ice flushing from st. lawrence seaway locks · the st. lawrence seaway development corporation...

48
/: /I ;;+ r: 'l , I r I ,.. ' 0 REFERENCE 10 I 101 1 00 DO 101 TECHNICAL REPORT H-76-9 ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS Model Investigation by Noel R. Oswalt Laboratory U.S. Army Engineer Waterways Experiment Station P. 0. Box 631, Vicksburg, Miss. 39180 July 1976 Final Report Approved For Public Release; Distribution Unlimited Prepared for St. Lawrence Seaway Development Corporation Massena, New York 13662 tiBRARY BRANCH TECHNICAL INFORMATION CENTEfi US ARMY ENGINEER WATERWAYS EXPERIMEN STA ,,, 1 VICKSBURG. MISSISSIPPI

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Page 1: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

/: /I

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REFERENCE 10 I

llvU.-~ 101 ~ ~

100 DO 101

TECHNICAL REPORT H-76-9

ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS

~ydraulic Model Investigation

by

Noel R. Oswalt

~ydraulics Laboratory U.S. Army Engineer Waterways Experiment Station

P. 0. Box 631, Vicksburg, Miss. 39180

July 1976

Final Report

Approved For Public Release; Distribution Unlimited

Prepared for St. Lawrence Seaway Development Corporation Massena, New York 13662

tiBRARY BRANCH TECHNICAL INFORMATION CENTEfi

US ARMY ENGINEER WATERWAYS EXPERIMEN STA ,,, 1

VICKSBURG. MISSISSIPPI

Page 2: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

Unclassified SECURITY CLASSIFICATION OF T HIS PAGE (Whan Date Entered)

REPORT DOCUMENTATION PAGE READ INSTRUCTIONS BEFORE COMPLETING FORM

1. REPORT NUMBER 2. GOVT ACCESSION NO . 3. RECIPIENT'S CATALOG NUMBER

Technical Report H- 76- 9

4 . TITLE ( end Subtitle) s. TYPE OF REPORT & PERIOD COVERED

ICE FLUSHING FROM ST . LAWRENCE SEAWAY LOCKS ; Final report Hydraulic Model Investigation

6 . PERFORMING ORG. REPORT NUMBER

7. AUTHOR(e) 8. CONTRACT OR GRANT NUMBER(e)

Noel R. Oswalt

9. PERFORMING ORGANIZATION NAME AND ADDRESS 10. PROGRAM ELEMENT. PROJECT, TASK

u. s . Army Engineer Waterways Experiment Station AREA & WORK UNIT NUMBERS

Hydraulics Laboratory P. o. Box 631 , Vicksburg, Miss . 39180 .

11. CONTROLLING OFFICE NAME AND ADDRESS 12. REPORT DATE

St . Lawrence Seaway Development Corporation July 1976

Massena, New York 13662 13. NUMBER O F PAGES

45 14. MONITORING AGENCY NAME & ADDRESS(lf dJlferent from Controlling Olllce) 1 s. SECURITY CLASS. (of thle report)

Unclassified 1 Sa. DECL ASS I FICA TION/ DOWNGRADING

SCHEDULE

16. DISTRIBUTION STATEMENT (of thle Report)

Approved for public release; distribution unlimited .

17. DISTRIBUTION STATEMENT (ol the abstract entered I n Block 20, II different from Report)

18. SUPPLEMENTARY NOTES

19. KEY WORDS (Continue on reverse side II necesaary end Identify by block number)

Floating ice St . Lawrence Seaway Flushing Hydraulic models Ice on rivers , lakes, etc . Locks (waterways)

20. ABS~AC:T (C4Dtiaue ~~a~..,._,._ .Ida If nece-aq aod. Identity by block number)

Corporation secured the services of The St. Lawrence Seaway Development the U. s . Army Engineer Waterways Experiment Station to determine, with the aid

effective and economical method of ridding a the most of physical model tests , lock chamber of floating ice . Tests were conducted in an existing 1:25- scale lock model modified to simulate the pertinent features of the St . Lawrence Sea-

way Lock chambers . A manifold at the upstream end of the chamber proved best

for flushing ice from the chamber . Flow through the manifold was pumped (Continued)

DD FOR .. \JAN 73 1473 EOfTION OF J NOV 65 tS OBSOLETE Unclassified

SECURlTY CLASSIFICATION OF THIS PAGE ( Wh-en D eta Entered)

Page 3: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

Unclassified SECURITY CLASSIFICATION OF THIS PAGE(When Data Entered)

20 . ABSTRACT (Continued).

from various locations in the chamber or piped through the upstream miter gate sill; both of these methods were designed to create a sufficient slope of the water surface in the chamber to flush the ice. These model tests provided the means to determine the size and configuration of the manifold and the amount of flow required for total flushing .

Initially, the concept of pumping water to an upstream manifold from the lower end of the chamber was tested with limited success. Total flushing of the chamber was not accomplished with the pumped high-velocity manifold submerged, and considerable spray from the high- velocity jets would generate additional ice in actual prototype conditions with the jets at the water sur­face . Therefore, a high discharge with a low head to reduce velocities and increase the water-surface slope was preferred for greater flushing efficiency.

Heads of 38. 5 to 42.5 ft at Dwight D. Eisenhower Lock (Robinson Bay) and 46 ft at Bertrand H. Snell Lock (Grass River) are available for gravity flow water- supply systems to the manifold located beneath the upstream ship bumper. These heads proved sufficient to flush 10- by 10- ft blocks of ice 1.5 and 3 . 0 ft thick from the entire 860- ft- long by 80- ft-wide chamber with the proper size and placement of the manifold .

