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BA6 Cooling Towers Test Day Process Control Functionality and Performance Tests TCR – PCR Monitoring

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Page 1: BA6 Cooling Towers Test Day Process Control Functionality and Performance Tests TCR – PCR Monitoring

BA6 Cooling Towers Test Day

Process Control Functionality and Performance Tests

TCR – PCR Monitoring

Page 2: BA6 Cooling Towers Test Day Process Control Functionality and Performance Tests TCR – PCR Monitoring

Objectives

• Test the process functionality and performance• Better understand impact of the new cooling

system on SPS operation (ST-CV, TCR, PCR)• Validate the TCR monitoring in a real fault

situation• Validate the new joint TCR-PCR monitoring

GTPM(Gestion Technique Panne Majeure)

Page 3: BA6 Cooling Towers Test Day Process Control Functionality and Performance Tests TCR – PCR Monitoring

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Page 4: BA6 Cooling Towers Test Day Process Control Functionality and Performance Tests TCR – PCR Monitoring

SAFETY MODE TEST

• The main objective of the « safety mode » functionality is to keep the temperature of the primary cooling water (raw water) within the upper critical limit in order to preserve the SPS accelerator from being stopped by a increase of the temperature of the secondary circuit (demineralised circuit)

The safety mode is automatically triggered when under specific conditions the temperature of the primary water increases and reaches about 26.5

• Cooling tower considered out of order is replaced by the safety regulation circuit. The hot water is therefore rejected to the Nant d’Avril.

• Information is transmitted to the SIG control system which automatically supplies with cold water the SPS Primary circuit to balance the wasted missing water The cold water flow rate represents the exact quantity of the wasted hot water.

Page 5: BA6 Cooling Towers Test Day Process Control Functionality and Performance Tests TCR – PCR Monitoring

SAFETY MODE TEST

9: 30 am Cooling towers are placed in normal operating conditions

The SPS main magnets have been pulsed since 6: 00 am at 400GeV and all the power equipment has been switched on. The conditions corresponded to the normal SPS physics operation.

Fans & regulation system are working properly Parameters at this moment T ext = 10 º C

T retour = 30.5 º CT depart = 21 º CFlow rate = 564 l/s (through towers 2 and

3)

10:00 am Tdepart and flow rate increased

T retour = 31.8º CT depart = 23.3º Cflow rate = 638 l/s (through towers 2, 3 and 4)

Page 6: BA6 Cooling Towers Test Day Process Control Functionality and Performance Tests TCR – PCR Monitoring

SAFETY MODE TEST

9:30 am Fans are put out of order (simulation of regulation problem)

T depart increased 26.7- º CT retour 31 º CFlow rate 500 l/s

10:00 am Safety mode triggered(Wasted water flow rate regulation on )

Flow rate regulation system with SIG is working properly Parameters at this moment Safety flow rate 230 l/s

Wasted flow rate 227 l/sSIG cold waste flow rate 225 l/s

The BA4 regulation tank showed to perfectly absorb the flow rate disturbances. Regulation keeps the level between 2.3 and 2.7 m.

Page 7: BA6 Cooling Towers Test Day Process Control Functionality and Performance Tests TCR – PCR Monitoring

SAFETY MODE TEST Status after having been triggered

10:20 am Tdepart & towers input flow rate decreasing

T depart increased 25.5 º CT retour 31 º C

10:40 am StabilizationTdepart goes on decreasing slowly up to recovering the 21º Cof origin.

The safety mode can compensate a disturbance or saturation in the heating exchange in the cooling towers. The test is concluded to be positive

Page 8: BA6 Cooling Towers Test Day Process Control Functionality and Performance Tests TCR – PCR Monitoring

SAFETY MODE TEST Determination of the BAs critical point

10:40 am Safety mode is manually turned off Some parameters at this moment:

T depart increased 21.5 º CT retour 31.5 º C

10:50 am No fans; no safety mode. Tdepart starts to increase.T depart increased 26.7º C —> 28.4 º CT retour 32.8 º C Maximum reached

The BA3 has stopped by 11:09 (TCR confirmed during the afternoon debriefing meeting that it had been at 11:06) The test showed that the BA’s can work with a Tdepart up to around 28 º C

SL indicated: the stop has been due to a temperature interlock on the sextupolesin BA6 that were not correctly connected to the demineralised water circuits.

Consequently the BA3 could have been in operation some more time

Page 9: BA6 Cooling Towers Test Day Process Control Functionality and Performance Tests TCR – PCR Monitoring

BA4 Regulation tank

Upon a too high level at the BA4 regulation tank ( 4.3 m ) stopped the SIG station stopped progressively as it was expected

As a consequence of the stop of the SIG station, BA1 and BA3 stopped ( reason not determined during the tests ). In the afternoon debriefing meeting R. Mollay indicated that a too low primary water pressure during 30s causes the BAs to stop )

No alarm appeared in TCR concerning the stop of the cooling stations at BA1 and BA3. TCR operators detect the stop because the electrical alarms coming from the compensators.Alarms for the pressure of the primary circuit are being implemented for all the BA’s.

Remote reset and restart of BA1 and BA3 not possible, on-site intervention necessary – modification in the PLC demi water under investigation.

TCR measurement of the regulation tank level identified as wrong – is being corrected.

Page 10: BA6 Cooling Towers Test Day Process Control Functionality and Performance Tests TCR – PCR Monitoring

TCR-PCR Monitoring

• Globally the TCR monitoring worked as foreseen

• Some minor errors have been identified and are corrected

• All information for TCR operation available

• The GTPM monitoring worked correctly– Easy detection of machine state

– Easy detection of the state of the technical infrastructure

– Easy communication between TCR and PCR

• TCR process and monitoring documentation will be completed with the experience gained during the tests

Page 11: BA6 Cooling Towers Test Day Process Control Functionality and Performance Tests TCR – PCR Monitoring

Conclusion

• Satisfying functioning of the cooling

• The SPS can continue working in physics mode for approximately 3 hours with the cooling towers in the safety mode – total transparency

• Good experience as to what happens in case of a fault

• Better understanding of the cooling monitoring