performance 20072008
TRANSCRIPT
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7/28/2019 Performance 20072008
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April 2007
Successfully provided Mud Services in Drilling/ Production testing of wells SKFH, KLOY, KLCC
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KLOY DI L CW-IV 4/4/2007
26/4/2007
30/4/2007
01643
1643
Spudded the Well, Kicked off the
Well at 200m drilled to 305m..
Lowered & cemented 9 Casing.Further drilled down to 1640m.
Made a S/T of 35 stands. HDIL-SP-
GR logging tool did not go beyond
1582m.Recorded from 1582 to300m. Made R/T and conditioned the
hole but Logging tool did not gobeyond 1538m. R/I bit and observed
held up at 1538m. While reaming,String got stuck at 1623m and
released the same with circulation,
and reamed to bottom. Further,
recorded CDL-CNT-Cal-GR and
HRI-SP-GR Logs from 1643 to
1300m. Conditioned the hole andlowered 5 Prodn. Csg. to
1633.49m(F/C, 610.71m). WOC.
Scrapped the Well, recorded CBL-VDL-CCL-GR Log (1603 to
1175m). Found good Cement
Bondage with Cement rise up to
1210m. HT at 250 ksc in water ok.
Perforated the object I. AppliedCompressor to 120ksc. Only Water
flowed. Carried out Reverse wash
with Water. 300 Liters Oil surfaced.
Found Injectivity 260lpm @ 120ksc.
Applied N2 to 140 ksc. 0 to 100 ksc,
initially 50itres of Oil followed by
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Rig: CW- IVWell :KLOY, Type/ Profile: DI L, Drilled Interval: 0 1643m, Meterage Drilled : 1643m
Activity: Spudded the Well with 12 bit. Kicked off the Well at 200m drilled to 305m. Conditioned the hole. Lowered & cemented 9 Casing.
IWH, IBOP and drilled F/C, Cement, Csg Shoe and formation to 1640m. Made a S/T of 35 stands. HDIL-SP-GR logging tool did not go beyond1582m.Recorded from 1582 to 300m. Made R/T and conditioned the hole but Logging tool did not go beyond 1538m. R/I bit and observed held up at 1538m.
While reaming, String got stuck at 1623m and released the same with circulation, and reamed to bottom. Further, recorded CDL-CNT-Cal-GR and HRI-SP-GRLogs from 1643 to 1300m. Conditioned the hole and lowered 5 Prodn. Csg. to 1633.49m(F/C, 610.71m). WOC. Scrapped the Well, recorded CBL-VDL-
CCL-GR Log (1603 to 1175m).HT at 250 ksc in water ok.
Perforated the object I in 1.05 NaCl brine.Applied Compressor to 120ksc. Only Water flowed.Reverse wash with Water. 300 Liters Oil surfaced. Found
Injectivity 260lpm @ 120ksc. Applied N2 to 140 ksc. 0 to 100 ksc, initially 50itres of Oil followed by water and 100 to 140ksc Water along with traces of Oil
flowed. Carried out BHS and Rig released.
Mud Parameters:Drilled Interval Sp.Gr Visco
sity
Gel10 Fluid
Loss
San
d
pH PV YP Gel 0/10 Solid
m Sec,API
sec Cc,API
%,v/v
CPS Lbs/100 sq.ft
Lbs/100 sq.ft
%, v/v
0-300 GTO 1.05-1.10 37-42 47-52 NC
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DEVIATION DATA
Well KLOY : Inclined LProfile (KOP: 200m, Hole 12 - 0 - 305m & 8 -305 -1643m MD)
DD(m) Angle, o Azimuth, o
0 0 0.00
200 0 0.00206 1.50 16.00
215 3.00 24.00
225 4.00 17.00
234 6.00 9.00
271 8.50 3.00
316 9.50 358.00
364 10.00 355.00
412 10.50 355.00
470 11.50 355.00
560 13.5 357.00
600 17.00 358.00
640 17.00 359.00670 15.75 1.00
698 15.00 1.00
745 13.50 1.00
773 13.00 1.00
802 1300 5.00
830 13.75 7.00
869 13.50 10.00
913 13.25 10.00
953 13.00 11.00
991 12.50 13.00
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1039 13.00 15.00
1120 13.00 18.00
1255 13.00 26.00
1350 13.50 32.00
1500 13.00 37.00
1577 13.00 37.00
1579.2 13.00 37.00
Rig: R-IIWell: SKFH, Type / Profile:D , Drilled Interval ; 0-1777 mts Meterage Drilled :1777 mts
Activity: During lowering of 9 5/8 casing at the depth of 1248 m approx. ,observed no mud return ,decieded to establish circulation but in vain. Lowered
three more singles of casing pipe & try to establish circulation ,no success. P/O the casing up to the depth 1100m approx.& resumed circulation. Circulationestablished, resumed lowering of casing after gel breaking at the interval of 200m till bottom.