Optimum flushing of the surface ice was accomplished with four 4-ft - diam pipes spaced 16 ft apart between the lock walls with their center line level with the lower pool . A total discharge of 2000 cfs was required for optimum flushing. Special consideration was given during these development tests to accommodate a 2- to 3-ft variation in water-surface elevation of the lower pool ana to minimize spray which would generate additional ice. The average total flushing time for 120 blocks of 10- by 10- by 3- ft ice was 15 min.

Unclassified SECURITY CLASSIFICATION OF THIS PAGE(When Data Entered)

Page 4: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

PREFACE

A hydraulic model investigation to determine effective ways and

means of flushing ice from the St. Lawrence Seaway Locks was authorized

by the Office, Chief of Engineers, in the first indorsement dated

25 July 1974 to a letter dated 16 July 1974 from the Director of the

U. S. Army Engineer Waterways Experiment Station (WES), Vicksburg,

Mississippi. The St. Lawrence Seaway Development Corporation considered

it highly desirable that the tests be conducted at WES where research

concerning application of multipart diffusers had been conducted for

desalinization plants and to induce circulation in stagnant embayments.

It was considered that the suggested application and development of a

multipart manifold to induce sufficient circulation downstream from the

upper miter gate would be of use in removing ice from similar Corps locks

with side port or bottom longitudinal filling and emptying systems. The

desired tests were technically feasible and were performed with existing

facilities and available personnel without interfering with work in prog­

ress at WES. The study was accomplished in the Hydraulics Laboratory

of the WES during the period 6 September 1974 to 19 February 1975.

The investigation was conducted under the general supervision of

Messrs. H. B. Simmons, Chief of the Hydraulics Laboratory; John L. Grace,

Chief of the Structures Division; and G. A. Pickering, Chief of the

Locks and Conduits Branch. The engineer in immediate charge of the

model was Mr. N. R. Oswalt, assisted by Messrs. H. H. Allen and C. L.

Dent. This report was prepared by Mr. Oswalt.

During the course of the investigation, Messrs. John B. Adams III,

William S. Spriggs, and Patrick M. Gillon of the st,. Lawrence Seaway

Development Corporation; Messrs. Walter E. Webb and Martin Liou of the

St. Lawrence Seaway Authority, Canada; and Dr. George D. Ashton of the

U. S. Army Cold Regions Research and Engineering Laboratory visited

WES to observe model operation and discuss test results.

Directors of WES during the conduct of the tests and the prepa­

ration and publication of this report were COL G. H. Hilt, CE, and

COL John L. Cannon, CE. Technical Director was Mr. F. R. Brown.

l

Page 5: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

CONTENTS

PREFACE . . . . . . . . . • • • • • • • • • • • • • • • • • • • •

CONVERSION FACTORS , U. S . CUSTOMARY TO METRIC (SI) UNITS OF MEASUREMENT . . . . . . . . • . . . . • • • • • • • •

PART I : INTRODUCTION . . . • • • • • • • • • • • • • • • • • • •

The Prototype . . . . . . . . . . . . . . . . . . . . . . . Description of the Prototype Problem . . . . . . . . . . . Purpose of Model Study . . . . . . . . . . . . . . . . . .

PART II : THE MODEL . . . . . . . . . . . . . • • • • •

• • • • • Description of Model and Appurtenances Scale Relat i ons . . . . . . . . . . . • • • • • •

• • • • •

• • • • •

• • • • •

PART I II : TESTS AND RESULTS • • • • • • • • • • • • • • • • • •

Page

1

3

4

4 4 6

1

1 8

9

Test Procedure . . . . . . . . . . . . . . . . . . . . . . 9 Low Discharge- High Head Manifold . . . . . . . . . . . . . 9 Hi gh Dischar ge- Low Head Manifold . . . . . . . . . . . . . 11 Special Considerations for Prototype Installation

and Oper ation . . . . . . . . . . . . . . . . . . . . . . 15 Prototype Sy stem Designed for Eisenhower Lock . . . . . . . 16

PART IV : DISCUSSION OF RESULTS

PHOTOS 1- 10

PLATES 1- 9

• •

2

• • • • • • • • • • • • • • • 17

Page 6: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

CONVERSION FACTORS, U. S. CUSTOMARY TO METRIC (SI) UNITS OF MEASUREMENT

U. S. customary units of measurement used in this report can be con­

verted to metric (SI) units as follows:

Multiply

feet ' feet per second

cubic feet per second

degrees (angular)

By

0.3048

0. 3048

0. 02831685

0 . 01745329

3

To Obtain

metres

metres per second

cubic metres per second

radians

Page 7: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

ICE FLUSHING FROM SAINT LAWRENCE SEAWAY LOCKS

Hydraulic Model Investigation

PART I : INTRODUCTION

The Prototy-pe

1 . Dwight D. Eisenhower and Bertrand H. Snell Locks are located

on the St. Lawrence Seaway between Lake St. Lawrence and the St . Law­

rence Seaway International Bridge (Figure 1) . Both locks have side port

systems for filling and emptying the 80- ft - wide* by 860- ft - long cham­

bers . Lifts vary from 38.5 to 42.5 ft at Eisenhower and remain near

46 ft at Snell . The existing period of navigation without ice flushing

devices is approximately April through November . With the proposed

ice flushing system, the navigation period could be extended approxi­

mately two months, allowing navigation from March through December .

