motor project buet
TRANSCRIPT
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BANGLADESH UNIVERSITY OF ENGINEERING AND TECHNOLOGY
DEPARTMENT OF ELECTRICAL AND ELECTRONIC ENGINEERING
Course No: EEE 208
Course Title: Energy Conversion Laboratory
Project Title: Re-wiring Stator Winding of a 3-Phase Induction Motor
Submitted to:
(1)
Dr. Shahidul Islam Khan
Professor
EEE, BUET
(2)
Hamidur Rahman
Associate Professor
EEE, BUET
Submitted By:
Name Student I.D.
Md. Redwan Islam 1006066
Md. Rayhan Khan 1006067
Abdullah Abu Sayed 1006068
Arifuzzaman Faisal 1006069
Kamruzzaman Nahid 1006070
Mohammad Tariqul Islam 1006071
Md. Khalid Mahmud 1006072
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Objective:
1. To study the structure of a three phase induction motor.
2. To re-wire the stator winding of a squirrel cage induction motor.
Description of the Motor:
A motor with following nameplate is bought:
TEECO 3PHASE INDUCTION MOTORTYPE MS 712-4 IP 44
0.5 HP 0.37 KW 440 V
Y 0.97A 1400 rpm
INS. OL. B 50 Hz S1
STANDARD JB/T 1009-2007 NO.
TEECO STANDARD MOTORS LTD.
Discussion about the Stator Winding:
The stator winding is observed and the following data is obtained:
Type of Wire 26 Gauge (0.405 mm diameter)
Stator Type Semi-closed Slot Stator
No. of Slots 24
Connection Type 4 pole Y - Connected
No. of Layers 1
Wires in each Slot 165
From the nameplate, this is a Design Class B motor. So, expected maximum torque is
moderately high.
The stator winding follows the following diagram:
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The YConnected Stator is shown in above figure. The phases follow the following pattern:
Phase No. Winding Direction Color in the figure
a Phase 01-06-12-07-13-18-24-19 Red
b Phase 05-10-16-11-17-22-04-23 Blue
c Phase 09-14-20-15-21-02-08-03 Green
The terminals 19, 23 and 03 are shorted. And terminals 01, 05 and 09 are the 3 phase voltage
input.
Procedure:
1. The motor is dismantled under the supervision of Lab Assistant Mr. Debashish. The
following picture is taken:
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2. Then the motors stator winding is completely removed.The following is a picture of
stator after the wires has been removed:
And the following picture is of wire:
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3. Then the winding was done again with the wire of same diameter:
4. After this the motor parts have been re-assembled.
Tests:
Weight of Removed Stator Winding:
980 grams.
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DC Test:
Parameters Value
RDC 49.4
No Load Test:
Parameter Value
Vnl 400V
Inl 0.9A
Pnl(1 Phase) 42W
Locked-Rotor Test:
Parameter Value
Vlr 90V
Ilr 0.97A
Plr(1 Phase) 31W
Motor Parameter Calculation:
From DC Test:
R1= RDC/2 = 49.4/2 = 24.6
From No Load Test:
V,nl= 230.94V
Znl= V,nl/ Inl= 256.6
Now,
R12+ (X1+XM)
2= Znl2
from this expression,
X1+XM = 251.8
From Locked Rotor Test:
Note: Locked Rotor test was done in 50Hz (line frequency)
V,lr=51.96V
Zlr=V,lr/Ilr=53.57
lr=cos-1(P/(V,lrIlr)) = 52.04
Now,R1+R2= Zlrcos(lr) = 32.95
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Xlr=X1+X2= Zlrsin(lr) = 42.23
Now,
R2=32.95-R1=8.35
Since it is a design B motor,X1=0.4Xlr=16.869
X2=0.6Xlr=25.338
XM=251.8X1=234.931
So, the data obtained are:
Parameter Value
R1 24.6
R2 8.35X1 16.869
X2 25.338
XM 234.931
Discussion:
While re-wiring we phased some complications. These are listed below and it is also
explained how the complications were dealt with:
1. The lamination in the stator was damaged in the process of removing old stator coils. As aresult the stator needed re-lamination.
2. While removing the old winding and re-wiring, we accidentally displaced some of the
walls of stator slots. This created a problem while we tried to install the rotor after re-wiring.
Since the air gap is too small, a small displacement resulted in the rotor being stuck. This
problem was removed by hammering in the places which were displaced. The displacements
were removed as much as possible.
3. The wooden mount required for shaping the coils was acquired from a machine shop. But,
while using the mount, some of the wires got tangled and resulted in larger diameter coil thannecessary. As a result the coils didnt fit in the slots. These coils had to be prepared for the
second time.
4. Due to the Semi-Closed Slot, the coils could not be inserted directly into the stator, rather
special mechanism was required. Feeders or Insulating Papers were inserted into the stator so
that the lamination of stator and insulation of wires dont get damaged. Since it is a single
layer winding the complications were limited.
5. After the wiring is done, lamination coating was again applied on the wires.
6. The values obtained in Blocked Rotor Test are not completely correct. As, the frequency of
text was 50Hz, the obtained value is highly erroneous.