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    Copyright 2006, IADC/SPE Drilling Conference

    This paper was prepared for presentation at the IADC/SPE Drilling Conference held in Miami,Florida, U.S.A., 2123 February 2006.

    This paper was selected for presentation by an IADC/SPE Program Committee followingreview of information contained in a proposal submitted by the author(s). Contents of thepaper, as presented, have not been reviewed by the International Association of DrillingContractors or Society of Petroleum Engineers and are subject to correction by the author(s).The material, as presented, does not necessarily reflect any position of the IADC, SPE, theirofficers, or members. Electronic reproduction, distribution, or storage of any part of this paperfor commercial purposes without the written consent of the International Association of DrillingContractors and Society of Petroleum Engineers is prohibited. Permission to reproduce in printis restricted to an abstract of not more than 300 words; illustrations may not be copied. Theabstract must contain conspicuous acknowledgment of where and by whom the paper waspresented. Write Librarian, SPE, P.O. Box 833836, Richardson, TX 75083-3836, U.S.A.,fax 1.972.952.9435.

    AbstractWells drilled into the deep Bossier formations of the east

    Texas Hilltop Field encounter low-permeability, gas-bearing

    formations at over 15,000-psi pressure and 400Ftemperatures. The wells require high-pressure fracture

    stimulations and extreme production drawdown to produce at

    economic rates. Wellbore temperature variations occurringbetween stimulation and production operations are extreme.

    The gases in these formations are also highly corrosive. Two

    of the first three wells completed in this area failed fromcasing collapse during completion operations or within the

    first few weeks of production.Finite element analysis (FEA) modeling coupled with log-

    derived formation properties confirmed that the extreme

    stresses applied to these wells rendered previous casings andcement sheaths under-designed. Using an approach that

    combined formation, casing, and cement mechanical

    properties into a system, the wells were redesigned. Detailed

    thermal and mechanical modeling of all wellbore operations

    resulted in redesigned casings and a cement sheath moreapplicable to the extreme loads being exerted. Minor changes

    were also implemented to the job placement procedures to

    lessen the loads placed on the cement sheath.

    High-strength, corrosion-resistant casings and specialtycement designs were successfully used on the first two wells.

    Since those wells have been on production, additional wells

    have been drilled and completed using incrementally-

    simplified designs. All the wells have withstood multiplestimulations at treating pressures exceeding 14,000 psi,

    production test drawdowns at the perforations of over 13,000

    psi, and temperature changes estimated at more than 300F.

    The wells have withstood these extreme pressure andtemperature changes without failure of either the casing or

    cement sheath.

    The cement and casing designs employed have proven

    competent for the high-pressure, high-temperature (HPHT)conditions encountered. The successful design methodology

    couples well-specific casing and cement designs into a system

    capable of surviving the extreme pressure and temperatureconditions imparted on the well during stimulation and

    production operations of deep, low-permeability HPHT gas

    sands.

    IntroductionConstruction of deep gas wells involves a large capita

    expenditure, and they are typically prolific wells. In addition

    remedial work can be very costly, not only in terms of los

    production, but also in the cost of materials and serviceneeded to perform the work. Catastrophic well failure

    although rare, does occur and can doom remaining reserves in

    place when it happens. Hence, there is a large incentive to do

    things right the first time.The traditional focus of the cementing job of designing

    adequate slurry properties and getting the slurry properly

    placed still applies, but that is only the beginning. As these

    wells are completed and produced, the cement sheath isdesigned to survive extreme stresses. Wellbore longevity wil

    depend not only on how the cement sheath is designed to

    impart maximum sealing properties, but also on how it

    behaves when coupled to the casing and formation during alwell operations. All operations and their associated timing

    with respect to the completeness of the cement hydration are

    fair game for investigation, including: Continued drilling operations (in the case of intermediate

    casings). Completion operations (e.g. completion fluid

    circulations and stimulation treatments). Well testing (e.g. pressure testing, severe drawdown

    tests, etc.). Access to various annuli for pressure control during

    thermal changes. The effects of gradual drawdown during long-term

    production.