Description of the Prototype Problem

2 . In the early spring (and sometimes late fall) when navigation

is under way and there are ice formations in the river, considerable

problems occur in clearing the lock approaches and chambers of ice to

permit vessel transits. Conditions are such that, upon a downbound

entrance into the lock, a vessel tends to move the ice ahead of its bow

and push the ice into the chamber . The proposed ice flushing system

will enable moving ice masses out of a lock chamber quickly, safely,

and completely without causing undue strain and stresses to develop in

the present lock operating equipment . As a result, the plans for ex­

tending the navigation season will be greatly enhanced .

* A table of factors for converting U. S . customary units of measure­ment to metric (SI) units is presented on page 3.

4

Page 8: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

- N- ONTARIO

SEAWAY INTERNATIONAL BRIDGE Q U E B E C

SALMON RIVER _...__ ____ _ INTERNATIONAL BOUNDARY

EISENHOWER LOCK MORRISBURG .... · --r.'-

MASSENA MASSENA AIRPORT

IROQUOIS LOCK N E W Y 0 R K

IROQUOIS DAM

Figure 1 . Vicinity map

Page 9: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

Sometimes as many as five or six ice lockages are necessary before the

vessel can be "locked through." These ice lockages are extremely slow,

and each lockage consumes as much as 30 to 45 min of time before the

chamber can be partially cleared.

3. The lock filling and emptying system is presently used for

the ice lockages . First , the ice is drawn into the chamber by closing

the upstream culvert valves and partially opening the downstream valves

to create a current into the chamber by drawing the water through the

ports . (This would be similar to lmvering the lock chamber , except that

the upstream miter gates are opened to allow the ice to enter . ) Once

the ice is in the chamber , the upstream miter gates are closed and the

downstream culvert valves fully opened as in a normal lockage . When

the chamber is at low pool , the downstream miter gates are opened and

the downstream culvert valves are closed. The upstream valves are then

partially opened and a current is created in the chamber by allowing

water to enter the chamber via the ports . As the current moves down­

river , it carries the ice along . The whole process is extremely slow ,

inasmuch as extreme caution has to be maintained to protect the equipment

from surges, ice jamming against the gate , etc ., which can happen if the

valves are opened too much. This whole operation, besides being ex­

tremely slow, only partially clears the lock chamber since there is no

way to create a current and clear the ice from the chamber in the area

between the upstream miter gate and the most upstream filling port as

shown in Plate 1 .

Purpose of Model Study

4. Model tests were conducted to determine the most effective

ways and means to move ice masses out of a lock chamber quickly , safely ,

and completely, without causing undue strain and stresses to develop in

the present lock operating equipment . The object of the tests was to

develop a system that would flush the ice from the entire lock chamber

without using the filling and emptying system .

6

Page 10: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

PART I I : THE MODEL

Description of Model and Appurtenances

5. An existing 1 : 25- scale lock model was used for the study . It

reproduced 800 ft of upstream approach, the entire filling and emptying

system including intakes , valves, floor culvert system , lock chamber,

and outlet basin , and about 600 ft of downstream approach . The model

was modified to simulate only the pertinent physical features of Eisen­

hower and Snell Locks. The most significant revisions were to the lock

chamber . The filling system was simulated , although it was not used

during flushing tests . Basic geometric and structural features such as

the bottom shape and ship bumper were considered significant to the

tests and subsequently were accurately reproduced . The model flume is

shown in Figure 2 .

~; I 1- 19

Figure 2. Inside test flume; looking up­stream to ship bumper (in black) and

type 1 ice flushing manifold

1

Page 11: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

6. Discharges through the ice flushing diffuser were measured

with a rotameter and/or V- notch weirs, and water- surface levels were

set with piezometers and staff gages. Flushing times were taken with

hand stopwatches and electronic timers .

7 . A low- density polyethylene material which has the same density

as ice was used to simulate 10- by 10- ft blocks of ice both 1 . 5 and

3 . 0 ft thick .

Scale Relations

8. The accepted equations of hydraulic similitude , based on

Freudian relations , were used to express mathematical relations between

the dimensions and hydraulic quantities of the model and prototype .

General relations for transference of model data to prototype equiva­

lents are as follows :

Characteristic

Length

Area

Velocity

Time

Discharge

All characteristics in this

Dimension

L

12 R

~/2

11/2 R

15/2 R

Model :Prototype Scale Relation

LR - 1:25

~ - 1 : 625

VR - 11/2 - 1 : 5 R

TR - 11/2 - 1 : 5 R

QR - 15/2 - 1 : 3125 R • report are glven ln prototype dimensions.

8

Page 12: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

PART III: TESTS AND RESULTS

Test Procedure

9 . The lock chamber water surface was covered with 10- by 10- by

3- ft blocks of ice to determine the efficiency of various types of mani­

folds and manifold positions required to flush the blocks from the cham­

ber . Efficiency was measured by the manifold discharge and velocity

versus the time required to move the ice mass various distances in the

chamber . Various ice loads and relative spacing between ice blocks were

tested to establish realistic flushing times . Special consideration was

given to developing a system that would elimi nate the use of the filling

and emptying valves for ice flushing operations or otherwise develop un­

due stresses on the present lock operating equipment .

Low Discharge- High Head Manifold

10 . During the initial tests , discharges of 100, 150 , 200 , and

300 cfs were pumped at heads of 60 ft from various locations withi n the

lock chamber to the ice flushing manifold beneath the ship bumper . The

initial diffuser consisted of a 2- ft - diam manifold (type 1) with five

0 . 92- ft- diam , 4- ft - long nozzles . The manifold was submerged 34 ft below

lower pool as shown in Figure 3 . The 4- ft- long nozzles did not allow

the jets to spread over the width of the lock chamber , and tests were

conducted with various lengths of nozzles to determine their optimum

length, which was found to be 2ft (type 3 manifold) . Shorter lengths,

unsymmetrical jets, or improper jet angles created eddies that reduced

flushing efficiency. Photo 1 shows flow conditions with the type 3

design with the upper third of the chamber initially covered with i ce .

