low-cost hydrogen distributed production system development · 2020. 11. 21. · frank lomax,...

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Low-Cost Hydrogen Distributed Production System Development Frank Lomax, Ph.D., P.E., Chief Technology Officer (PI) Rick Todd, Ph.D., Maxim Lyubovsky, Ph.D., C.E. Thomas, Ph.D., Ed McCullough, Chris Van Dyke, Khalil Nasser, Kelly Leitch H 2 Gen Innovations, Inc. June 10, 2008 PD1 This presentation does not contain any proprietary, confidential, or otherwise restricted information

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Page 1: Low-Cost Hydrogen Distributed Production System Development · 2020. 11. 21. · Frank Lomax, Ph.D., P.E., Chief Technology Officer (PI) ... • Bill of material cost meets goal

Low-Cost Hydrogen Distributed Production System Development

Frank Lomax, Ph.D., P.E., Chief Technology Officer (PI)Rick Todd, Ph.D., Maxim Lyubovsky, Ph.D., C.E. Thomas, Ph.D.,

Ed McCullough, Chris Van Dyke, Khalil Nasser, Kelly LeitchH2Gen Innovations, Inc.

June 10, 2008

PD1

This presentation does not contain any proprietary, confidential, or otherwise restricted information

Page 2: Low-Cost Hydrogen Distributed Production System Development · 2020. 11. 21. · Frank Lomax, Ph.D., P.E., Chief Technology Officer (PI) ... • Bill of material cost meets goal

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Overview

• July 1, 2005• June 30, 2008 • Complete

• Barriers addressed• Fuel Processor Capital Costs. • Fuel Processor Manufacturing• Operation and Maintenance

(O&M)• Feedstock Issues. • Control and Safety• Total project funding

– $3.46M DOE funds– $1.89M contractor share

• $450,000 DOE funds in FY05• $400,000 in FY06• $1,997,361 in FY07• $609,354 in FY08

Timeline

Budget

Barriers

• Süd-Chemie, Inc.Partners

Page 3: Low-Cost Hydrogen Distributed Production System Development · 2020. 11. 21. · Frank Lomax, Ph.D., P.E., Chief Technology Officer (PI) ... • Bill of material cost meets goal

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Objectives

Execute on the following specific goals as part of theoverall plan to overcome the barriers identified by theUSDOE and to meet the USDOE technical targets interms of cost and energy efficiency

• Design, build and test a 565 kg/day hydrogen plant for 99.999% pure hydrogen to meet DOE hydrogen $3/kg cost target for SMR and PSA

• Develop a catalyst suite based on our current technology suitable for use with fuel grade ethanol to facilitate renewablehydrogen production

Page 4: Low-Cost Hydrogen Distributed Production System Development · 2020. 11. 21. · Frank Lomax, Ph.D., P.E., Chief Technology Officer (PI) ... • Bill of material cost meets goal

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Milestones

• Commissioned first 565 kg/hr prototype (HGM5001) plant at field site 10/07

• 3,889 production hours on HGM5001 as of May 12, 2008

• Demonstrated sub-scale advanced HGM reactor 1/08

• Shipped 2nd generation 565 kg/hr prototype (HGM5002) 2/08

• Operated EtOH catalysts 1,900 hours

Page 5: Low-Cost Hydrogen Distributed Production System Development · 2020. 11. 21. · Frank Lomax, Ph.D., P.E., Chief Technology Officer (PI) ... • Bill of material cost meets goal

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ApproachFirst steps – analysis and bench scale experiments• Catalyst improvements - done• Balance of plant improvement - done• Advanced reactor design - done

Second step - integration and test improved technology in the existing HGM-2000 platform

1. Incremental improvements - done2. Obtain long-term test data (eventually in commercial test fleet) - done3. Make ongoing progress towards USDOE goals - done

Final deliverable1. Design 565 kg/day plant using DFMA, FMEA and other best practices based on

lessons learned from second step – done2. Construct first 565 kg/day plant – done3. Test first 565 kg/day plant - done4. Redesign 565 kg/day plant based on test results and DFMA - done5. Test second 565 kg/day plant – in process

Page 6: Low-Cost Hydrogen Distributed Production System Development · 2020. 11. 21. · Frank Lomax, Ph.D., P.E., Chief Technology Officer (PI) ... • Bill of material cost meets goal

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1st Prototype plant HGM5001• On time and under budget• Over 3800 runtime hours• Achieved 84% of target output

flow rate• HHV thermal efficiency 96% of

target value• Bill of material cost meets

goal

Page 7: Low-Cost Hydrogen Distributed Production System Development · 2020. 11. 21. · Frank Lomax, Ph.D., P.E., Chief Technology Officer (PI) ... • Bill of material cost meets goal

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Output data for HGM 5001

0

1,000

2,000

3,000

4,000

5,000

6,000

7,000

8,000

9,000

10,000

2000 2200 2400 2600 2800 3000 3200 3400

Flow to reactor (scfh)

Prod

uct

flow

rat

e (s

cfh)

Original superheater 2/3 UA of originalNew sec. blower Flame < 950 CFlame >= 950 C

original bottleneck at 75% of design

Changed operation yields 79% output, but worse efficiency

most recent changes yield 80% to 84% output and better efficiency

Page 8: Low-Cost Hydrogen Distributed Production System Development · 2020. 11. 21. · Frank Lomax, Ph.D., P.E., Chief Technology Officer (PI) ... • Bill of material cost meets goal

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1st prototype thermal efficiency

50

55

60

65

70

75

80

2000 2200 2400 2600 2800 3000 3200 3400Flow to reactor (slpm)

HH

V t

herm

al e

ffic

ienc

y (%

)

Original superheater 2/3 UA of originalNew sec. blower Flame < 950 CFlame >= 950 C

78% HHV Goal from HYSYS simulation

Drooping efficiency at highest feed rates

indicates thermal bottleneck (i.e. heat transfer limitations)

Though below goal, 75% HHV is best in class!

