heritage foods limited - knowledge...

8
78 First Prize Dairy HERITAGE FOODS LIMITED Hyderabad (Telangana) Unit Profile Hertage Foods Limited, Uppal Dairy Plant Commissioned in the year 2006 with a rated capacity of 0.6 LLPD and was subsequently expanded to 0.74 LLPD in 2007, 1.1 LLPD in 2010 and 1.5 LLPD in 2012. Presently, Heritage Milk and Milk Products have market presence in Andhra Pradesh, Telangana, Karnataka, Tamilnadu, Kerala, Maharashtra, Odisha and Delhi. Energy Consumption Energy is the biggest component of the operational costs in the Dairy Industry. The Unit has taken this as a challenge to reduce its energy cost. The energy conservation drive got a good momentum when the Unit declared Energy Management Policy in 2012. Description Unit 2012-13 2013-14 % Reduction Specific Electrical Energy kWh/Ton 61.99 48.25 22.17 Specific Thermal energy million kCal/Ton 0.05921 0.05289 10.67

Upload: others

Post on 21-Oct-2020

2 views

Category:

Documents


0 download

TRANSCRIPT

  • 78

    First Prize

    Dairy

    HERITAGE FOODS LIMITED

    Hyderabad (Telangana)

    Unit Profile

    Hertage Foods Limited, Uppal Dairy Plant Commissioned in the year 2006 with a

    rated capacity of 0.6 LLPD and was subsequently expanded to 0.74 LLPD in 2007,

    1.1 LLPD in 2010 and 1.5 LLPD in 2012.

    Presently, Heritage Milk and Milk Products have market presence in Andhra Pradesh,

    Telangana, Karnataka, Tamilnadu, Kerala, Maharashtra, Odisha and Delhi.

    Energy Consumption

    Energy is the biggest component of the operational costs in the Dairy Industry. The

    Unit has taken this as a challenge to reduce its energy cost. The energy

    conservation drive got a good momentum when the Unit declared Energy

    Management Policy in 2012.

    Description Unit 2012-13 2013-14 % Reduction

    Specific Electrical Energy kWh/Ton 61.99 48.25 22.17

    Specific Thermal energy million kCal/Ton 0.05921 0.05289 10.67

  • 79

    Energy Conservation Measures Taken

    1. Installation of Ammonia Chiller

    Ammonia chiller installed in return chilled water

    line from processing to reduce the temperature

    by 3 °C which reduces the load on IBT (PHE

    system of cooling is more effective as the

    ammonia and return chilled water passes

    through plate by plate which increases the

    contact surface tremendously and leads to

    instant exchange of heat).

    Electricity saving : 2.409 Lakh kWh/yr

    Cost saving : Rs 19.36 Lakh/yr

    2. Centrifuge for installation for Oil fired Boiler

    Centrifuge has been installed for Pre-Filtration of

    furnace oil to Boiler which ultimately reduced

    nozzle choking and efficiency of Burner have

    been improved.

    The steam generation per liter of Furnace Oil

    have been improved which saved an annual of

    7% of Furnace Oil.

    Furnace Oil saving : 16.74 kL/yr

    Cost saving : Rs. 8.41 Lakh/yr

  • 80

    3. Installation of Pre-Heater for pre-heating the Curd Milk

    Pre heating of curd milk with OHT soft water has

    double impact both on FO & Electrical energy.

    Due to preheating the inlet temp. of curd milk to

    the curd past. Increased to 17 °C against 5 °C

    which saves 8.46 kL of Furnace oil.

    On the other hand the OHT soft water cooled to

    15 °C which used in RSM (Reconstitution

    skimmed milk) preparation and in cream past for cooling cream after regeneration.

    Electricity savings : 0.401 Lakh kWh/yr

    FO saving : 8.46 kL/yr

    Cost saving : Rs. 7.48 Lakh/yr

    4. Arrangement of Cyclic timers for Milk silo agitator motors

    15 nos. of Cyclic timers were arranged for

    packing milk Silo’s for operating with cyclic

    intervals of 10 minutes span with which we can

    save electricity of 161 Units per day.

    Agitator running hrs per day has been reduced.

    Maintenance cost also reduced accordingly.

    Electricity savings : 0.57 Lakh kWh/yr

    Cost saving : Rs. 4.65 Lakh/yr

    5. Downsizing of ETP Air blower pulleys

    Due to water conservation measures and GMP

    practices implemented, the water quantity and

    COD reduced by 25% & 38% respectively. As

    dissolve oxygen in aeration tank is found more,

    the blower pully has down sized, which results

    in reduction of RPM of Blower.

    With the above modifications the electricty

    consumption was reduced by 21%.

    Electricity savings : Rs. 0.401 Lakh kWh/yr

    Cost saving : Rs 3.22 Lakh/yr

  • 81

    6. Condensate recovery from CIP Tanks

    In CIP section the direct steam injection to

    generate hot water is replaced with SS pumpkin

    type coils.

    Due to this the heating time reduced to half and

    the collected condensate is used as a boiler feed

    water.

    Furnace oil savings : 8.10 kL/yr

    Cost saving : Rs 4.07 Lakh/yr

    ENERGY POLICY

    The Unit is committed in Energy Management Performance on a continual basis

    through

    • Continuous up gradation of technology, systems and service to optimize the

    energy cost.

    • Monitor and control the Energy consumption effectively.

    • Providing Resources to achieve measurable objectives whenever necessary.

    • Educate and motivate all the people concerned through effective

    communication and recognition

    • From time to time identify the energy saving potential for reduction of energy

    consumption.