This design moved the blocks 200 ft downstream in 350 sec (prototype)

with a total discharge of 200 cfs (60-ft head); however , it was not

effective in removing the ice from the entire lock chamber .

11 . The manifold was raised to the elevation of the lower pool

and tests were conducted with the nozzles discharging horizontally along

9

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• •

~ ST\IDV Of ICC fW~HI .. c; ,lOOM

ST LAWRENC£ SUWAY l OCKS SCAU

1 n .. oon .. 2~ n. ~Tu~

Figure 3. Close- up of ship bumper and type 1 ice flushing manifold

• •

the water surface . This greatly improved the efficiency of the system

and was designated type 4 manifold (Plate 2 ) . Flow conditions with this

design are shown in Photo 2 . The blocks were moved from the upper

220 ft of the lock chamber in 180 sec with a discharge of 200 cfs ; how­

ever , this design was not successful in removing the blocks from the

entire lock chamber .

12 . Tests were conducted with one, two , and three jets discharg­

ing horizontally from the manifold. The efficiency of any of these

designs was about the same as with design 4 with only the upper 250 ft

of the lock cleared of ice . Flow conditions with only one jet in the

center of the chamber (manifold 6) are shown in Photo 3 .

13 . Various angles of discharge were tested with the manifold

submerged 1 t o 6 ft below the water surface; however , none of these

designs was as effective as the horizontal discharge along the water

surface of t he lower pool .

10

Page 14: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

14. During all of the above tests, the water was pumped from the

lock chamber , 50 ft below the lower pool. Four different intake loca­

tions along the lock center line were tested (sta 0+50 , 2+20 , 4+30, and

6+00); and sta 0+50 (Plate 2) was found to be the most effective loca­

tion . Flow was also withdrawn from the side culvert in an effort to

create a circulation pattern capable of moving the floating ice the full

length of the 860- ft chamber without success.

15 . Several tests were conducted in an existing 3- by 3- by

40- ft- long glass flume to observe the current patterns produced by vari­

ous heads and discharges from multipart manifolds in an effort to capi­

talize on any helpful ice flushing currents in a homogeneous chamber.

No obvious helpful current patterns were generated during these tests,

indicating that only high discharges would effectively move large ice

masses from the lock chamber.

High Discharge- Low Head Manifold

16 . During tests with low discharges pumped at high heads , it

became obvious that lar ger discharges would be necessary to completely

flush the ice from the lock chamber . It is desirable to obtain these

discharges in the prototype with gravity flow from the upper pool rather

than by pumping . Heads of 38.5 to 42.5 ft at Eisenhower Lock and 46ft

at Snell Lock are available for gravity flow water- supply systems to

the flushing manifold. Previous tests had also indicated that the best

flushing was produced with the manifold jet or jets discharging horizon­

tally at the water surface ; however, consideration had to be given to

accommodating a 2- or 3- ft variation in the chamber water surface and

preventing spray which would generate additional ice. Supply pipes

4 ft in diameter were used to provide the large discharges and accommo­

date the variation in tailwater, thereby eliminating the need for an

adjustable manifold. Also , ice generation should be minimized with this

size jet since there was no spray at the manifold . A 40- ft head was

used for comparison of the various manifold designs; however, higher

heads were tested with the recommended design .

11

Page 15: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

17. Tests were conducted to determine the effect of varying lock

chamber water levels on the time required to rid the chamber of ice.

Results of tests with three different water levels are plotted in

Plate 3, indicating that the half-submerged jet is best for total flush­

ing. Therefore, the center line of the flushing jets should be posi­

tioned at the normal lower pool (Plate 4) to provide the best flushing

and remain effective within the expected range of varying tailwater.

As shown in Plate 3, prototype times of 67, 50, and 43 min were required

to flush 220 lin ft of 10- by 10- by 3-ft-thick ice blocks from the

860- ft - long chamber with the two 4- ft- diam jets discharging a total of

580 cfs while fully submerged, nonsubmerged, and half submerged. Move­

ment of the ice during the tests with the jets half and fully submerged

is shown in Photos 4 and 5, respectively . Since less time was required

to remove the ice from the chamber with the manifold center line even

with the water surface, all remaining tests were conducted with the

discharge jets half submerged.

18. The effects of increased discharge on the time required to

rid the lock chamber of 220 lin ft of ice were determined with two,

three, and four 4- ft-diam pipes located beneath the ship bumper. The

two pipes were spaced 13 ft from the lock center line; the third pipe

was placed on the center line; and with the design using four pipes ,

the pipes were spaced on 16- ft centers across the lock width . Each of

the pipes had separate intakes in the approach area . Total flushing

times for respective discharges of 580, 830, and 1080 cfs were 42, 39,

and 29 prototype minutes as shown in Plate 5 .

19 . A multiported manifold (Figure 4) which had twenty 1- ft-diam

ports on 3-ft centers was sensitive to jet alignment and produced eddies

that kept the ice in the lock chamber when flow was directed other than

parallel to the lock walls. Even with properly directed flow, the multi­

ports tested were less effective than 2, 3, or 4 larger jets with equal

discharge .