Mud Parameters:
Drilled Interval Sp.Gr Viscosity Gel10 Fluid
Loss
Sand pH Pv Yp Solid
0-302 GTO 1.05-1.15
37-42 47-52 N/C< 2%
9.0-9.5
- - -
Actual 1.05-
1.08
37-40 47-50 N/C 1 9.0 - - -
300-
700
GTO 1.10-
1.15
35-40 45-50 N/C-12 1 9.0-
9.5
- - -
Actual 1.06-
1.09
38-40 48-50 N/C 1 9.0-
9.5
700-
1200
GTO 1.15-
1.20
37-42 47-52 12-6 1 9.0-
9.5
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Actual 1.10-
1.20
39-42 49-52 12-7.6
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May2007
Successfully provided Mud Services in Drilling/ Production testing of wells SKFH,
KLXC EV CW-IV 06.05.07
25.05.07
0
1491
1491
Spudded the well.D/D 306 m.Lowered
& Cemented 9 5/8 casing.Further
drilled down to 1382 m. Cut core of
1382-1390 m .Further drilled down to
1487 m. Recorded logs.Lowered &
cemented 5 casing. Recorded
CBL-VDL logs.Tested casingharmatically. Placed brine cushion of
200 m & perforated Obj.I 1435-1425
m. Displaced well fluid with water.
Applied nitrogen twice. Observed flow
of water with traces of oil. Carried out
HF job. Applied compressor obs. Littleflow. PA PT nil.
Rig : CW-IVWell: KLXC , Type / Profile: EV, Drilled Interval : 00-1491 , Meterage drilled: 1491 m
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Activity: Spudded in the well.D/D to 306 m. Lowered and cemented 9 5/8 casing. After IWH and IBOP D/D with 8 1/2 bit to 315 m. Carried out
LOT. LOT value 1.71 MWE. D/D to 1382 m. Cut core from 1382 to 1390 m , D/D to 1396 m. Cut a core from 1396 to 1403 m. D/D to 1487 m.
Recorded logs. Lowered and cemented 5 casing.
After IWH and IBOP scrapped the well. Recorded CBL-VDL-GR logs. Recorded zero effect survey from 1440 to 100 m by VSP party. Tested
casing hermetically at 250 KSC. Placed a brine cushion of 200 m Perforated Object I (1435-1425 m , K-X ). Applied Nitrogen up to 100 KSC. Observed
0-60 KSC flow of water, 60-100 KSC flow of water with oil traces.Released nitrogen. WUO. PA,PT- Nil. Applied nitrogen up to 130 KSC. 0-100 KSC noflow, 100 liter oil surfaced, 100-130KSC flow of water with oil traces. Nitrogen cut at 130 KSC. Released nitrogen. WUO. No flow. PA,PT nil. Carried
out BHS. Injectivity 130 lpm at 130 KSC. Carried out HF job. Observed flow of chemical water with oil traces. PA,PT nil. Applied compressor up
to 110 KSC. Observed flow of water + oil traces + little gas. WUO.PA,PT- nil.
Mud Parameters:
Drilled Interval
m
Sp.Gr Viscosity Gel10 Fluid
Loss
Sand pH Pv Yp Solid
00-
300
GTO 1.05-1.10 38-42 48-52 NC
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1.25+ 17 18 14
SKFH DS R-II 06-04-2007
12-05-0715-05-2007
1777
2090313
Drilled successfully to it s target depth
without any problem .
CL-CLS
System
Rig: Rum-II
Well: SKFH Type/ Profile:D , Drilled Interval :1777-2090m Meterage Drilled :313m
Activity: Drilled successfully to its target depth without any problem and saved 7 drilling days.
