final aircraft accident report presentation
TRANSCRIPT
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Final Aircraft Accident Report
Regarding The Airbus 310-324
Accident on 10/06/2008Registration ST-ATN
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Presented by
The Investigation Board which was formed by
The Minister,
and being nominated by the Deputy
DGCA at the time of the accident
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The Board Comprises :
Eng. Sirelkhatim Kambal Head of BoardMr. Kamil Ahmed Member
Mr. Abdelkariem A/Lateef Member
Mr. Mohmed Elhassan MemberCap. Osman Alsaied Member
Cap. Abdelfatah Satti Member
Eng. Abdelgadir Sirelkhatim MemberMr. Abdelmuniem Tyfor Member
mr. Abdelsamie Adam Member
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BEA (Accident Investigation Bureau) of France
appointed
Mr. Francois Hochart Accredited representative
Assisted by
Mr. Vincent Ecalle
Airbus Industry investigators teamMr. Albert Urdiroz Flt. Safety director
Mr. Xavier Barriola Flt. Safety
Mr. Jean Philippe Propulsion systemMr. Jean Paul Structure
Mr. Christophe Duphil Systems
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International Statistic about the Airbus 310 SerialNumber 548 (current ST-ATN)
The First Flight was On 23/08/1990
Delivered to Singapore On 22/10/1990
Registered as 9V-STU
Leased to Air India by Owner (Osprey AircraftLeasing Limited of Cayman Islands)Registered as VT-EVF and
issued Indian Airworthiness Certification On
7/2/2001Delivered to Sudan On 14/09/2007
Registered as ST- ATN
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Ref Airliners.net
The accident was
9th
loss of Airbus 310 at that date
7th worst accident involving A310 at that time
6th worst accident in Sudan
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From general history
The A310 serial number 548 accomplished the
C1 + C2 in the period
06 March 2007 26 August 2007 at
Jordan Aircraft Maintenance Limited
Which covered
Routine, zonal, structural task, ADs, SBsprovided by Air India i.a.w the Approved Main.
Program.
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During the check 41 Discrepancies were found andbeing repaired. This includes
Fuel leakage at
(L/H wing)
Aft pylon fitting, lower surface, wing inner tank wing
jacking fitting through access panel 575DB, etc(R/H wing)
Lower surface, aft pylon fitting, drain hole at slat 2screw jack alignment, at lower I/B area I/B of pylon
In addition to corrosion areas and spots andreinforcement panels cracks
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Objective of the Investigation
In accordance to Annex 13 Para
The sole objective of the investigation is
to draw lessons from the occurrences that mayhelp to prevent future accidents and incidents
and
NOT. NOTTo apportion blame or to assess individual or
collective responsibility
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Number of witnesses being interviewed by theInvestigation Board were as follows :-
Sudan Airways personnelThe Flying Captain
The First Officer
7 Cabin Crew membersThe Flying Security Officer
Others
3 Police officers different ranks9 Citizens ( passengers)
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Brief description of the accident flight
On 10th of June 2008 A310 serial number 548
Arrived Khartoum Airport from Cairo With a
deactivated No. 1 engine Thrust reverser.
As it was previously scheduled for a flight to
Oman
The designated Captain for that flight accepted
to fly the aircraft as being labelled according the
MEL requirement.
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Flight to Amman via Damascus was uneventful.
On the return flight there were 203 passengersand eleven crew members on board.
On Approaching Khartoum that day in theafternoon and due to bad weather conditions
The Captain of the flight decided to divert to PortSudan and landed safely.
20 tons of fuel topped up at Port Sudan
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The captain said he was on contact with Khartoum
enquiring about the weather.
After staying at Port Sudan for 1:15 hrs he was
informed that the weather is getting better.