20. In an effort to reduce the time required to completely flush

the lock chamber, tests were conducted with two 4- ft - diam pipes beneath

the ship bumper and two entering the lock chamber at sta 2+75 at a

12

Page 16: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

MODEL STUDY OF ICE FLUSHING

FROM

STLAWRENCE SEAWAY lOCKS SCALE

I FT {MODEL =2$ FT. (NATURE)

Figure 4. Multiported manifold (half submerged) discharging 580 cfs , 150 sec (prototype) after starting

Page 17: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

45- deg angle . A discharge of 580 cfs from the two upstream pipes moved

120 blocks of ice to sta 2+75 in 450 sec , at which time the two side

pipes were opened to discharge an additional 500 cfs . Movement of the

ice during these tests is shown in Photo 6 . The best flushing time ob­

tained with this design and 1080 cfs was 28 min, compared with 29 . 5 min

with all four pipes located beneath the ship bumper and the same dis­

charge . Since the pipes along the sides would be considerably more

costly to install in the prototype locks , they were considered unworthy

of further testing .

21 . While the model study was being conducted it was determined

that the intakes for the discharge pipes could possibly be located in

the upper gate sill . This would eliminate considerable energy losses

that were present with the original model piping and valves and increase

the discharge from the 4- ft - diam pipes . The model piping was rearranged

as shown in Plate 4. This increased the discharge for each pipe to

approximately 480 cfs with the 40- ft head .

22 . Optimum flushing of the surface ice with a 40- ft head was ac ­

complished with four 4- ft- diam pipes spaced 16 ft apart between the lock

walls and a total discharge of approximately 2000 cfs released parallel

to the lock walls as shown in Plate 4 . The average total flushing time

for 120 blocks of 10- by 10- by 3-ft ice was 15 min . Additional total

flushing times and relations between length of ice movement versus time

throughout tests with discharges up to 1920 cfs are shown in Plate 6 .

23 . A plot of the total flushing time versus discharge is pro­

vided in Plate 7 for three different ice loads to show the effect of

these loads and discharges upon flushing times . As expected, lighter

ice loads move faster and have less tendency to create jams . Another

factor affecting the total flushing time is the concentration of ice

(relative spacing between ice blocks) which becomes more obvious with

large ice loads as noted by the scatter of data obtained with the

245 blocks of ice in Plate 7. 24 . Reducing the ice thickness from 3 ft to 1 . 5 ft had no sig­

nificant effect on the total flushing times with fifty 10- ft - square

blocks of ice .

14

Page 18: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

25 . An increase in head from 40 ft (Eisenhower Lock) to 46 ft

(Snell Lock) reduced the total flushing times required with 120 blocks

of ice with discharges up to about 2000 cfs as shown in Plate 8 . In­

creasing the total discharge from 1800 cfs (3 pipes) to 2400 cfs

(4 pipes) with the 46- ft head resulted in only a 2- min reduction of the

total flushing time .

26 . Movement of the ice during several flushing operations with

120 blocks of ice , 40- and 46- ft heads, and two and four 4- ft - diam

p i pes discharging from 960 to 1920 cfs is depicted in Photos 7-10;

flow conditions are shown on each photograph . During each flushing

operation, a photograph was taken at intervals representing 0 , 50 , 150 ,

and 300 prototype seconds.

Special Considerations for PrototyPe Installation and Operation

27 . Several observations were made during these tests that could

be pertinent to the installation and operation of the prototype flushing

system. Although opening all ports simultaneously is effective , it is

better to open the valves that discharge flow through the two pipes near

the lock walls first and then open the valves that will control the two

i nside jets about 5 min later . This helps to avoid ice jams , boosts

the ice movement, shortens the flushing time , and conserves water for

power generation. For large ice loads , jams can be created by mooring

b it or miter gate recesses , and discharges of 1500 to 2000 cfs are

needed to assure complete flushing . The optimum flushing operation

should be determined in the prototype by using several sequences of valve

openings that might permit reduced discharges with lighter ice loads .

Regardless of the number or size of pipes chosen to discharge the rec­

ommended flow rate of 2000 cfs , the pipes should be equally spaced

across the lock width and flow should be distributed uniformly across

the lock to prevent eddy action . It is believed that a four- port mani­

fold system capable of discharging 2000 cfs will provide an effective

means of flushing ice from the lock chambers .

15

Page 19: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

Prototype System Designed for Eisenhower Lock

28. Engineers for the St. Lawrence Seaway Development Corporation,

using the test results herein, designed the ice flushing system shown in

Plate 9 for Eisenhower Lock. In attempts to be both practical and eco­

nomical, several modifications were made to the recommended (model)

design. The most significant modification was the use of five 4- ft - diam

manifold pipes which will be supplied from one-directional flow into a

10- ft - diam feeder pipe as shown in Plate 9. Five pipes were essential

to keep equal spacing between the ship bumper supports. The single

10- ft- diam feeder pipe from only one 12- by 14- ft culvert was basically

an economic factor .

29. Engineers at the U. S . Army Engineer Waterways Experiment

Station reviewed the design with the above modifications and computed

the expected head losses through the entire ice flushing system. For

the 42- ft head at Eisenhower Lock, a total head loss of 24 ft was com­

puted leaving an 18- ft effective head at the outlet portals. The maxi­

mum flow release was computed to be 2050 cfs with velocities of 30 to

34 fps . This was in close agreement with the total discharge recommended

from the model study .

16

Page 20: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

PART IV: DISCUSSION OF RESULTS

30 . Model tests were conducted to assist engineers in selecting

the best ice flushing system for the St. Lawrence Seaway Locks . All

tests were concerned with quickly ridding the entire 860- ft- long by

80- ft- wide chamber of ice without using the filling valves, creating

undue stresses on the structure and operating machinery, or passing

excessive volumes of water through the lock.

