTER DIAMETER
BURNISHING MACHINE
Mangesh S. Raimal, Gopal P. Badarkhe, Ashay G. Kohad
B.E. 8th Sem.
Mechanical, Y.C.C.E., Nagpur
AbstractIn todays world of automation every industry wantsto make the machine tool or equipment automatic so as to
increase productivity; as automation reduces cycle time and
increases accuracy & efficiency. The company where we areapproaching to do automation has a burnishing machine where
round bars have been feed manually into the machine. Company
wants to make machine labour free by doing automation into it;
for doing so we virtually made mechanisms to feed bars
automatically and proposed these solutions to the company and
they have accepted it.
In first solution the mechanism has a conveyor belt with
grooves. Hopper is placed above the belt and one rod will occupy
space in groove and move forward to the burnishing chuck and it
will pushed inside with the help of plunger.
In second solution bars will slide and then it will be picked upby the clamps on the pulley then that clamp will come in front of
chuck & bar will be pushed inside with the help of plunger.
INTRODUCTION
Excel controlinkages pvt. Ltd. (situated at MIDC, Hingna,
Nagpur) is one of the leading manufacturer of control linkages
and automobile equipments. Different types of machines are
used in the company. One of them is mini centre less OD
burnishing machine which is used for super finishing
operation. Presently it is manually operated due to which
production rate is low. As company required more production
rate, we have given solution about automation in burnishing
machine.
Roller burnishing is a cold working process, which
produces a fine surface finish by the planetary rotation of
hardened rolls over turned parts. It improves surface structure
of turned part. Mini centre less OD burnishing machines are
suitable for small pins/shafts from 2 to 20 mm OD. In
company different jobs are burnished having diameters 4.7,
6.35, 7.8 and 9.5mm.
So we have virtually design portable, simple and flexible
bar feeding mechanisms and proposed these solutions to the
manager of company and they have accepted. This mechanism
consists of simple pulleys, clamps, belt, motor, plunger andsensors. This mechanism is simple in sense that it gets easily
detached from the actual machine, Also adjustment is
provided for varying length and diameters of bars.
Fig.1 Burnishing Machine
PROJECTOBJECTIVE
1. Automation in Mini Centre less OD BurnishingMachine to increase the production rate.
2. To provide a feeding mechanism of bars havingdifferent diameters and length.
3. To assist comfort for workers.
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METHODOLOGY
1. Project selection:-We have decided to work on the industrial
project as there is much scope to generate feasible
system and to assist our self to a level that it develops
our confidence and to generate some innovation.
2.
Problem identification:-We have searched for the problem faced by the
worker and different machines. After that we have
decided to automate the burnishing machine in sense
to design feeding mechanism of bars.
3. Study of machine:-We were visited the company weekly to study
the actual construction and working of machine and
taken all the dimensions and specifications to
generate the cad model.
4. Software used:-To generate cad model we have select CATIA &
PRO-E. We virtually design the CAD model and
proposed these models to the manager of companyand they have accepted these solutions.
FIRST SOLUTION
Jobs will be placed in hopper, from which they will
occupy place in grooves on belt. Then Belt will move ahead.
When sensor near pallet sense the job it will stop the motor as
the motor is stepper motor and at the same time actuate
plunger, which will push the job into the machine. Machine
automatically burnishes the job. When job returns back, again
sensor will sense the job and activate electromagnet which
will attract job and pull it out. At that point after some timelag belt will start moving. Again when sensor sense new job
same process will be repeated. At end burnish job will be
collected in pan. The adjustable plunger is provided for the
different length of bar & hopper is provided for different
diameters.
fig.2 View 1 Bar Feeding Mechanism
fig. 3 View 2 Bar Feeding Mechanism
SECOND SOLUTION
Set of Pins will be placed in hopper. Motor starts, then
one pin will be picking up by clamp. Then in next pulse motor
rotates and clamp will reach to the next position.(i.e. in front
of the pallet) Pin gets sensed by sensor. Considering some
time lag plunger will get activated and push the pin into the
burnishing machine pallet. Burnishing process will start.
Sensor will sense the returning pin and activate electromagnet
which will pull the rod from machine. Considering some time
lag, motor will start and clamp will rotate and release the pin
into the collecting pan. Again same process will be repeated.
Angle positions are
1. 0 to120Clamps are in close condition2. 120 to 360Clamps are in open condition
fig 4 View 1 Bar feeding mechanism
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Proceedings of the National conference on Advances in Engineering, Technology and Applied Sciences SPANDAN-13.
Fig. 5 view 2 bar feeding mechanism
SCOPE
1. The project on which we are working is feedingmechanism of steel bars of varying length and
diameters; as these bars are of varying length and
diameters the feeding mechanism has a adjustable
plunger for length and hopper for position change forvarying diameters.
2. The feeding mechanism provided is totally detachableso that we can use it in another machine of same
purpose also.3. This mechanism is also use to convey material of
round shape and in length.4. By providing magnetic attachment we can use this
mechanism for separation of different material which
has got mixed
Conclusions
1. Due to automation in Burnishing Machine, productionrate increases.
2. Due to automation in Burnishing Machine, machinecan be operated without involvement of labour.
3. Due to automation in Burnishing Machine, efficiencyof material handling increases.
4. Due to automation in Burnishing Machine, we canremove bar from machine at exact time due to which
processing errors are reduced. This means that if bar is
not removed on time it may get damaged.
5. Due to automation in Burnishing Machine, overalllabour cost required is reduced.
ACKNOWLEDGMENT
Apart from our efforts, success of any project depends
largely on the encouragement and guidelines of many others.
We take this opportunity to express our gratitude to the people
who have been instrumental in the successful completion of
the project.
It is with deep sense of respect that, we would like to
show our greatest appreciation to our guide Prof S.S.Akant for
his valuable guidance, constant motivation, encouragement
and other useful suggestions during the course of our project.
We express our deep gratitude to Mr.Avinash Lanjewar
(senior manager) and complete crew of EXCEL CONTROL
LINKAGES Pvt Ltd. For their time to time guidance,
cooperation, encouragement and feedback on this project
report.
The dossier of knowledge that we have gained from
them will surely be an asset for us in our professional career
ahead.
Last but not the least I would like to thank all those
people who were directly or indirectly involved with the
completion of the project.
REFERENCES
[1] www.excelcontrollinkage.com[2] www.wikipedia.com[3] www.mechindia.com[4] Automation, Production System, and Computer Integrated
Manufacturing by MIKELL P. GROOVER
[5]
Production Technology by R. K. Jain
http://www.excelcontrollinkage.com/http://www.excelcontrollinkage.com/http://www.wikipedia.com/http://www.wikipedia.com/http://www.mechindia.com/http://www.mechindia.com/http://www.mechindia.com/http://www.wikipedia.com/http://www.excelcontrollinkage.com/