replacement of a 22 years old secondary reformer - gpic's .../fileser… · process licensor...
TRANSCRIPT
Page 1
Replacement of a 22 years old Secondary Reformer - GPIC’s
experience This paper discusses the reason for replacing a 22 years old Secondary Reformer, the improvements
that were made in the new Secondary Reformer, the proactive measures that were taken for
successful replacement and the actual operational performance after replacement.
Samih Al Alawi and Cholaperumal Subramanian
Gulf Petrochemical Industries Company, Kingdom of Bahrain
K. Schmalstieg and M. Wolske
KARRENA GmbH, Germany
1.0 Introduction
ulf Petrochemical Industries Co.
(GPIC), Bahrain was established in
1979 as a joint venture with equal
participation by Government of Bahrain,
Petrochemical Industries Company (PIC)
Kuwait and Saudi Basic Industries Company
(SABIC) Saudi Arabia. GPIC is a fine example
of a successful joint venture between Arab Gulf
companies in the Arabian Gulf.
GPIC operates a complex comprising of single
stream Ammonia and Methanol Plants, each of a
capacity of 1200 MTPD and a single stream of
1700 MTPD Urea Plant (Granulation route)
along with associated utilities, off-site and
material handling units. The Ammonia and
Methanol Plants are in operation since 1985
while the Urea Plant was commissioned in
January 1998 and is in operation since then.
Process licensor for Ammonia and Methanol
plants is Uhde GmbH, Germany and the process
licensor for Urea Plant is Snamprogetti, Italy. In
just over two decades GPIC has grown to
become a major petrochemical venture. It has
earned a reputation for reliability, quality,
safety, health and care for the environment on an
international scale. Its achievement in terms of
plant reliability is spectacular and proven by
many benchmarking studies with similar plants
throughout the world. The company has earned
an outstanding reputation not only within the
region but in the international arena too, for its
continuous on stream record of 738 days, 941
days and 931 days of Ammonia, Urea and
Methanol plants respectively. The Company
remains fully committed to complying with, and
wherever possible, exceeding all national and
international safety and health laws and
regulations. GPIC continues to place a top
priority on its excellent management of safety,
health and environment. The many awards
received from highly recognized international
institutions are a proof of this commitment.
The Ammonia Process is a conventional steam
reforming process for synthesis gas generation
and an axial bed converter for ammonia
G
187 AMMONIA TECHNICAL MANUAL2008
synthesis followed by the ammonia recovery
step.
One of the most critical equipment items in an
Ammonia Plant is the Secondary Reformer.
During the turnaround of the Plant in November
2007, GPIC replaced the 22-year-old Secondary
Reformer with the new one with improved
design features.
2.0 Design features of the old Secondary Reformer.
The Secondary Reformer is a standard Uhde
design where the process gas enters from the
bottom through the central riser and mixes with
the hot air introduced through a ring shaped
burner and the combustion takes place. The gas
then flows through the catalyst bed axially and
exits the Secondary Reformer from where it is
routed to the Process Gas Cooler. The detail of
the old Secondary Reformer arrangement is
provided in Figure 1. The pressure shell of the
Secondary Reformer is lined internally with
refractory lining. The design temperature of the
hot face of the refractory lining above the
catalyst bed is 1800 oC (3272
oF). The pressure
shell is designed for 150 oC (302
oF). In order to
keep the pressure shell within its design
temperature, the external surface of the
complete vessel is provided with a non-
pressurised water jacket. The hot face lining of
the combustion zone (inner layer) in contact
with the hot gasses is of high alumina type
bricks and the outer insulating layer is of high
silica based refractory concrete. (Figure 2)
2.1 Observations made during Refractory inspection in 2005 turnaround
The most effective check of the refractory lining
is possible only during shut downs when
inspections enable the evaluation of the
conditions of the hot face skin.
During the regular shut down of the plant in
2005 an inspection of the Secondary Reformer
lining was done at the dome area and the
cylinder wall above the catalyst bed. The
following observations were made.
• The brick lining of the dome and first part of
the cylindrical wall area was so far in
acceptable condition taking into
consideration the operation time of 20 years.
(Picture 1)
Picture 1: Brick lining of dome after 20 years
Picture 2: Brick lining above catalyst bed
• Several larger cracks that were filled up with
a mixture of Saffil fibre and mortar during
the previous shutdowns were observed to be
in a satisfactory condition. (Picture 2).