31 . Efforts to establish helpful ice flushing currents or suffi­

cient water- surface differential with low discharge- high head manifolds

to rid the chamber of ice were unsuccessful. Only partial flushing was

possible with discharges below 1000 cfs for heads up to 60 ft.

32 . A manifold with a relatively large discharge and a low head

is preferred in lieu of a low discharge with high head. The best flush­

ing was produced with the manifold jets discharging horizontally along

the water surface. Consideration was given to accommodating a 2- to

3- ft variation in the water- surface elevation of the lower pool and to

preventing spray which would generate additional ice .

33. Optimum flushing of the surface ice with a 40- ft head supplied

from the upper pool was accomplished with four 4- ft - diam pipes spaced

16 ft apart between the lock walls and a total discharge of approximately

2000 cfs released parallel to the lock walls . The average total flushing

time for 120 blocks of 10- by 10- by 3-ft ice was 15 min. The discharge

from a 4- ft - diam pipe could be slightly different in the prototype and

model, since the bends, valves, etc., will be different. Thus, the

flushing times may be altered somewhat. However, this should have only

a minor effect on the flushing operation.

17

Page 21: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

a . Before test b . 30 sec (prototype) after starting test

Photo 1 . Type 3 manifold , d i scharge 200 cfs (sheet 1 of 2)

Page 22: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

c .

@iCT ;t

M004l SJUOY Of t(' rlUS,WIHG J''ION

STLAWRENCE SEAWA~ LOCKS SCALl

1 '1 tMOOR a26 FT.IHA'Mt(

150 sec (prototype) after starting test

Photo 1 (sheet

d . 350 sec

2 of 2)

MOOft sruov or n nusto!H"Co

•oo~

STLAWRENCE SEAWAVLOCKS SCAU

1 n_ MOOU a 21 n. AAJU>l[

(prototype) after starting test

Page 23: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

NOOU ~uov ~ 11.:1 f\U~"'~ ,.o ... ST LAWRENCE SEAWAY lOCKS

S.C.AL( n MOOU. 25 n NAT\11(

a. Before test b.

Photo 2. Type 4 manifold, discharge

.. ODU. TI,IO"' C. ICI fW'"IMi

"''"' STLAWRENCE SEAWAY LOCKS U AU

1 ,, .. aou. ~ a• n. '-A"TVJtt

----

50 sec (prototype) after

200 cfs (sheet 1 of 2)

starting test

Page 24: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

Wc!l"fl. iUCV ~ Cl ,~,,.G

'ROM

ST LAWRENCE SEAWAY LOCKS

HT I "'OOU .:26F1. NAT\IRE ,

c . 150 sec (prototype) after starting test

Photo 2 (sheet 2 of 2)

Page 25: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

I

I

• ....

M(ltl L T 0 .l 'WW'II"'~ J:AOI<1

STLAWRENCE SEAWAV lOCKS SCALI:

'Fl !MODil ~ 211 f-l NAlURt

,.. _ I I

I j

'

·~

\ I

\

., . . , •

a . 50 sec (prototype) after starting test , discharge 200 cfs

i

WOC I 0 ,.. II'W '"llri(i

•oo~

STLAWRENCE SEAWAV lOCKS SCAL(

I n 4MOOH e26 rt. N~TURl

-,. J

, .... •

b . 50 sec (prototype) after starting test , discharge 300 cfs

Photo 3 . Type 6 manifold , discharge 200 and 300 cfs

Page 26: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

' _,

MOOU $TUDV or IC( ,~Hifrt~

roow ST LAWRENCE SEAWAY lOCKS

sc.ut 1n I WOOU. •alfl'.~HAl\llit( l

a. Before test

b .

MOOD. ST\1 (II: a. f\.1,1'1: ~ lifG

"'"" ST LAWRENCE SEAWAY LOCKS

50 sec (prototype) after starting test

Photo 4. Type 8 manifold (half submerged), discharge 580 cfs (sheet 1 of 2)

Page 27: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

IIIOOtl Sf\IOY Of: ICI fUI'Sif: "'IliG . ..,~

ST LAWRENCE SEAWAY LOCKS SOL<

t n j iOIODil ; 25 "- 1'\AT\IRE

I

c . 150 sec (prototype) after starting test

Photo 4 (sheet 2 of 2)

Page 28: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

a .

Photo 5.

NJOOfi <>lUOY ()j: C1 FlUSHI"'C.

·oo• ST LAWRENCE SEAWAVlOCKS

stAU

Before test

• , .. ~ . ;

• •

b.

Type 8 manifold (fully submerged) ,

IJQIU $TUOV Of IC( fW5HIJIO

FROM

ST LAWRENCE SEAWAY LOCKS SUI.(

1 n ~MOOR • 2S f"t. Ml\IPt

50 sec (prototype) after starting test

discharge 580 cfs (sheet 1 of 2)

Page 29: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

• .woe;.. r .... 1c.1 1\.liSM ~ •

<OOM

ST lAWRENCE SEAWAY LOCKS ...

SCAl£ 1 n MODEl • 26 n. H,AJUR[

c . 150 sec (prototype) after starting test

Photo 5 (sheet 2 of 2)

Page 30: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

,

- .. • r -- ·

a . Before test

.. .. •oe•

ST LA-.at ~C( SU~•• lOO'i

..

b . 50 sec (prototype) after starting test

Photo 6. Two 4- ft jets at sta 0+20 , t wo 4-ft jets at sta 2+75 with 40- ft head , discharge 1080 cfs (the t wo 4- ft jets at sta 2+75 were turned on at 450 sec after starting test)

(sheet 1 of 2)

Page 31: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

c.