    • Conducting energy conservational studies & energy audits through internal &

    external professional.

    • To Establish bench mark Energy standards in dairy industry.

  • 82

    Second Prize

    Dairy

    SURAT DISTRICT CO-OPERATIVE MILK PRODUCERS

    UNION LIMITED, SUMUL DAIRY

    Surat (Gujarat)

    Unit Profile

    Surat District has been a Pioneer in India in channeling trade in Cotton and

    Milk through co-operatives. Before SUMUL stepped in, traditional Private Milk

    Traders were dominant in the area. Dairying on the other hand, was never

    popular with tribal (a major rural population in the district) as practically no

    infrastructure existed for milk marketing in their talukas, inaccessibility to their

    villages as well as taboos regarding keeping of buffaloes prevented the entire

    population of tribal from considering dairying as a source of income. To salvage the

    poor producers from the clutches of these Private Traders, Organization and

    integration of procurement, processing and marketing of milk and milk products by

    the producers themselves on a sound co-operative line was essential; this would

    also ensure elimination of middlemen, equitable distribution of benefits to Rural Milk

    Producers and indirectly to urban milk consumers as well. Being a producers owned

    organization, it eliminated the middlemen and minimized the overhead costs giving

    the maximum overall net-returns to its producer members from their milk

    production enterprises.

  • 83

    Energy Consumption

    There is a steady decline of specific energy conservation due to implementation of

    various energy conservation measures in last 2 years. The details are as given

    below:

    DESCRIPTION UNIT 2012-13 2013-14

    Annual Milk & Milk Production MT 470407 492490

    Total Electricity Consumption / Annum Lakh kWh 110.142 111.950

    Specific Energy Consumption kWh / MT 23.41 22.73

    Total Thermal Energy Consumption / Annum million kCal 21995.57 21106.56

    Specific Energy Consumption – Thermal million kCal / MT 0.0467 0.0428

    Summary of Annual Saving in Energy Conservation 2013-14

    Section Investment (Lakh Rs)

    Annual Saving (Lakh Rs)

    Electrical 106.57 89.40

    Thermal 45.88 177.21

    TOTAL 152.45 266.61

    Energy Conservation Measures Taken

    Electrical Points

    1. Installation of Soft Starter in place of Conventional starters up to 10 HP Motors.

    2. Installation of Low Speed 2 HP Agitator in place of 7.5 HP Agitator for Milk Silos

    – 4 Nos.

    3. Installation of Ammonia based milk cold storage in place of Frion Based at Main

    gate area.

    4. Installation of VFD for Milk pouch filling Direct from Milk Silo in place of VMST –

    2 Nos.

    5. To Reduce the Chilled water supply pressure from 3.5 Bar to 3.2 Bar for

    supplying the Chilled water in plant area.

    6. Energy Saving for Crate Washing & Crate conveyor by installation of High

    Speed Milk Conventional Machine – 1 Line.

    7. Energy Saving for Pouch Machines by Installation of High Speed (Speed: 9600

    Pouches / Hr.) Milk Pouch Packing Machine in place of Conventional Machine

    (Speed: 5400 Pouches / Hr.) – 5 Nos.

    8. Installation of 30 HP VFD in place of Star Delta Starter for Blower of Aeration

    Tank at ETP.

    9. Installation of Energy Efficient Grundfoss make 20 HP Pump in place of 30 HP

    Pump at Boiler Feed Water.

    10. Installation of VFD on Air Blower motor of Burner at Boiler.

    11. Installation of LED Lowbay Lighting Fixtures in place of 250 Watt Conventional

    fixtures for plant lighting – 35 Nos.

  • 84

    12. Installation of VFD in place of Star Delta Starter on 40 HP Motor for Alfa Laval

    Butter Churn Machine.

    13. Installation of Energy Efficient Grundfoss make 7.5 HP Pump in place of 12.5

    HP for Under Ground Tank Return Pump.

    14. Installation of VFD in place of DOL starter for Booster Pump of Milk Pasteurizer

    – 2 Nos.

    15. Installation of Energy Efficient Grundfoss make 3 HP Pump in place of 5 HP for

    Chilled Water Circulation in Pouch Machines.

    16. Installation of 45 Watt LED Street light fixtures in place of 150 Watt for Campus

    lighting – 30 Nos.

    17. Reduce the Running hour for Chilling the Milk by Installation of energy Efficient

    Chiller for GOA plant.

    18. Installation of 33 Watt LED light Fixtures in place of 72 Watt for Office lighting

    – 30 Nos.

    Thermal Points

    1. Reducing the Set-point of Germfree Chemical from 59 Deg C to 45 Deg C for

    Process CIP System.

    2. Installation of Packaged Plant Room System (PPRS) to supply hot water in

    place of Direct heating for Dahi Section.

    3. Installation of Packaged Plant Room System (PPRS) to supply hot water in

    place of Direct heating for UHT Section.

    4. Installation of VFD for Milk Pouch filling Direct from Milk silo in place of VMST –

    2 Nos.

    5. Energy Saving for Crate Washing & Crate Conveyor by installation of High

    Speed Milk Pouch packing machine in place of Conventional Machines – 1 Line.

    6. Prevention of thermal losses by adopting LRB insulation in place of Glass wool

    for 1.5”, 2”, 2.5” & 3” hot water supply lines.

    7. Installation of Economizer in Boiler for Recovery of heat & pre-heating of Feed

    water.

    8. Recovery of Flash Steam of 10 TPH Boiler.

  • 85

    ENERGY POLICY