• The mortar joints and the brick shapes had
eroded strongly due to the hot process gas.
188AMMONIA TECHNICAL MANUAL 2008
The hot face of the bricks was glazy caused
by the advanced operation time period and
the hot process gas. The mortar at the joint
was also observed to be partly eroded.
(Picture 3).
Picture 3: Cracks and eroded joints
• The expansion gaps at the expansion joints
were found to have increased and might not
close completely during operation.
Furthermore they must be cleaned to allow
for free expansion before next heating up
(Picture 4).
Picture 4: The expansion joint is extended
The refractory lining of the dome and upper
cylindrical part seemed to limit seriously the
lifetime of the lining. Due to the joint conditions
a potential risk for gas bypassing could not be
excluded. This may cause higher temperatures
of the steel shell, which will not be immediately
obvious because of the water jacket.
2.2 Merits and Demerits of Silica based Refractory:
Silica based refractory material has good
insulating property. Hence the former designs of
Secondary Reformer refractory lining were
based on using insulating products containing
Silica. The refractory lining of the old
Secondary Reformer was designed for a skin
temperature of 170 oC (338 oF) at the pressure
shell (without water jacket).
However, it is now well known that Hydrogen
rich process gas considerably affects Silica at
higher temperatures in reducing atmospheres.
Hydrogen can remove Silica as per the
following chemical reaction:
SiO2 (solid) + H2 (gas) ����SiO (gas) + H2O (gas)
This chemical reaction depends on the process
gas temperature and pressure.
If condensation of gaseous SiO will take place
later in the process, fouling at downstream heat
exchanger tubes could be a typical result of this
chemical reaction.
GPIC had observed voids behind the hot face
refractory brick lining in the shutdowns prior to
2005. GPIC had also been experiencing fouling
phenomenon of the downstream Process Gas
Cooler due to silica migration from the
refractory lining corroborating with the above
theory.
Based on the above findings, GPIC decided to
change the refractory lining of the Secondary
Reformer. Uhde recommended to change the
refractory from silica based to alumina-based
refractory to overcome the refractory
deterioration due to silica migration, as has been
carried out in the Secondary Reformer of the
recent Uhde Ammonia Plants.
189 AMMONIA TECHNICAL MANUAL2008
3.0 Reason for GPIC to replace the entire equipment
Two options towards replacement of the
refractory lining were considered and evaluated.
• Replacement of the whole refractory during
a turnaround:
The cost of this option will be low.
However, it would have required a 50 days
plant outage for the repair works, costing in
terms of lost production.
• Replacement of the Secondary Reformer
during a turnaround:
GPIC would have to incur cost of new
equipment, but the number of days required
for restoring production would reduce, thus
minimizing the costs in terms of lost
production.
This option also offered an opportunity to take
advantage of the latest design improvements in
the Secondary Reformer technology.
Cost incurred in the replacement of the
refractory during Turnaround and the lost
revenue in terms of production (Option 1) was
Figure 1: New Secondary Reformer with air ring header and air inlet
nozzles arrangement. Old Secondary Reformer with air ring burner
arrangement.
New Secondary
Reformer
Old Secondary
Reformer
Catalyst
Bed
Gas Outlet
Gas
Inlet
Combustion
Zone
Water
Jacket
Air Nozzle with
ring header
outside
Air ring
burner inside
Gas Outlet
190AMMONIA TECHNICAL MANUAL 2008
estimated to be USD 25.3 million. Cost of
procurement of the new Secondary Reformer
and its installation during Turnaround (Option
2) was estimated as USD 15.1 million. Option 2
was found to be a competitive choice. A
conscious decision was taken to pursue Option 2
(i.e. procurement of a new Secondary
Reformer).
4.0 Design features of the new Secondary Reformer & Refractory
Basic Engineering and procurement
specification for the new Secondary Reformer
was provided by Uhde. Uhde also provided their
services for approval of the vendor's drawings &
documents, inspection during fabrication of the
equipment and during erection of the equipment
at site.