IIIICICt$tl."C'W'OJICl~ .... ST l.lWR!HCE SEAWAY lOCXS

suu

150 sec fprototype) after

"

starting test d .

Photo 6 ( sheet 2

.... STlAV.P!IoCE SO•Av lOCKS

600 sec (prototype) after starting test

of 2)

Page 32: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

.I ,.

L...

r-.,J

ST lAWAfNt£ SEAWAY!O<KS ... r' 140011 •:JSfT NA~VIII

"'

Oil ....... - J.

,__J

~ l -I J

ti... I

!tA.l t t ~~:101~ ·~& n h.-tuat

..

... r ,.

~ L ~ ... ~ •

"' J ._... -

a. Before test b . 50 sec (prototype) after starting test

Photo 7 . Two 4- ft - diam jets at sta 0+17 with 40- ft head , discharge 960 cfs ; 120 blocks of ice (10 by 10 by 3 ft) (sheet 1 of 2)

Page 33: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

III<XH l)fN "f "l ' u~ ... "'

""'" ST l AWREWCE St.t.WlV LOC~S

,, • .,.001 ... ;-.r '"T'rll ...

c . 150 sec (prototype) after starting test

Photo 7 (sheet

.... ST lAWRfNC! Sf AWAY lOCKS

'

d . 300 sec (prototype) after starting t est

2 of 2)

Page 34: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

I ' J. , ~

. ~

""" ST lA .. Rt \ :£ S£A"•' I.DCIIS • t" MC:i 2S '1 fll.l,. ••

.. ~ A

"' ..._ ~

-=-

'

C1 >0 .... STu~qf"' O: S£.,1'1\' l'tlOC.,.S

,._ II

I j I J

..

a . Before test b. 50 sec (prototype) after starting test

Photo 8. Four 4- ft - diam jets at sta 0+17 with 40- ft head, discharge 1920 cfs; 120 blocks of ice (10 by 10 by 3 ft) (sheet 1 of 2)

Page 35: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

• ~

ST &.Jo,o.P£"1::£ t;.U;~.i ~s

,

c. 150 sec (prototype) after starting test

Photo 8 (sheet

-«!n :f o ':II 1 "'"'""r, '"'.

SH.AWREhCf sr •w•vtoc•s "' ,. " •21• 11-1. ..

d. 300 sec (prototype) after starting test

2 of 2)

Page 36: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

... ~~ 'h :~~,, r "'"" ..,. .... STLAWRENCE HAWAYIOCKS

"' f" ~ODIL • 2 .. n . !oJ.U;lt

a . Before test

110.; I i "'t' lU .,1..._ , ... ST UWAE~tf SEAWAY LOC~S

""' ''' .. ~. a,;" ,..,.

b. 150 sec (prototype) after starting test

Photo 9. Two 4- ft - diam jets at sta 0+17 with 46- ft head, discharge 1200 cfs; 120 blocks of ice (10 by 10 by 3 ft) (sheet 1 of 2)

Page 37: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

I

.. ....,.,CJ IOC •

ST LM•OEJICf SU"'A' lOCI<S

c . 300 sec (prototype) after starting test

Photo 9 (sheet 2 of 2)

Page 38: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

, • S.f .......

- I

"

\

' ... ST l~WRE~CE SEAW.V LOC•S

·~t

1 w. • .. ,. .. ...., a •

\ \ \

a. Before test b . 50 sec (prototype) after starting test

Photo 10. Four 4- ft- diam jets at sta 0+17 with 46-ft head , discharge 2400 cfs; 120 blocks of ice (10 by 10 by 3 ft) (sheet l of 2)

Page 39: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

·-s· I.J."'!!ti!Cl SlJ~U lOCPS ... .. ""!I>JI .....

c. 150 sec (prototype) after starting test

Photo 10 (sheet 2 of 2)

Page 40: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,
Page 41: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

""0 r )> ....... m tv

,~

SHIP BUMPER

10'

U/S P I NTLE

20'

~I EL 20~

LOWER POOL EL !99

AlAN/FOLD

EL U6

TYPE 4 MANIFOLD

Page 42: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

-o r ):> _. m w

z ~

70

60

50

w 40 Q.. >-~ 0 t-o a:: D..

"' 30 w ~

20

10

FULLY SUBMERGED

NOTE : TWO 4-FT-DIAM JETS AT STA 0+ 20

Cll 1-LIJ ...., u.. 0

z 0

!i u 0 ...J

Q= 560 CFS HEAD= 40FT

100 200 300 400 500 DISTANCE, PROTOTYPE FT

600

NONSUBMERGED

....A ~ 0

700 600

EFFECT OF CHAMBER WATER LEVEL ON ICE FLUSH I NG T I ME

Page 43: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

"U r )> -1 m ~

SHIP BUMPER

VALVE

U/S PINTLE

201

17'

EL 204

LOWER POOL EL 199

4' DIAM PIPE

EL 146

PREFERRED FLUSHING DESIGN

Page 44: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

50

40

z ~ 30 w ~ > .... 0 .... 0 a: ~

... w 20 ~ -....