He decided to return to KhartoumHe initiated a night approach for R/W 36 after being
cleared to land
The Tower provided the flight with Windinformation as
{ 320/7 Kt} and R/W condition {Wet}
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At that moment the actual METAR was
10/1830 150/10 Kt 9/9 few CB 050 to E SCT 056SCT 056 Q 1010
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The Accident
Most important remarks obtained fromwitnesses interview were as follows :-
The Flying pilot stated
The weather was somehow bad and
the hold took a long time before being clearedto land and
he was always asking the First officer to monitor
himThe touchdown was very smooth and it waswithin the required distance
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He did not select autobrake for passenger comfort onlanding
Autobrake was not a must as it is a recommendation atthat time
After selected both engines reverse the aircraft slippedrightward
Due to that he deselect the reverse and managed toreturn the aircraft to R/W centreline by using differentialbrakes
Using brakes the deceleration was abnormal
Called the F/O to assist on brakes
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Approaching the end of the R/W he selected
reverse and aircraft did not decelerate
The aircraft overrun the R/W and burst on fire
Right hand slides could not be deployed
Passengers and crew vacated from the left front
slide
Two of the occupant stated that they saw fire on
the right wing during aircraft rolling on R/W
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FDR Information
The flying pilot was the captain
The aircraft was fully and properly configured forlanding
The AP was disconnected at 800 ft with Athrengaged till landing
Both thrust levers set to idle for touchdown
Touchdown at 132 kt IAS, 155Kt ground speedTouchdown was smooth at about 800 meters afterR/W threshold
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FDR event (UTC time )16 h 12 Takeoff
16 h 30 Level off at FL310
16 h 47 Top of descent
17 h 02 min 15 s Level off at 7000 ft
17 h 06 min 52 s Level off at 5000 ft
17 h 09 min 43 s Spoiler 5 FAULT/OFFparameter turns to
FAULT
17 h 13 min 48 s Master warning Capt (2 s)
VFE exceedance due to slatsDeployment
CAS 250 kt, VFE 245 kt
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17 h 14 min 58 s Level off at 4000 ft CAS 202 kt
17 h 17 min 18 s Level off at 3000 ft CAS 206 kt
17 h 22 min 57 s Top of final descent Zp 2800 ft
CAS 153 kt, GS 152 kt
A/THR engaged in SPEED mode
A/P 1 engaged in CMD
FLAPS 41, SLATS 25
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17 h 23 min 45 s Spoiler 5 FAULT/OFF parameter
turns to NO FAULT
17 h 23 min 52 s A/P disengaged CAS 142 kt,
GS 148 kt
17 h 25 min 06 s Thrust levers pulled to idleposition
Both EPR decrease to around 1
CAS 139 kt, GS 159 kt
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17 h 25 min 10 s Touchdown (LH then RH main
landing gears compressed)
A/THR disengagedAll spoilers deploy except LH and
RH number 5 spoilers
CAS 132 kt, GS 154 kt
17 h 25 min 12 s Thrust levers pulled to full reverseposition
Engine 2 thrust reversers deploy
and EPR of engine 2 start toincrease
CAS 132 kt, GS 150 kt
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17 h 25 min 13 s Spoiler 5 FAULT/OFF parameter
turns to FAULT
CAS 131 kt, GS 148 kt17 h 25 min 15 s Nose gear compressed
CAS 126 kt, GS 142 kt
17 h 25 min 20 s Max EPR of engine 2
reached at 1.2
Thrust levers pushed to idle
position
EPR of engine 2 start todecrease
CAS 103 kt, GS 128 kt
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17 h 25 min 28 s GPWS Terrain warning (2 s)
CAS 95 kt, GS 111 kt
17 h 25 min 30 s GPWS Whoop whoop pull
up warning (22 s)
CAS 90 kt, GS 106 kt17 h 25 min 38 s Thrust levers pulled to full
reverse position
CAS 79 kt, GS 93 kt
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17 h 25 min 46 s Runway excursion
CAS 54 kt, GS 76 kt17 h 25 min 54 s Spoilers retract CAS NCD
(
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CVR ReadoutThe readout was done at the BEA laboratory
The recording contains the following tracks:
3 tracks corresponding to the last 30 minutes of
recording containing VHF and crew communications(Captain, First Officer, CAM)
1 track corresponding to the 2 hours of recording
containing the Public Address signal
1 track corresponding to the 2 hours of recordingcontaining the signal of the first three channels mixed
together
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Note: this track allocation is not standard sincethe signal from the cockpit area microphoneshould always be recorded separately andduring two hours on this type of CVR.