4.1 Features of new Secondary Reformer (Steel)
In the new Secondary Reformer design, the
internal ring burner is removed and instead a
ring shaped air header is provided on the outside
of the vessel. The inlet air then passes through
the flexible pigtails and is released at high
velocity into the Secondary Reformer through
the nozzles oriented at an angle. The angular
orientation of the nozzles creates a vortex flow,
which enables better mixing of gas and air and
also prevents the flames to come in contact with
the central riser pipe or the refractory on the
shell. The height of the combustion zone has
been increased in the new Secondary Reformer
in order to have sufficient residence time to
achieve uniform temperature before entry into
the catalyst bed. Due to this the height of the
new Secondary Reformer is 16.8 metres (55.12
ft) which is 2.35 metres (7.71 ft) more than the
old one. The details of the new Secondary
reformer arrangement are provided in Figure 1.
The main advantages of the new design are
• better mixing of gas and air by creating a
vortex flow (lower methane slip)
• sufficient residence time to achieve a
uniform temperature before the gas enters
the catalyst bed.
• avoidance of flame impingement on the
refractory or catalyst
• no metallic burner in the combustion zone
(no replacement of the burner ring
required)
The weight of the new Secondary Reformer
steel is 120 tons, which is 30 tons more than the
old one. The operating weight of the new
Secondary Reformer is 371 tons as compared to
the operating weight of 295 tons for the Old
Secondary Reformer. The ex-works delivery of
the Secondary Reformer was 14 months from
the date of Purchase Order. The equipment was
received at site 15 months after Purchase Order
date.
4.2 Features of Refractory of new Secondary Reformer
The basic concept for the refractory design of
the new Secondary Reformer is Silica free lining
and installation of the refractory under hot
climate conditions in Bahrain. Bubble alumina
is used as back-up lining in the new design
instead of silica based lining. The Silica free
refractory lining will reduce the potential risk
for fouling in heat exchanger tubes of
downstream Process Gas Cooler due to
condensation of gaseous SiO. Since the
insulation properties of bubble alumina are not
as good as the silica-based material, the heat
transferred to the water jacket will rise. The
refractory lining of the new Secondary Reformer
is designed for a skin temperature of 260 oC
(500 o
F) at the pressure shell (without water
jacket) as against 170 oC (338
oF) for the old
one.
191 AMMONIA TECHNICAL MANUAL2008
The installation, which was scheduled in
Bahrain under hot climate conditions, is the
reason to use Bubble Alumina pre cast shapes in
the second layer of Secondary Reformer lining
instead of casting both insulation layers. The
benefits of using pre cast shapes are:
� Less water in the refractory lining and
therefore safer dry out.
� Less working period with castable
which is of particular importance under
hot climate conditions
New Secondary Reformer
Modern Refractory design
Figure 2: Secondary Reformer of different designs
� The time period for installation will be
reduced.
� More economical because of avoiding
solid steel shuttering.
The details of new refractory design of
secondary reformer compared to the former one
together with main characteristics of the
refractory materials are provided in Figure 2 and
Table 1.
Old Secondary Reformer
Former refractory design
Bubble Alumina
shapes
High Alumina
Refractory Bricks
Bubble Alumina
shapes
Bubble Alumina
Insulating Layer
Insulating Firebrick
ASTM-Group 23
Insulating Layer with
approx. 30% SiO2
Synthesis gas
flow
High Alumina Castable
192AMMONIA TECHNICAL MANUAL 2008
5.0 Planning of Replacement
The Secondary Reformer replacement site
activities had to undergo careful planning
because of the criticality and complexity
associated with it. The planning for the
replacement activities at site started at the same
time the Specification for the new Secondary
Reformer was finalized. Extensive consultations
were held with Uhde, Karrena and the erection
contractor for execution of the project in a safe
manner and in the shortest possible time.
The new Secondary Reformer was supplied by
the vendor with the water jacket and the air inlet
ring header pre-installed in the vendor
workshop. To prevent any damage to the air
inlet pigtails during transport, the pigtail
connection between the air inlet header and the
inlet nozzles were carried out at site before the
shutdown.
To reduce the activities and time during the
plant shutdown, it was decided to carryout
installation of the refractory lining and dry out
of the lining prior to the start of the plant
shutdown. In order to reduce the lifting and
shifting activities of the new Secondary
Reformer after installation of the refractory
lining, the new equipment was erected on a
temporary foundation closer to the existing
Secondary Reformer (19.35 metres [63.48 ft]
from the existing reformer) (Picture 5 and
Picture 7).