    BackgroundPrior well designs in the Hilltop area consisted of what will be

    referred to as first-through-third generation designs. The first

    generation well was completed with a conventional 2-D casing

    design. Completion procedures consisted of nothing more thanacidizing the formation and placing the well on production

    IADC/SPE 98869

    Finite Element Analysis Couples Casing and Cement Designs for HP/HTWells inEast TexasJ. Heathman, Halliburton, and F.E. Beck, Gastar Exploration

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    2 IADC/SPE 98869

    This well started producing drilling mud approximately 3

    months later, and was subsequently found to have undergone

    casing collapse. This was quickly followed with a second wellfor which improved tubular designs were employed. This

    design did not collapse, but the well failed because of an

    insufficient completion methodology.

    The third-generation well was designed with a more robust

    and presumably adequate casing and cementing program, asshown in Fig. 1. This casing design was intended to withstand

    full evacuation. The wells were cemented, cleaned out with

    KCl water, perforated, and multiple formations weresuccessfully stimulated down casing at 20 bbl/min at over

    13,000-psi surface pressure using high-strength proppant.

    During the course of post-stimulation flowback at full

    drawdown rate and maximum heating, this well also collapsed

    in the lower part of the well.When the current production company acquired the lease

    after the three previous wells had failed, a review of the casing

    design using a thermodynamic casing analysis model did notindicate that the casing for the third-generation well had been

    under-designed. This observation resulted in speculation about

    causes ranging from a faulty coupling or joint of casing,

    formation effects, some sort of cement sheath failure, to a

    combination of these factors. It appeared that at least one ofthe failures occurred in the tieback string just above the

    polished-bore assembly. It was also speculated that a trapped

    mud pocket might have existed between the cement above thePBR and the liner top below that subsequently expanded due

    to thermal effects when high-rate flow-back and production

    started. However, no definitive evidence indicated that any of

    this was the case. Subsequent modeling with casing design

    software and FEA was never able to determine a cause.

    Following the mechanical failure of this well and thesubsequent lack of an obvious cause, or a consensus regarding

    the most likely cause(s), this operator elected to step back andrevisit the entire well design. Before drilling another of thesewells, the plan was to perform a detailed analysis of the casing

    and its metallurgy, the couplings, and the cement sheath.

    Finite Element AnalysisThe coupled wellbore modeling was conducted using asoftware that has as its core the DIANA finite elemental

    analysis program from the Diana Corporation. This software is

    a practical wellbore model in the sense that it takes intoaccount all forces exerted on the cement sheath, casing, and

    formations caused by pressure and thermal changes. This

    design software was developed over several years and has

    proven itself in numerous situations.1-4

    In the model, the system composed of the formation

    material, cement, and casing are divided into a finite numberof parts, or elements, so that the governing equations can be

    solved. When analyzed, each element must satisfy the

    relationships and constraints set forth by the user so that asolution is found. This can enable not only a diagnosis of the

    elements, but also a diagnosis of the boundaries between each

    layer. Subsequently, the presence and width of microannuli or

    cracks resulting from debonding can be predicted.

    The radius of the surrounding formation when modeled issuch that far-field stresses remain unchanged. However, near-

    field stresses can affect not only wellbore elements but also

    the competency of the formation itself. This mode

    accommodates all wellbore operations, as well as reservoir

    changes caused by pressure drawdown and formation

    subsidence. Interpretation of modeling results can produce arange of solutionsranging from simple modifications to

    operational procedures or wellbore design to a complex

    cement sheath redesign, or any combination thereof.

    Problem Setup and Initial AnalysisTable 1and Figs. 1 through6provide a substantial portion of

    the initial well design, formation, and operational event data

    used in the FEA model. The new casing program, herein

    referred to as the fourth-generation design, shown in Fig. 7

    addressed metallurgical and well delivery constraints of the

    previous design. Because CO2and H2S had been observed in

    previous wells, with as much as 400 ppm and 14%

    respectively. Additionally, a larger production casing diameter

    was desired (than had been used previously) to accommodate

    more aggressive stimulation treatments and production ratesBefore beginning the FEA work, a careful design analysis o

    the casing was performed using a 3-D casing design model to

    ensure that the design was robust enough for the intendedsevere well testing program. The design limit plot of Fig. 8is

    a result of that work. Heavy-wall casing, premium couplings

    and super-alloy metallurgy became a part of these HTHP

    wells.

