polyvoid case study0104.nccdn.net/1_5/219/1c8/0d4/case-study-presentation--1-.pdf · polyvoid case...

16
PolyVoid Case Study Gunnedah NSW

Upload: others

Post on 05-Jun-2020

2 views

Category:

Documents


0 download

TRANSCRIPT

Page 1: PolyVoid Case Study0104.nccdn.net/1_5/219/1c8/0d4/Case-Study-Presentation--1-.pdf · PolyVoid Case Study Gunnedah NSW. PolyVoid Slab Under ... ¥ Stage 2 was the excessive moisture

PolyVoid Case Study

Gunnedah NSW

Page 2: PolyVoid Case Study0104.nccdn.net/1_5/219/1c8/0d4/Case-Study-Presentation--1-.pdf · PolyVoid Case Study Gunnedah NSW. PolyVoid Slab Under ... ¥ Stage 2 was the excessive moisture

PolyVoid Slab Under“Abnormal Moisture”

Conditions

Page 3: PolyVoid Case Study0104.nccdn.net/1_5/219/1c8/0d4/Case-Study-Presentation--1-.pdf · PolyVoid Case Study Gunnedah NSW. PolyVoid Slab Under ... ¥ Stage 2 was the excessive moisture

The Customer’s Concern

• Client contacted Builder claiming the slab had sunk under his en-suite

• 3 hairline cracks were around the doorway from bedroom to en-suite, and en-suite to wardrobe

• The fall of the non-screened shower had changed and water was falling away from the waste slightly

Page 4: PolyVoid Case Study0104.nccdn.net/1_5/219/1c8/0d4/Case-Study-Presentation--1-.pdf · PolyVoid Case Study Gunnedah NSW. PolyVoid Slab Under ... ¥ Stage 2 was the excessive moisture

It Started With This

‘Pooling’ Capability

Created with Paving Edge

Drains All Covered Up

Half of the Pot Plants had been

removed at this stage

A Tap Was Leaking

Continuously next to a

lightweight Section of the

House

En-Suite

No drainage behind DIY retaining

wall

Page 5: PolyVoid Case Study0104.nccdn.net/1_5/219/1c8/0d4/Case-Study-Presentation--1-.pdf · PolyVoid Case Study Gunnedah NSW. PolyVoid Slab Under ... ¥ Stage 2 was the excessive moisture

What We Knew About the Soil

• The site tested as having a Ys of 100-120mm• It had rained for a month prior to construction of the slab and the soil was considered to be at 40-50% saturated• This was one of the first PolyVoid Slabs in NSW and therefore the practice of connecting the edge piles was not carried out• Only the soil around this particular wall was wet. In all other areas of the house perimeter, the soil was dry

Page 6: PolyVoid Case Study0104.nccdn.net/1_5/219/1c8/0d4/Case-Study-Presentation--1-.pdf · PolyVoid Case Study Gunnedah NSW. PolyVoid Slab Under ... ¥ Stage 2 was the excessive moisture

The Soil’s Reaction

Page 7: PolyVoid Case Study0104.nccdn.net/1_5/219/1c8/0d4/Case-Study-Presentation--1-.pdf · PolyVoid Case Study Gunnedah NSW. PolyVoid Slab Under ... ¥ Stage 2 was the excessive moisture

The Soil’s Reaction

Edge-Beam Voids

Compressing under Heave

Force

Soil had not swollen as much at the perimeter. There was still space under the edge-voids

Page 8: PolyVoid Case Study0104.nccdn.net/1_5/219/1c8/0d4/Case-Study-Presentation--1-.pdf · PolyVoid Case Study Gunnedah NSW. PolyVoid Slab Under ... ¥ Stage 2 was the excessive moisture

The Soil’s Reaction

Plastic Membrane

225mm PolyVoid

‘Heaved’ Soil

Page 9: PolyVoid Case Study0104.nccdn.net/1_5/219/1c8/0d4/Case-Study-Presentation--1-.pdf · PolyVoid Case Study Gunnedah NSW. PolyVoid Slab Under ... ¥ Stage 2 was the excessive moisture

The Soil’s Reaction

An estimated total of

200-210mm of heave has occurred

Page 10: PolyVoid Case Study0104.nccdn.net/1_5/219/1c8/0d4/Case-Study-Presentation--1-.pdf · PolyVoid Case Study Gunnedah NSW. PolyVoid Slab Under ... ¥ Stage 2 was the excessive moisture

Root Cause Determination

• After many inspections and assessment by structural and geotechnical engineers, it was determined that there had been a two-stage effect on the slab• Stage 1 was that the daily watering of the many pot plants, leaking tap, and lack of proper drainage had created the initial stages of heave• The Stage 1 level of movement caused the plumbing to fail under the en-suite as the proper expandable joiners were not used• Stage 2 was the excessive moisture forced under the slab from the shower waste as the plumbing was not working

Page 11: PolyVoid Case Study0104.nccdn.net/1_5/219/1c8/0d4/Case-Study-Presentation--1-.pdf · PolyVoid Case Study Gunnedah NSW. PolyVoid Slab Under ... ¥ Stage 2 was the excessive moisture

The Soil’s Reaction

The fully suspended slab allowed the plumber to get in and replace the pipes and joiners

Page 12: PolyVoid Case Study0104.nccdn.net/1_5/219/1c8/0d4/Case-Study-Presentation--1-.pdf · PolyVoid Case Study Gunnedah NSW. PolyVoid Slab Under ... ¥ Stage 2 was the excessive moisture

The Soil’s Reaction

The fully suspended slab allowed the plumber to get in and replace the pipes and joiners

Page 13: PolyVoid Case Study0104.nccdn.net/1_5/219/1c8/0d4/Case-Study-Presentation--1-.pdf · PolyVoid Case Study Gunnedah NSW. PolyVoid Slab Under ... ¥ Stage 2 was the excessive moisture

The End Result• The plumbing was repaired using the appropriate joiners etc• The soil was removed from the underside of the slab and left to dry for a period of time• The slab settled back down the 50mm onto the piers• All of the cracks closed up and the shower is now falling properly directly into the waste• Further investigation has revealed an unidentified source of subsoil water, and a storm water run-off issue at the back of the property. The council is now involved

Page 14: PolyVoid Case Study0104.nccdn.net/1_5/219/1c8/0d4/Case-Study-Presentation--1-.pdf · PolyVoid Case Study Gunnedah NSW. PolyVoid Slab Under ... ¥ Stage 2 was the excessive moisture

Key design changes

Page 15: PolyVoid Case Study0104.nccdn.net/1_5/219/1c8/0d4/Case-Study-Presentation--1-.pdf · PolyVoid Case Study Gunnedah NSW. PolyVoid Slab Under ... ¥ Stage 2 was the excessive moisture

PolyVoid Slabs for Reactive Soils

Screw Piles arenow connectedinto the slab

Page 16: PolyVoid Case Study0104.nccdn.net/1_5/219/1c8/0d4/Case-Study-Presentation--1-.pdf · PolyVoid Case Study Gunnedah NSW. PolyVoid Slab Under ... ¥ Stage 2 was the excessive moisture

Key Design Changes• After years of research, testing and number crunching, The Katana Void Slab Manual has been published• The concrete member calculations in this design manual has been given third party certification by a leading Australian engineering firm• Extensive testing on the new slab design proved the slab’s capability in soils with a Ys of up to 140mm• All Katana documentation is available for structural engineers on a specifically issued USB stick