The following activities carried out on a
proactive basis helped in the smooth execution
of the replacement work.
a. Based on the technical specification for
the new Secondary Reformer prepared by Uhde,
increase in weight of the new Secondary
Reformer due to the increased height was
envisaged. The maximum load bearing capacity
of the existing foundation was checked and
calculated prior to floating of enquiry. Vendors
were informed of this foundation load capacity
limitation during the enquiry stage itself thereby
ensuring the weight of the new equipment to be
within the load capacity limit of the foundation.
b. The new Secondary Reformer had to be
erected on the existing foundation bolts and
connected to the existing inlet and outlet
connection on the gas side. Hence it is of utmost
important that the bolt circle diameter of the
base ring bolt holes, base bolt hole pitch,
Description UOM
Karrena material no. 2037 5016 2037 4006 4001 5206
Product description
High Alumina
brick
High Alumina
shapes or castableHigh Alumina brick
Bubble Alumina
brick
Insulating fire brick
ASTM Group 23
Insulating castable
layer
Main raw material
Fused
CorundumBubble Alumina Fused Corundum Bubble Alumina Fireclay
Light weight
aggregates
Max. service temperature °C (°F) 1600 (2912) 1800 (3272) 1600 (2912) 1700 (3092) 1150 (2102) 1250 (2282)
Chemical composition
AL2O3 %wt. 99 96 99 98.5 37 50
SiO2 %wt. 0.1 0.5 0.1 0.7 46 31
CaO %wt. 3 14 16
Fe2O3 %wt. 0.1 0.2 0.1 0.1 1 0.7
Bonding system ceramic hydraulic ceramic ceramic ceramic hydraulic
Apparent porosity % 16 48 16 64 82 45
Bulk density g/cm³ 3.32 1.55 3.32 1.45 0.55 1.1
CCS after heating at 110°C (230°F) Mpa (psi) 95 (13778) 10 (1450) 95 (13778) 8 (1160) 0.8 (116) 3 (435)
Thermal conductivity @ 400°C (752 °F) W/mK 7.5 1 7.5 17 0.15 0.24
Thermal conductivity @ 800°C (1472 °F) W/mK 4.5 0.8 4.5 1.3 0.21 0.3
Table 1 : Comparison of Refractory Material Properties of Old and New Secondary Reformer
New Secondary Reformer Old Secondary Reformer
193 AMMONIA TECHNICAL MANUAL2008
angular orientation of the base bolts, elevation
& angular orientation of the gas inlet and outlet
nozzles for the new Secondary Reformer are the
same as that of the existing Secondary Reformer
at site.
Picture 5: New Secondary Reformer as received
at site and ready for erection on temporary
foundation.
As-built dimension measurement of the old
Secondary Reformer was carried out before the
start of actual shop fabrication of the new one.
The as-built dimensions of the old Secondary
Reformer were checked with the aid of 'Total
Station' survey equipment. Dimensional
difference was noted in the bolt circle diameter
and the pitch of the base bolts from the
dimensions indicated on the drawing. The pitch
of the base bolts was observed to be not
uniform. These dimensions were incorporated
into the fabrication of the new Secondary
Reformer. The bolthole diameter of the base
plate of the new Secondary Reformer was
increased to accommodate the variation in the
base bolt pitch observed at site. This proactive
approach eliminated the problems that would
have been encountered if dimensional
corrections had not been incorporated in the new
equipment.
c. The air inlet piping of the new
Secondary Reformer had to be modified due to
the increased height of the new equipment and
also due to the change in design to air ring
header type. Uhde carried out stress analysis for
the modified piping arrangement. The existing
pipe supports and spring hangers of the air inlet
piping were observed to be adequate for the new
piping arrangement.
d. Experience of other plants with the Uhde
designed Secondary Reformer similar to our
new Secondary Reformer indicated higher jacket
water consumption due to the poor insulating
property of silica free type of refractory lining
and also due to the many air inlet nozzles cooled
by the jacket water. Hence the number of water
jacket vent pipes was increased from 2 to 4 to
handle the increased steam generated from the
water jacket. This will prevent the jacket water
from splashing out from the top seals of the
water jacket.
e. The Transfer Line (Gas outlet header)
from the Primary Reformer is welded to the gas
inlet nozzle of the Secondary Reformer. The
inside of the Transfer Line and the gas inlet
nozzle are refractory lined with Incoloy 800H
sleeve on the inner bore. The refractory joint
between the Transfer Line and the inlet nozzle
of the Secondary Reformer at the site weld is a
Z-joint with the inner sleeve overlapping the
sections with a sliding arrangement. This is to
allow for thermal expansion of the refractory
lining and the inner Incoloy Liner. (Figure 3).