    Model Setup and Initial AnalysisConcerns regarding casing design were alleviated because the

    new design enabled greater flexibility in withstanding severeconditions during formation testing and stimulation treatment

    The next step was reinitiation of the cement sheath

    examination. Using the new casing design as the basis for all

    modeling, the original cement sheath design was first

    examined to establish a new baseline case. Mechanicaproperties of all cements modeled were determined using atriaxial load cell at unconfined and various confining loads

    The wellbore was examined at multiple depths, the most

    important being in the top of the reservoir sand, just below theprevious casing shoe, and at depths that offset logs indicated

    substantial changes in formation lithology, pressures, and in-

    situ stresses. This multiple-depth investigation not only helps

    provide an understanding of the cement sheath behavior a

    many different conditions, but also can enable a sensitivityanalysis by allowing a review of how the cement is behaving

    across the various formations.Fig. 9 is an example of the remaining capacity summary

    associated with each operation. Although numerous depthswere modeled, only the modeling at true vertical depth (TVD

    of 18,000 ft is shown (for brevity). Despite the robust casing

    design, multiple failure modes were predicted in the cement

    sheath, most noticeably debonding with subsequen

    development of a substantial microannulus and shear failurewithin the cement matrix. This failure pattern occurred to

    varying degrees of severity at all depths of investigation. Even

    for those load cases where failure was not predicted, someremaining capacity predictions could have been interpreted as

    being at high risk. Finally, a sensitivity analysis conducted by

    varying the values of parameters such as the casing

    eccentricity, hole washout, and Mohr-Coulomb parameters

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    IADC/SPE 98869 3

    indicated the modeled well was extremely sensitive to

    relatively small variations in these key variables.

    Scenario ImprovementThe analysis process at this point consisted of altering the

    operational and completion parameters to look further at

    model sensitivity and for ways to offset the cement failures

    predicted. Improvements were seen by (1) reducing the pre-frac pressure drawdown, (2) performing the frac job through

    tubing and packer rather than down casing, and (3) altering the

    completion plan such that the cement job would be displacedwith brine instead of the previous procedure of displacing it

    with the heavy drilling mud and later replacing it with a light

    completion brine. While all these changes provided

    incremental improvements, only the last change was feasible

    for the design of this well.Fig. 10 provides the remaining capacity summary of the

    best-case completion scenario using the existing conventional

    cement design. While displacing the cement job with 3% KClwater would have been the most desirable plan from a

    mechanical standpoint, the resulting surface pressures while

    displacing the cement would have been substantial. After

    working both job simulation models and the FEA program

    congruently, it was decided that the best tradeoff for adisplacement fluid was a completion brine no heavier than 13

    lb/gal. But this maximum brine density value was contingent

    upon the accuracy of the data being placed in the model; thus,the general idea was still: the lighter the better.

    Another advantage of displacing with brine rather than oil-

    basesd mud (OBM) is that it eliminates the rig time and

    expense of cleaning the OBM from the casing prior to

    perforating. However, this still placed an allowable limit of no

    less than 5,500 psi during the prestimulation drawdown test;therefore, while improvements would have been gained, shear

    failure and debonding were still predicted.To achieve all the desired goals of this well, the only

    alternative was to modify the mechanical properties of the

    cement sheath. The positive modifications that were

    logistically and economically feasible (as shown in Table 2 as

    third-geneation completion procedures) were implemented

    from this point forward to minimize the changes required tothe cement sheaths mechanical properties.

    New Cement DesignSensitivity analysis indicated that any new cement design

    would have to possess much lower values for Youngs

    Modulus and friction angle and higher values for cohesion,

    tensile strength, and Poissons ratio. Also, it was obvious thatbulk shrinkage from cement hydration could not be allowed.

    Achieving these goals in a lightweight cement is relativelysimple. However, the high solids content of a 19-lb/gal slurry

    does not lend itself to becoming essentially an elastic

    cement. Foamed cement would have been the easiest cementin which to achieve the desired mechanical properties, even at

    a final downhole density of 19 lb/gal, but foamed cement is

    not conducive to an environment that might reach more than

    395F bottomhole circulating temperature (BHCT) during

    slurry placement. Another option, ground-up recycled tirerubber, used for many years as a lost-circulation material, was

    deemed undesirable for these conditions because it could

    degrade with time at high temperature.