Page 9: Low-Cost Hydrogen Distributed Production System Development · 2020. 11. 21. · Frank Lomax, Ph.D., P.E., Chief Technology Officer (PI) ... • Bill of material cost meets goal

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Efficiency data at optimized operating configuration for 1st prototype

50

55

60

65

70

75

80

40 45 50 55 60 65 70 75 80 85

Percent of rated output

Fuel

Effi

cien

cy, e

xclu

ding

ele

ctric

ity, %

HHV effciiencyLHV efficiency

Page 10: Low-Cost Hydrogen Distributed Production System Development · 2020. 11. 21. · Frank Lomax, Ph.D., P.E., Chief Technology Officer (PI) ... • Bill of material cost meets goal

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HGM 5001 electricity consumption

0

5

10

15

20

25

30

40 45 50 55 60 65 70 75 80

Percent of rated H2 output

Elec

tric

al c

onsu

mpt

ion

(kW

)

Electricity data are sparse because measurement was done onsite, not via SCADA

Electricity consumption reduces efficiency by ~2%, using USDOE approach

Page 11: Low-Cost Hydrogen Distributed Production System Development · 2020. 11. 21. · Frank Lomax, Ph.D., P.E., Chief Technology Officer (PI) ... • Bill of material cost meets goal

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Root cause of shortfall in output and efficiency compared to program goals

• Low heat exchanger UA products• Steam generator and economizer shortfall was predicted

as of last year’s meeting• Reactor shortfall in heat transfer performance was

unexpected

Page 12: Low-Cost Hydrogen Distributed Production System Development · 2020. 11. 21. · Frank Lomax, Ph.D., P.E., Chief Technology Officer (PI) ... • Bill of material cost meets goal

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Process improvements for 2nd

prototype, HGM 5002

Surface areaFlue side Reynold’snumber

Process side Reynold’snumber

Other

Reactor same Increased 50% same

5X lower mechanical stresses

Steam generator

Increased 11%

Increased 20% same

Designed with wall-wetting features

Economizer Increased 39%

Increased 20% same Designed for

10% quality

Page 13: Low-Cost Hydrogen Distributed Production System Development · 2020. 11. 21. · Frank Lomax, Ph.D., P.E., Chief Technology Officer (PI) ... • Bill of material cost meets goal

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Machinery improvements

Direct-drive, low-noise

regenerative air blowers

Small compromises in BOM cost andPower consumption have been made for HGM 5002 to maximize reliability

Geared drive, redundant feed water

pumps

Page 14: Low-Cost Hydrogen Distributed Production System Development · 2020. 11. 21. · Frank Lomax, Ph.D., P.E., Chief Technology Officer (PI) ... • Bill of material cost meets goal

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Packaging improvements

•Major focus on reducing clutter, aiding access for service•Remedying any points of subtle vibration, or weakness of mounting points (step proofing)

Page 15: Low-Cost Hydrogen Distributed Production System Development · 2020. 11. 21. · Frank Lomax, Ph.D., P.E., Chief Technology Officer (PI) ... • Bill of material cost meets goal

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2nd prototype HGM5002 being installed at field site

• Commissioning underway, but no test data as of May 15• less than 12 months from start of redesign to commissioning

Page 16: Low-Cost Hydrogen Distributed Production System Development · 2020. 11. 21. · Frank Lomax, Ph.D., P.E., Chief Technology Officer (PI) ... • Bill of material cost meets goal

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Ethanol Reforming

• 1900 hr test under the conditions matching that of HGM unit• Demonstrated reforming of ethanol with standard fuel additivesNext steps:• Long term microreactor testing with fuel grade ethanol E95/E85.• Dual fuel (ethanol/PSA waste gas) burner testing.• Ethanol based HGM unit construction and testing.

0

10

20

30

40

50

60

70

80

0 500 1000 1500 2000time, h

Con

cent

ratio

n (%

)

CO2_GC

CH4_GC

CO_GC

H2_GC

• Microreactor aging test.• Ethanol pre-reforming catalyst

followed by standard HGM SMR, WGS catalysts.

• Ethanol column reflux feed• Complete ethanol conversion in the

pre-reforming section

Page 17: Low-Cost Hydrogen Distributed Production System Development · 2020. 11. 21. · Frank Lomax, Ph.D., P.E., Chief Technology Officer (PI) ... • Bill of material cost meets goal

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Future Work• Commercialize 565 kg/hr hydrogen plant (not using

USDOE funds)• Continue EtOH testing, extending to denatured fuel

ethanol• Conduct design for fuel supply and combustor

systems• Test burner system

Page 18: Low-Cost Hydrogen Distributed Production System Development · 2020. 11. 21. · Frank Lomax, Ph.D., P.E., Chief Technology Officer (PI) ... • Bill of material cost meets goal

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Summary

Distributed Hydrogen Generation Targets

Production Parameter Units System Target Achieved by 5/12/08

Hydrogen Output Kg/day 565 475

System efficiency % LHV >67.5 67-68%

Parts Cost $ <$350,000 Proprietary

Field test time hours 2,500 3,889

Ethanol Reforming Target

Catalyst test time hours >1,000 1,900