Due to this arrangement, lifting out of the
Secondary Reformer without sufficient gap
between the Transfer Line and inlet nozzle of
the Secondary Reformer will damage the
internal refractory and the Incoloy liner of the
Transfer Line. Hence, the Transfer Line has to
be pulled away from the Secondary Reformer
after cutting of the site weld. (Picture 6)
194AMMONIA TECHNICAL MANUAL 2008
Picture 6: Transfer Line pulling arrangement
The pulling away of the Transfer Line will also
result in movement of all the five sub-headers
welded to the Transfer Line and the Primary
Reformer tubes welded to the sub-headers.
Expansion gaps are provided around the
Catalyst tubes at Primary Reformer floor. These
gaps were also physically verified and checked
at site soon after the plant shutdown.
Extensive dimensional measurements were also
carried out on the inlet and outlet nozzles of the
new and old units to decide the exact cutting
location.
The edges of the refractory at the Transfer Line
end and the gas inlet nozzle end have to be
properly made to ensure correct Z-joint fit
between them after erection.
Any problem in this connection can lead to hot
spots at this site weld joint during plant
operation.
f. The Secondary Reformer gas outlet
nozzle is welded to the inlet nozzle of the
Process Gas Cooler (PGC), which is of
horizontal, double compartment design. Extra
precaution was taken to maintain the position
and level of the PGC inlet nozzle after cutting of
the Secondary reformer outlet nozzle
connection. Adequate hold down and movement
arresting temporary clamps were welded to the
support saddles of the PGC to prevent possible
cold pull back of the PGC or change in elevation
and position of the PGC inlet nozzle, after
cutting of the Secondary Reformer nozzle
connection.
Figure3: Old Secondary Reformer to transfer line joint Figure4: New Secondary Reformer to transfer line
joint
195 AMMONIA TECHNICAL MANUAL2008
6.0 Site Erection
The erection activities can be divided into the
following activities.
1. Temporary foundation and erection of
new Secondary Reformer on it.
2. Installation of refractory lining and dry
out of refractory before turnaround.
3. Removal of old Secondary Reformer and
erection of new Secondary Reformer.
6.1 Temporary foundation and erection of new Secondary Reformer:
The temporary foundation was made on the road
closer to the Secondary Reformer due to site
limitation. The anchor bolts locations were fixed
with the help of the base ring template supplied
by the vessel manufacturer. The new Secondary
Reformer received at site was directly erected on
the temporary foundation and aligned vertically.
Perfect vertical alignment of the equipment on
the temporary foundation is of utmost
importance for later installation of the refractory
lining (Picture 7).
Picture 7: New Secondary Reformer erected and
aligned on temporary foundation.
6.2 Installation of refractory lining and dryout of refractory before turnaround:
Scaffolding was build around the vessel and
covered with tarpaulin to avoid overheating of
the steel surface by the sun. A platform was
built in front of outlet nozzle for material
transport and in between storage (Picture 8).
Furthermore a transportable air condition system
was used for best working conditions inside the
vessel.
The refractory installation was started with
casting of gas inlet nozzle at the bottom of
Secondary Reformer (Picture 9).
Picture 8: Platform in front of Secondary Reformer
Picture 9: Casting of inlet nozzle
196AMMONIA TECHNICAL MANUAL 2008
In the next step the first brick rings made of high
alumina were placed on the bottom of secondary
reformer, which is the foundation of the whole
brick lining (Picture 10).
Picture 10: First bricks placed
After completion of the bottom, which is
designed with bubble alumina castable and one
layer high alumina castable on the top, the main
brick laying activity started (Picture 11 &
Picture 12).
Picture 11: Placing of brick in area of catalyst
dome
Until finish of refractory lining activities
Karrena had worked 30 days continuously in
day and night shift. 60 tons High Alumina
bricks, 30 tons High Alumina concrete and 60
tons Bubble alumina concrete were installed
during that time period (Picture 13).
Picture 12: Casting of secondary reformer neck.