    To achieve the desired properties, a copolymer elastomer

    bead was chosen as a large portion of the cement blend. Thismaterial, in conjunction with a gas-generating additive and

    careful selection of other conventional components, provided

    the cement mechanical properties needed for the anticipated

    stresses. Fig. 11provides the remaining capacity summary ofthe final well design at 18,000 ft. Note that the remaining

    capacity for the cement-to-formation debonding prediction is

    very low. While this level of risk may be unacceptable in

    some situations, repeated runs of the model showed very little

    sensitivity to change. In addition, this interval was in themiddle of the long lower Bossier sand that was expected to be

    perforated and hydraulically fractured. Analysis did not show

    a gas/water contact on previous wells at this depth; thereforethe risk was considered acceptable. The remaining capacity of

    the debonding prediction was considerably higher at other

    depths under investigation.

    To conclude the analysis, the cement design chosen for

    this high-stress HTHP application was subjected to a varietyof tests. Because of a great variance in the specific gravities of

    the major components of this blend, concerns emerged

    regarding the deblending during pneumatic transfer andtrucking to location, and about the slurrys mixability. Table 3

    shows the results of specific gravity checks pulled from the

    blend at different times during the handling process, indicating

    no significant effects. Slurry mixability was indeed found to

    be slow, thus the decision was made to batch-mix this blend

    on location.Flow testing through float equipment for 2 hr at 215

    gal/min indicated no issues with float equipment erosion or

    plugging. The slurry was then mixed for a yard test andpumped into a wellbore model cured at 420F. This mode

    was subjected to pressure and thermal cyclic loads whilemonitoring the integrity of the cement-to-casing bond. Fig. 12

    shows a cross-section of the model after cycling for which no

    debonding or sheath damage was observed, based onlongitudinal pressure testing with water and nitrogen. For

    comparison, Fig. 13shows results for a conventional cement

    subjected to the same testing. Note the visible cracks anddebonding that occurred.

    All the testing was successful, which instilled confidence

    in the team that this blend could be placed and would perform

    as designed.

    Examination of Shallower (Previous) Casing Strings

    After the casing, cementing, and completion designsassociated with the 5-in. production casing had been

    thoroughly explored, design analysis progressed to theacceptability of the 7 5/8- and 9 5/8-in. casings and associated

    cement sheaths used previously. The 9 5/8-in. casing was a

    full casing string that could provide an annular leak path to

    surface. The operation was expected to cover potentiallyproductive intervals up through the Travis Peak formation. On

    the other hand, the entire 7 5/8-in. liner would be covered with

    cement during the production cementing operation. As a resul

    of these scenarios, emphasis was placed on the 9 5/8-in. casing

    interval. The primary concern, aside from the same long-termzonal isolation as the production casing, was the possibility of

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    sustained casing pressure (SCP) on the 9 5/8-in. casing by the

    13 3/8-in. annulus. SCP has been a growing concern of

    operators and regulatory agencies alike for both land andoffshore installations.5

    FEA Model, 9 5/8-in. Production CasingAs before, the base model for the 9 5/8-in. casing was

    established using conventional cementing programs. Themodel was set up from the shoe of the 13 3/8-in. casing to the

    anticipated depth of this intermediate casing. Four key depths

    were chosen for investigation: (1) the shoe of the previouscasing, (2) the bottom of the lead slurry, (3) the top of the tail

    slurry, and (4) total depth (TD) for this interval. Table 4

    provides a summary of the basic assumptions used in the

    model, and Figs. 14and 15detail the results of this model for

    the lead and tail cements. Several modes of failure aredisplayed for both lead and tail cements; of most interest is the

    unrecoverable plastic deformation in the cement structure. The

    cement-to-formation debonding occurred at all depths ofinvestigation and for all load cases. Both predicted failure

    modes could lead to SCP at the surface during the operating

    life of this well.

    Ensuring the Integrity of the 9 5/8-in. Cement SheathAs with the production casing, the first attempt to improve the

    remaining capacity was to look for (1) events that could be

    modified or removed that cause prestressing of the cementsheath, and (2) potential modifications to the completion

    design or order of events that will not significantly change the

    cement design. In this case, the drilling program did not allow

    for any changes that would prevent cement sheath damage.

    Consequently, the cement design would have to be modified.

    The obvious first step was to prevent bulk hydrationshrinkage. This modification would be achieved as before by

    using a gas-generating additive in both cement blends. Notethat this only prevented shrinkage; no bulk expansion of theset cement was created nor necessary.