10

Q=580 CFS

NOTE : HEAD::: 40fT 220 LINEAR FT OF ICE

OL_--~~~~-~~-----L----~------L------L----~----~ 0 100 200 300 400 500

DISTANCE, PROTOTYPE FT 600 700 800

EFFECT OF DISCHARGE (580, 830, AND 1080 CF"S)

ON FLUSHING TIME

Page 45: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

"""0 r > -I m

"'

. z ~

UJ (L

>-.._ 0 .._ 0 a:: (L

-I.U ~ 1-C) z -I <I) ~ .J ~

50

40

30

20

10

<I)

1-UJ ..., ~ 0 zo 0(\1 -+ ~0 U-c 0 .J<I)

"V 6 0

0

NO. OF 4-FT DIAM

JETS

(HALF SUBMERGED)

I 2 3

4

DISCHARGE CFS

480 960

1440

1920

NOTE : 40 - FT HEAD-GRAVITY FLOW

120 BLOCKS OF ICE IN LOCK

ICE BLOCKS - 10FT x 10FT X 3FT

100 200 300 400 500

ICE MOVEMENT, PROTOTYPE FT

19 2o cfS

600 700 800

TOTAL FLUSHING TIMES

EFFECT OF DISCHARGE (480, 960, 1440, AND 1920 CFS)

ON fLUSHING TIME

Page 46: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

-o r )> -I m ......,

z ~

w

70

60

~50 t-o t-o 0:: (l.

... Cl) w ~ 40 t-C) z -I Cl) ::> ...J

~ 30 .:( t­o t-

20

~

\ \

0

\ \

0

0

\ 0

X ""- -

0

0 0

0

0

0 X

10~------------~------------~---------------~------------~

0 500 1000 1500 2000 DISCHARGE, PROTOTYPE CFS

NO OF 4-FT DIAM

JETS

(HALF SUBMERGED)

2 3

4

LEGEND 0 245 BLOCKS OF ICE

0 120 BLOCKS OF ICE

X 50 BLOCKS OF IC E

DISCHARGE CFS

480 960

1440 1920

NOTE: 40-FT HEAD-GRAVITY FLOW

ICE BLOCKS- lOFT x lO FT X 3FT

EFFECT OF ICE LOAD ON TOTAL FLUSHING TIMES

1, 2, 3, AND 4 FOUR- FT- Dl AMETER JET HALF SUBMERGED

Page 47: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

-o r )> ...... m ex>

60

-~ 50 ~

w Q..

>­r 0 r 0 a: 40 Q..

... (f) w ~

r C> z - 30 :r: (f) ::::> _J u. _J c{ r g 20

0

0

\ \ \

~EISENHOWER 40-FT HEAD

SNELL > 46-FT HEAD "-..

0

o"-..

""" .........._-....o 0

NOTE: 120 BLOCKS OF ICE 10FT X 10 FT X 3 FT

----0 ---o 10~--------~--------~--------~--------~--------~------~

0 500 I 000 1500 2000 DISCHARGE, PROTOTYPE CFS

2500 3000

EFFECT OF HEAD ON TOTAL FLUSHING TIMES

1, 2, 3, AND 4 FOUR- FT- DIAMETER JET HALf SUBMERGED

Page 48: ICE FLUSHING FROM ST. LAWRENCE SEAWAY LOCKS · The St. Lawrence Seaway Development Corporation secured the services of the U. s. Army Engineer Waterways Experiment Station to determine,

"1J r )> -f m -o

\

' ' ' '

\

.... '-

A

....... ___ _

_j

ml (!) _j ((

0 0 (/) w 0 0

• lL. ll. . N CD ~ 0 :E

q: q: om ::J (/)

I- I- z8 (!) I-(/) (( (/) w · lL. a> o - m 0 -

q: 0 " ll. ID

I- z cr; lL. (/) w ~ 0

q: 0 I- z (/) w

A

q: (!) (!)

0 (!) 0

0 0 0 0 0 0 • . a>

CD • •

I.{) CD N ~ -

q: q:

q: q:

I-I- I-

(/) EL 204.00 (/) I- (/) (/)

EL 199.00 • ~ EL 19 -1 -· --+ - -

EL 193.00 tJ:1( ~ EL 186.00

I 4 I DIAM I I I

q: I 10 ' DIAM 01 w >-

/ :~ ~ > (( -~L 175.00 *l ~ w

-4. - ._

(/)_j "-Y q: 0 _j EL 166.50 l--1(( q: •: (/) u 0 I,

'• <..U '• LADD ss '• It

Ll

9.00

LOCK

ER 4' DIAM FIBERGL A PIPES

SECTION A- A SLUICE GATE

I - BUTTERFLY VALVE 1 J CULVERT BULKHEA D RECESS

I 1 \ 1 VA L VE RECESS -------,--

1-- -- - - ~ ---- __ ~ -- - ,- CULVERTBULKHEADRECESS

I I MOTOR RECESS I ~ -I I I L ------ J=.=:~---1~-M-I-T~ER-- --'- _ _ _ _ _ _ L- _ _ _ FILLING AND EMPTYING CULVERT

~-- 4 GATE GEAR RECESS • t- -- ~ -1 I '----1

(/)w C/lll. q:- (!)

NOTE: DATUM IS USLS 1935. r--------.Jil. -1'---------~----------------------~ ----~-------------~ 0~ 1CD (( - .,;

I STA 63.00A M ONOL I TH JO I NT

wo ~ (!)- .... -, ,, I­lL. ~ (/)

ST A 24. 00 A MONOLITH JOINT

P LAN

(l)I

8t-. -g.J 0

q:Z t-O C/l:E

ST A 87.008

M ONOLITH JOI NT PROPOSED ICE MANIFOLD

EISENHOWER

FLUSH lNG FOR LOCK