This unusual track allocation could be relatedto the wiring of the CVR.
Samplitude audio editing software was used toperform the read out of the audio files.
It was confirmed that the event was recorded.The overall quality of the recording isacceptable
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Reading indicated that
* The captain got clearance to perform approach
R/W 36
* Aircraft configured for landing, checks completed
* Captain got clearance for landing
* Controller informed the flight wind 320/07kt and
R/W condition (rain, wet)
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* Co-pilot suggested the use of Auto-brake and
captain decided not to use it* Co-pilot announced centre line
* Co-pilot announced centre line left
* A single chime was recorded about 20 secondsafter touchdown
* GPWS warnings were triggered several times
prior to overrun TerrainPull up
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As the readout of FDR could not provide accurate
information about the low deceleration, the Board,
Airbus and BEA suggested to again to review
aircraft Maintenance documentation
To examine wreckage parts by appropriate
laboratories in France under supervision of the
board through BEA
Such parts are as
Parking brakes, the tyres, the brakes, remaining
computers, the anti-skid switch
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Unfortunately no remaining computers
were found
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Review of log books show
1- No braking issue was highlighted2- No report about the GPWS was highlighted
3- Engine No. 1 thrust reverser was found stuck
in open position after landing on 22/04/2008and was deactivated up to 10/05/2008 when
the RH master actuator was replaced
4- No tyre inflation information is recorded as theaircraft was not equipped with TPIS
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The aircraft was fitted an EGPWS P/N 965-0976-
003-206-206
The aural warning Terrain, Pull up were trigged
19 seconds after touchdown
Such warnings are Mode 2 which based on radio
altitude and closure rate associated
Below 30 ft no warnings should be triggered
The A310 MSN 548 was not covered by Airbus
Service BulletinA310-34-2163
That is its installation was not defined by Airbus
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Unfortunately no computers were found
The brake units were tested locally at Sudan
Airways facility attended by representatives
from :-
Sudan Investigation Board
The BEA
Sudan Airways
Airbus
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The aim of the test was to determine the status
of both normal and alternate braking systems
Visual inspection revelled that
* All brakes were in good shape within wear limit
* No hydraulic leak was evidenced
* There several impacts due to accident
* Pistons were covered with dirt from accident site
* Some pistons covered with melted aluminium
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On hydraulic Test
* All pistons were active under low pressurewith no leak
* At low pressure ( 200 psi)
pistons were observed moving,discs were not free to rotate,
pistons applied pressure on thrust plate
* At high pressure (2000 psi) no leak was seen* According to the test no failure was evident dueto brakes
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Also
According to FDR analysis
The left main gear braking system was working
about 10 seconds after touchdown when the
captain succeeded to bring the aircraft back on the
centre line by differential brakes as he stated.No failure of brakes was recorded on the FDR
and
According to the rubber marks at the end of theR/W due to wheel lock , braking system failure
appears to be unlikely
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Tyres Examination
The tyres were shipped to France and being examined in
a French Laboratory the
Centre dEssais Aeronautique de Toulouse
(CEAT)
Conclusion of examination 8 tyres show flat spot on the tread
The flat spot damage were due to locking of the wheels
7 tyres were burst except tyre No. 1 (LH/MLG)
No evidence of hydroplaning Wheels rim had no wear marks indicating the rim did
not touch R/W surface, no scraping
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Antiskid
The BRK A/SKID lever was found hanging from
the 401VU panel, in the position indicated in the
photo.
This position was consistent with the switch
being set to ALTN/OFF
Alternate braking/Antiskid off
The 3 push buttons of AUTO BRK selection were
severely damaged by fire.
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