    Subsequent runs indicated no further modifications were

    necessary for the cement mechanical properties for the initial

    conditions assumed. However, because of the possibility of

    encountering zones with higher pore pressures, furthersensitivity analysis using the assumed higher values and

    associated mud weights indicated that the nonshrinking

    version of the recommended water-extended, lightweight leadcement could be fairly sensitive to shear deterioration.

    Imparting bulk expansion was not the solution to this potential

    problem. However, minor adjustments were made to the ratio

    of primary components in the blend to affect the Mohr-Coulomb failure variables and the Youngs Modulus. Thisfinal analysis is provided in Figs. 16and 17.

    Finally, unlike the production casing analysis, the goals of

    the well-life analysis were carried out for this casing string

    through some very simple modifications to the cement blendusing conventional additives.

    On-Location DeliveryRefer once again to Table 2 for the operational proceduresapplied to the first well. As expected, the slurry mixability was

    slow. A sustained rate of over 4 bbl/min while mixing on-the-

    fly would not have been possible; thus, the conservative

    decision to batch-mix the 19-lb/gal elastomer slurry was

    beneficial. Because of the high concentration of copolyme

    beads and other components in this blend, rheology

    measurement with a rotational viscometer using aconventional R1/B1 rotor/bob combination was not possible

    A B2 bob was found to work somewhat better, but

    experiments showed that the new yield point adapter (YPA)

    rheometer kit (shown in Fig. 18) was well suited to thisapplication.

    6,7Additionally, the newly-developed generalized

    Hershel-Bulkley (GHB) rheology model was found to providean excellent pressure prediction.8 Fig. 19 provides the

    regression analysis of the data generated using the YPA

    instrument. Fig. 20provides the predicted vs. actual surface

    pump pressures for one of the 19,200-ft wells, illustrating the

    good predictive abilities of this new rheological model forcomplex fluids.

    Cement Evaluation Log of Production CasingThis paper would not be complete without a discussion of theobservations made on the cement evaluation log of the 5-in

    production casing. Although it was desirable to evaluate thi

    unique cement sheath with an ultrasonic tool, no tool available

    will withstand the temperatures of this well, as well asaccommodate both the small ID and large wall thickness of

    this production casing. Because the copolymer beads used

    imparted elastic properties to this 19-lb/gal cement, the log

    was expected to indicate poor attenuation and/or free pipemuch like a foamed cement sheath will behave. This is

    because elastic cement sheaths often do not attenuate the

    casing as does a conventional cement, thus allowing it to ring

    in response to sonic and ultrasonic evaluation tools. HoweverFig. 20indicated this was not the case.

    At the time this log was run, approximately one month

    after the cement had been placed, the wellbore still contained

    the 13-lb/gal brine that the cement job had been displacedwith, and the casing had already been pressure-tested to15,000-psi surface pressure. Under these circumstances

    cement-to-casing debonding occurs and a microannulus is

    nearly always created, as was the case with the nonelastomericlead slurry shown in Fig. 21. Of most interest on this log is the

    fact that the elastomer tail slurry deformed without going into

    plastic failurejust as it was designed. The lead slurry

    though mechanically-altered, was not designed to preven

    debonding due to the pressure test, thus a microannulusappeared periodically throughout the lead cement sheath

    Though caution should always be exercised when interpreting

    an evaluation log of any designer cement sheath, this case

    clearly shows the superior mechanical properties of theelastomer cement.9

    Ongoing Operational Changes and Evolution to TwoWell DesignsOne of the goals of this project was to continually evolve thecasing and cement designs as confidence in the data improved

    so that the wells become optimized to the conditions. This

    continuous process has resulted in simplifications to both the

    casing design and the cementing procedure.

    The high pump pressures associated with the displacemenprogram were of enough concern to revisit the brine density

    Further review with the FEA model with improved and greater

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    IADC/SPE 98869 5

    confidence in the formation property data has allowed the job

    to be displaced with a 12.8-lb/gal brine. This same review of

    improved wellbore data has also enabled the cementingprogram to be optimized in the sense that the elastomer slurry

    volume has been reduced to cover only those portions of the

    wellbore needing it. While this still involves a substantial

    portion of the openhole section, inclusion of a nonelastomeric

    lead slurry with modified mechanical properties has resultedin simplified location logistics and reduced job cost. This step

    has also resulted in lower ECDs during placement.