Picture 13: Completed refractory lining
Shortly after finish of lining activities the dry
out equipment was installed and the dry out was
started. The heating of the vessel was performed
by using a high velocity gas burner and
combustion air fan. To provide a clear space for
the burner flame and ensure no possibility of
flame impingement to the internal Incoloy liner,
a temporary extension pipe was installed
(Picture 14).
The time period for dry out was 6 days with a
maximum temperature of 550 °C (1022
oF).
The complete activity was finished in the time
period as scheduled.
197 AMMONIA TECHNICAL MANUAL2008
Picture 14: Dry out of refractory lining
6.3 Removal of old Secondary Reformer and erection of New Secondary Reformer
The gas inlet and outlet nozzle projection
measurements of the new Secondary Reformer
were transferred to the old one to mark the exact
cutting location at site. Cutting of the inlet and
outlet nozzle connections of the old Secondary
Reformer was carried out by rotary cutting
machine. This machine was also used to bevel
the nozzle edges for welding. The transfer line
was pulled away from the Secondary Reformer
by 40 mm (1.57”). (Picture 15)
Picture 15: Gap of 40 mm (1.57”) between transfer
line and Secondary Reformer inlet nozzle after
pulling.
Several site measurements in cold condition
with respect to fixed reference marks were taken
before the pulling process to confirm that the
transfer line, sub-headers connected to the
transfer line and the Primary Reformer tubes
also move along with it. These measurements
also helped in verifying that these items went
back to their original location after pushing in of
the transfer line.
A large tracked crane with lifting capacity of
600 tons was installed closer to both Secondary
Reformers. Land preparing and compaction was
done to protect the underground cables from
damage due to the high load of the crane
(Picture 16).
Picture 16: Crane positioned between the old
and new Secondary reformers.
The old Secondary Reformer was lifted out and
rested on compacted / levelled area closer to the
temporary foundation. The integrity of the gas
barrier closer to the cut edge inside the transfer
line was verified. The transfer line was edge
prepared and the internal refractory joint was
prepared to match the joint shape and dimension
of the refractory at the Secondary Reformer gas
inlet nozzle end (Picture 17, Picture 18 and
Figure 4).
198AMMONIA TECHNICAL MANUAL 2008
Picture 17: Gas inlet nozzle refractory joint.
The new Secondary Reformer was shifted to the
original foundation (Picture 19) and the transfer
line was pushed back. The old Secondary
Reformer was then erected on the temporary
foundation for later dismantling of the refractory
lining before shifting it horizontally to the
storage yard.
Actual erection activities from start of cutting of
the inlet and outlet nozzles, refractory repair at
the nozzle connections and welding back the
nozzle connections were completed within a
period of 8 days.
Picture 18: Transfer line refractory joint.
Picture 19: Erection of new Secondary
Reformer.
The modification to the air inlet piping was
carried out in parallel to the other erection
activities. Hydrotest of the air inlet piping along
with the ring header and the air inlet pigtails was
carried out. Loading of the catalyst was
completed in one day and the plugs welded to
the air inlet nozzles were cut and removed after
completion of catalyst loading.
7.0 Actual performance
After the installation in Turnaround 2007, the
new Secondary Reformer was put in service in
December 2007.
Performance of the new Secondary Reformer is
satisfactory. After installation of the new
equipment there has been no observation of
fouling in the Process Gas Cooler till date.
After the 2007 Turnaround, due to improvement
in the downstream equipment the air to the
Secondary Reformer could be increased. In the
Secondary Reformer with the old design, this
would have led to an impingement of flame on
the catalyst, which was detrimental for the
catalyst. With the improved design there is a
margin for increasing air into the Secondary
Reformer. This has helped in increasing the
ammonia production by processing additional
amount of hydrogen received from the PSA
Hydrogen Recovery Unit of Methanol Plant.
199 AMMONIA TECHNICAL MANUAL2008
This additional hydrogen is introduced upstream
of the Methanator.
The methane slip from the new Secondary
Reformer is 0.18% as compared to 0.35%
earlier.
8.0 Conclusion
The new design of the Secondary Reformer has
helped in reducing the methane slip and has
facilitated a higher throughput. This has resulted
in an increase of Ammonia production by
approximately 4 %.
Careful and thorough pre-planning and
proactive measures taken during engineering,
procurement and equipment fabrication as well
as during the plant shutdown helped in the
smooth replacement of the Secondary Reformer
in shortest time.
200AMMONIA TECHNICAL MANUAL 2008