Mud Parameters:
Drilled Interval Sp.Gr Viscosity Gel10 Fluid
Loss
Sand pH Pv Yp Solid
1777-
2090
GTO 1.65-
1.70*
42-47 52-57 6-5
< 1%
9.0-9.5 - - -
Actual 1.65-
1.75
39-46 49-56 6-5
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June2007
WDAQ EV R-II 22/5/2007 12772616
1339
Drilling CL-CLSSystem
Rig: Rum-IIWell: WDAQ, Type/ Profile:EV, Drilled Interval :1277-2618 m, Meterage Drilled : 1339 m
Activity: Drilling.
Mud Parameters:
Drilled Interval Sp.Gr Viscosity Gel10 FluidLoss
Sand pH Pv Yp Solid
100-1500 GTO 1.20-1.30 40-42 50-52 10-7 1 9.0-
9.5
ACTUA
L
1.14-1.34 40-41 50-51 8.0-5.2 1 9.0-
9.5
18 16 12-
18
1500-1750
GTO 1.30-1.40 42-44 52-54 7-6 1 9.0-9.5
ACTUA
L
1.40-1.37 40-42 50-52 5.2-5.0 1 9.5 15-
16
16-
18
18
1750-2800
GTO 1.55-1.57 42-45 52-55 6.0 1 9.0-9.5
1755-
2125
ACTUA
L
1.55-1.57 40-46 50-56 5-4.8 1 9.5 17-
15
13-
16
19-
22
2125-
2616
ACTUA
L
1.57-1.64 43-44 53-54 4.8-4.0 1 9.5 17-
24
16-
28
22-
24
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July2007
HIGHLIHGTS: WDAQ-First deepest well in Wadu area drilled with target depth 2800m without any problem .After logging tested Object-I ( 1801-1899m - Wadu sand ) .A 100m cement plug (2020-1920m ) was placed to isolate the zone before lowering 5 casing with 1801-1899m slotted casing. For
testing of Object-I conventionally 200m water cushion was placed & displaced with 5.5m3 mud of sp.gr1.65.During p/o 2 7/8 singles well became active ,
SIDPP & SICPP was recorded 1000 psi with mud wt. 1.65.Well was circulated with 6mm bean at 15spm in absence of adjustable choke & thus lost approx.
35m3 mud. Later on well was circulated through adjustable choke using mud wt. 1.63 & recorded shut in pressure 600 psi. Well was killed with 1.75 mud wt.
On observation shut in pressure recorded 100 psi , hence decided to kill the well with mud wt. 1.78.Well was killed with mud wt. 1.78 & further testing carried
on smoothly.
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WDA
Q
EV R-II 22/5/2007
21/7/2007
2616
2801
185
Drilling CL-CLS
System
Well: WDAQ, TYPE / Profile :EV, Drilled Interval : 2616- 2801 m, Meterage Drilled :185 m
Activity: Drilled down from 2616 m to 2801 m without any problem .After logging tested Object-I interval 1801-1899m ( Wadu sand ) .A 100m cement plug(2020-1920m ) was placed to isolate the zone before lowering 5 casing with 1801-1899m slotted casing. For testing of Object-I conventionally 200m water
cushion was placed & displaced with 5.5m3 mud of sp.gr1.65.During p/o 2 7/8 singles well became active, SIDPP & SICPP was recorded 1000 psi with mudwt. 1.65.Well was circulated with 6mm bean at 15 spm in absence of adjustable choke & thus lost approx. 35m3 mud. Well was circulated through adjustable
choke using mud wt. 1.63 & recorded shut in pressure 600 psi. Well was killed with 1.75 mud wt. On observation shut in pressure recorded 100 psi , hence
decieded to kill the well with mud wt. 1.78.Well was killed with mud wt. 1.78 Further testing carried on smoothly.
Drilled Interval Sp.Gr Viscosity
Gel10 FluidLoss
Sand pH Pv Yp Solid
2125-
2616
ACTU
AL
1.57-1.64 43-44 53-54 4.8-
4.0
1 9.5 17-
24
16-
28
22-
24
2616-
2800
GTO 1.55-1.57 42-45 52-55 6 1 9.5 - - -
2616-
2801
ACTU
AL
1.64+-1.70 42-45 52-55 4.0-
4.8