    Since the start of this project, these wells have encounteredseveral shallower formations that have proven economically

    productive. To speed development field development and cash

    flow, these wells at 10,000- to 15,000-ft TVD are being drilled

    with a reduced casing program. Because of the shallower

    depths and associated smaller pressure and thermaldifferentials, these wells have not required any extensive

    slurry redesign and associated mechanical property

    modifications to date.

    ConclusionsTo date, six HTHP wells have been drilled in the Hilltop Field.

    All have been successfully drilled, cemented, tested, and

    subjected to multiple-zone frac jobs down casing. Withoutexception, the mechanical integrity of all wells has been

    outstanding. Based on tracer surveys, all stimulation

    treatments stayed in zone. As each well was drilled and moreformation data was gathered, the FEA model was adjusted to

    accommodate the improved data. Since the first well was

    drilled and tested, pore pressure/frac gradient confidence in

    the area has allowed the operator to simplify the casing design.

    Electing to stop performing the severe prestimulation

    drawdown testing now that the necessary reservoir data hasbeen gathered has reduced the stresses subsequent wells have

    been subjected to, thus allowing the casing design to besimplified. However, because of these reduced casing designs,it has been imperative to maintain the cement sheath designs

    as originally planned to maintain wellbore integrity.

    This case study shows that, when every facet of a critical

    well is incorporated into a total well design, the resulting

    structural integrity management process can result in secureand economical wells.

    AcknowledgementsThe authors thank the management of Halliburton and FirstSource Gas, LP, and Gastar Exploration, Ltd for permission to

    publish this paper. They are also thankful for the hard work

    and dedication from all the technical and operations personne

    that made this project a success.

    References1. Bosma, M., et al.: Design Approach to Sealant Selection

    for the Life of the Well, paper SPE 56536 presented athe 1999 ATCE, Houston, TX, October 3-6.

    2. Ravi, K.R., et al.: Safe and Economic Gas Wells throughCement Design for Life of the Well, paper SPE 75700

    presented at the 2002 SPE Gas Technology Symposium

    Calgary, Canada, April 30May 2.

    3. Ravi, K.R., et al.: Cement Sheath Design for DeepwaterApplications, paper presented at the 2003 Offshore Wes

    Africa Conference, Windhoek, Namibia ,March 11.

    4. Griffith, J.E., and Tahmourpour, F.: Use of FiniteElement Analysis to Engineer the Cement Sheath for

    Production Operations, paper presented at the 2004

    Canadian International Petroleum Conference, Calgary

    Canada, June 8-10.

    5. Information from Current Methods for Analysis andRemediation of Sustained Casing Pressure, by Staurt

    Scott and Adam T. Bourgoyne, Jr., Petroleum

    Engineering Department and Louisiana State University.6. Dealy, S.T., Morgan, R.G., and Johnson, J.W.

    Viscometer for Multi-Phase Slurries, paper presented at

    the 2005 DEA/IADC Workshop, Galveston, TX, May 24

    25.

    7. Harris, P.C., Morgan, R.G., and Heath, S.J.Measurement of Proppant Transport of Frac Fluids,

    paper SPE 95287 presented at the 2005 ATCE, Dallas

    TX, October 9-12.8. Becker, T.E., Morgan, R.G., Chin, W.C., and Griffith

    J.E.: Improved Rheology Model and Hydraulics

    Analysis for Tomorrows Wellbore Fluids Applications,

    paper SPE 82415 presented at the 2003 Production andOperations Symposium, Oklahoma City, OK, March 22

    25.9. Frisch, G., et al.: Advances in Cement Evaluation Tools

    and Processing Methods Allow Improved Interpretation

    of Complex Cements, paper SPE 97186 presented at the

    2005 ATCE, Dallas, TX, October 9-12.

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    Final mud type (when interval is 18.3-lb/gal Diesel-based OBM

    Bottomhole thermal gradient 1.81F/100 ft

    MD 19,000 ft

    TVD 19,000 ft

    Estimated drilled-hole size 6.7-inch (to be drilled with 6.5-inch bit)

    TOC 14,000 ftModeled range Previous casing to TD

    Designed casing standoff 85%

    Displacement fluid for cementing job Drilling mud

    Lithology basis for rock properties Sandstone, sandy limestone

    Formation properties Derived by FracProPT curve-matching from mini-frac analysis of

    previous well. Will be updated with sonic logs as the well is

    drilled.

    Maximum casing test pressure profile 18.3-lb/gal OBM plus 15,000-psi surface pressure

    Parameters assumed for early

    production test

    5 MMscf/d, 40 BWPD, 72 hr, maximum drawdown to 2,500 psi

    at perfs, 0 psi on annulus, minimal drawdown in formation

    Frac treatment average parameters Through casing with 3,580 bbl fluid at 35 bbl/min, 13,000-psi

    surface pressure

    Post-frac flowback production 15 MMscf/d and 300 BWPD for 72 hr

    Long-term production 15 MMscf/day and 200 BWPD

    Table 1Initial Modeling Assumptions, 5-in. Production Casing

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    Original Second-Generation

    Well Design Completion Procedures

    Proposed Third-Generation

    Well Design Completion Procedures

    1. Displace cement job with drilling mud.

    2. No specifications on when continued operations

    are allowed.3. Pressure test casing and wellhead to 15,000 psi.

    4. RIH with workstring and scrapper and circulate

    out with KCl water.

    5. Perforate and perform production testing to

    maximum drawdown possible.

    6. Perform fracturing treatment down casing,

    20 bbl/min and 14,000-psi surface pressure.

    7. Forced-closure flowback and flow to tanks until

    cleaned up.

    8. Kill well, run tubing, and put on pipeline.

    1. Displace cement job with completion brine.

    2. WOC for minimum specified time to ensure

    mechanical property development.3. Run cement evaluation log.

    4. Pressure test casing and wellhead to 15,000 psi.

    5. RIH with workstring and circulate out with KCl

    water.

    6. Perforate and perform production testing.

    Maximum allowable drawdown of 5,500 psi at

    perforations.

    7. Perform fracturing treatment down casing,

    20 bbl/min and 14,000-psi surface pressure.

    8. Forced-closure flowback and flow to tanks until

    cleaned up.

    9. Kill well, run tubing, and put on pipeline.

    Final Procedures Used on First Well Procedures Used Today

    1. Displace cement job with 10 lb completion brine.

    2. WOC for minimum specified time to ensure

    mechanical property development.

    3. RIH with workstring and circulate out with 3%

    KCl water.

    4. Pressure test casing and wellhead to 15,000 psi.

    5. Run cement evaluation log.

    6. Perforate and perform production test. Maximum

    allowable drawdown of 2,500 psi at perforations.

    7. Perform fracturing treatment down casing;

    35 to 38 bbl/min at 14,500-psi pressure atsurface.

    8. Forced-closure flowback and flow to tanks until

    cleaned up.

    9. Kill well, run tubing, and put on pipeline.

    1. Displace cement job with 12.8 lb completion

    brine.

    2. WOC for minimum specified time to ensure

    mechanical property development.

    3. RIH with workstring and circulate out with 3%

    KCl water.

    4. Pressure test casing and wellhead to 15,000 psi.

    5. Run cement evaluation log.

    6. Perforate and perform fracturing treatment down

    casing; 35 to 38 bbl/min at 14,500-psi pressure

    at surface.7. Forced-closure flowback and flow to tanks until

    cleaned up.

    8. Kill well, run tubing (when applicable), and put on

    pipeline.

    Table 2Summary of Operational Changes Before Changing Cement Design

    Description Specific Gravity

    Initial sample caught at bulk plant 2.98

    4 in. from bottom of tank 2.91

    10 in. from bottom of tank 2.8614 in. from bottom of tank 2.89

    20 in. from bottom of tank 2.87

    25 in. from bottom of tank 2.91

    31 in. from bottom of tank 2.86

    41 in. from bottom of tank 2.97

    Maximum 2.97

    Minimum 2.86

    Average 2.90

    Standard Deviation 0.04

    Final sample caught from pneumatic line during mixing 2.97

    Samples Caught after Approximately 160 Miles

    Table 3Results of Deblending Check after 300 Miles of Travel

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    Final mud type (when interval is complete) 14 lb/gal WBM

    BHST 360oF (1.76

    F/100 ft)

    MD 16,500 ft

    TVD 16,500 ft

    Estimated drilled-hole size (from offset calipers) 13.25-in. (drilled with 12 1/4-in. bit)

    TOC 5,200 ft

    Assumed casing standoff 65%

    Displacement fluid for cementing job 14-lb/gal WBM

    Lithology basis for rock properties Sandstone, sandy limestone

    Maximum casing test pressure profile 14 lb/gal WBM plus 3,000-psi surface pressure

    Table 4Initial FEA Modeling Assumptions, 9 5/8-in. Casing

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    20-in., 133-lb K-55 BTC

    13 3/8-in. 68-lb HCK-55 BTC

    7-in. Tie-back string010,000 ft, 7-in. 41-lb HCQ-125

    Top of 7-in. liner

    9 5/8-in. 53.5-lb HCP-110 BTC

    Bossier "L"

    20,022 ft

    20,422 ft

    10,00014,381 ft,

    7-in. 41-lb HCQ-125 STL

    18,735 ft

    18,833 ft

    19,023 ft

    4 1/2-in. 18.80-lb Q-125 STL 20,940 ft

    2,901 ft

    14,910 ft

    TOC

    7,195 ft

    14,381 ft

    18,516 ftBossier "C"

    Bossier "K"

    Top of 4 1/2-in. liner packer

    Bossier "D"

    7-in. 41-lb Q-125

    Fig. 1Original well design.

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    Fig. 3Thermal simulator results for cementing operation.

    Fig. 4Thermal simulator results, post-cementing thermal recovery.

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    Depth

    Surface Casing F MW FIT

    24 3/4-in. Wall conductor 70 8.4 10.0

    1,000

    WBM

    2,000

    3,000 16-in., 84-lb J/K-55 BTC 131 9.5

    8.3 11.0

    4,000

    5,000

    2 7/8-in., 8.7-lb Tubing

    9.5

    6,000

    WBM

    14.5 lb/gal Inhibited packer fluid

    7,000

    8,000

    9,000

    10,000

    258 10.0

    9.5 14.0

    11,000

    12,000

    WBM

    13,000

    14,000

    13.5

    315 14.5 18.5

    15,000

    OBM

    16,000

    18.0

    18.0 19.5

    17,000

    OBM

    18,000 5-in. Production casing

    0-6,000 ft, 23.2-lb C-110

    6,00019,000 ft, 23.2-lb P-110

    19,000 408 18.5 107/115

    64

    82

    75

    6 1/2-in.

    10 5/8-in.

    0

    4

    6

    23

    14 3/4-in.

    Bits

    22-in.

    Days

    7 5/8-in., 39-lb P-110 liner

    8 1/2-in.

    12

    56

    11 7/8-in., 71.8-lb TCA-140 and Q-125

    9 5/8-in., 53.5-lb Q-125 liner

    28

    Fig. 7Final well design.

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    Fig. 8Design limit plot of new HTHP casing design.

    Fig. 9Remaining capacities, new casing and completion loads with conventional cement design. Risk of damageover load phases; depth along well=18,000 ft; cement material=19.0-lb/gal conventional Class H cement.

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    Fig. 10New casing and optimum completion plan with conventional cement. Risk of damage over load phases; depth alongwell=18,000 ft; cement material=19.0-lb/gal conventional Class H cement.

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    Fig. 11Remaining capacity summary, final HTHP casing and cement sheath design. Risk of damage over load phases;depth along well=18,000 ft; cement material=19-lb/gal elastic system.

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    Fig. 12Elastic cement after pressure cycling.

    Fig. 13Conventional cement after cycling.

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    Fig. 14Remaining capacities and plastic deformation; original lead cement at 10,500 ft. Risk of damage over load phases; depth alongwell=10,550 ft; cement material=12.7-lb/gal water-extended cement.

    Fig. 15Remaining capacities and plastic deformation; original tail cement at 16,500 ft. Risk of damage over load phases; depth alongwell=16,500 ft; cement material=16.4-lb/gal conventional cement.

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    Fig. 16Remaining capacities of new lead cement design for 9 5/8-in. casing at 16,500 ft. Risk of damage overload phases; depth along well=10,550 ft; cement material=13.2-lb/gal Class H cement and pozzolan blend.

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    Fig. 17 Remaining capacities of tail cement for 9 5/8-in. casing at 16,500 ft. Risk of damage over load phases;depth along well=16,500 ft; cement material=16.4-lb/gal Class H nonshrinking cement.

    Fig. 18FYSA adapter kit for rotational rheometer.

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    Fig. 19Regression analysis of YPA data.

    Fig. 20 Job placement summary.

    SpacerLeadSlurry

    TailSlurry

    Displacement

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    Fig. 21CBL of elastomeric tail slurry after 15,000-psi casing pressure test.

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