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    An Integrated Approach to TPM and Six Sigma Development in

    the Castings Industry.

    A.J. Thomasa, G.R. Jones

    b, P. Vidales

    c

    aManufacturing Engineering Centre, Cardiff University, CF24 3AA, UK

    bWall Colmonoy, Pontardawe, Swansea, SA1 3DEcEcole d'ingeniear CESI, France

    Abstract

    Both Total Productive Maintenance (TPM) and Six Sigma are key business process strategies which are

    employed by companies to enhance their manufacturing performance. However, whilst there is significant research

    information available on implementing these systems in a sequential manner, there is little information available

    relating to the integration of these approaches to provide a single and highly effective strategy for change in

    companies.

    This paper proposes an integrated approach to TPM and Six Sigma which was developed as a result of workundertaken in the castings industry. The effectiveness of the approach is subsequently evaluated highlighting the

    benefits the host organization received through this new approach by measuring the effects of implementation against

    the seven Quality, Cost and Delivery (QCD) measures.

    Keywords: TPM, DMAIC, QCD Measures

    1. Introduction to TPM and the Six Sigma

    Approach

    Total Productive Maintenance (TPM) is a

    maintenance program which employs a strategy for

    maintaining plant and equipment to its optimum level

    of operational effectiveness. Primarily the TPMapproach links into the Lean concept and aims at

    reducing waste due to poorly maintained machinery

    and provides for value added inputs by way ofensuring machinery remains in productive operation

    for longer periods of time [1]. Maintenance procedures

    and systems are designed so that they are easier to

    accomplish and this is achieved through machine

    redesign and modifications in order to facilitate this

    process.

    Six Sigmacan be considered both a business strategy

    and a science that has the aim of reducing

    manufacturing and service costs, and creating

    significant improvements in customer satisfaction and

    bottom-line savings through combining statistical and

    Business Process methodologies into an integratedmodel of process, product and service improvement

    [2].

    Although both strategies have similar aims, those of

    improving productive effectiveness, the way in which

    these strategies are implemented into companies varies

    greatly. Traditionally Six Sigma employs a structured

    five-phased DMAIC methodology. Six Sigma teams

    are created to tackle specific problems to reach Six

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    Sigma levels of performance [2]. TPM implementationon the other hand is seen to be implemented in a range

    of different ways, although attempts have been made to

    formalise the TPM strategy [3], [4], [5], there is still no

    formally defined approach that can be considered as an

    industry standard approach to TPM implementation.

    However, when considering TPM, it is worth notingthat the basic principles of the TPM strategy have very

    close links to the Six Sigma approach. In TPM the

    ultimate aim is to achieve significantly reduced

    breakdown levels through developing autonomous

    maintenance teams.

    Employing therefore a standard operational framework

    for implementing both approaches is seen as an

    obvious and necessary step for companies to achieve

    simultaneous benefits from the TPM and Six Sigma

    strategies. To this end the DMAIC process is used as

    the main operational approach for the implementation

    of TPM. The following section highlights the

    application of the DMAIC process in theimplementation of TPM in a castings company.

    2. Introduction to Wall Colmonoy

    Wall Colmonoy is a manufacturer of specialist

    castings. The company is based in South Wales and

    manufactures its products to a world wide market.

    Over the years the company has experienced

    increasing competition from the far-east where product

    unit costs have been dramatically reduced. This has

    brought about major changes to the company

    operations and has raised the need for the company to

    become leaner and more responsive to customers if

    they are to remain as serious competitors in their

    market.

    Over the past two years the company has embarked on

    a Lean manufacturing program. As part of the Lean

    approach, TPM and Six Sigma are seen as essential

    strategies for success. However, the company is

    concerned that the separate implementation of such

    approaches means the requirement of large scale

    human, financial and technical resources as well as the

    associated problems of running competing projects in

    the company. The company requires a simple yet

    effective operational framework that can be used as a

    standard approach to adopting both strategies in thecompany. The company expects that worker buy in

    will be easier if one common operational approach is

    adopted

    3. DMAIC at Wall Colmonoy

    The Six Sigma strategy concentrates on a simple

    five phase methodology called DMAIC. DMAIC is an

    acronym of the major steps within the methodology

    namely Define, Measure, Analyse, Improve, Control. It

    was decided that the DMAIC process would form thebasic foundation for the TPM strategy and hence the

    standard approach for adopting the major stages of the

    TPM project. Each stage is explained in detail in the

    following section of the paper.

    3.1 Define

    A benchmarking exercise was undertaken into the

    major product lines operated by the company. The

    product lines were benchmarked against on-time

    delivery and right first time quality levels. A gauge

    R+R study was undertaken in order to ensure that themeasuring equipment was suitable for measuring the

    outgoing quality from the processes. From the analysis

    of the key casting processes within the company, the

    investment casting process was highlighted as the area

    requiring greatest attention with scrap rates in excess

    of 4% and on-time delivery at only 65%. The

    definition stage triggered the development of a TPM

    team within the company. This involved the training ofteam members in the principles of TPM as well as the

    implementation of a 5S program* aimed at piloting

    autonomous cleaning and teamworking prior to

    specific and targeted TPM projects being undertaken

    within the investment casting area.

    3.2 Measure

    Overall Equipment Effectiveness (OEE) was

    calculated on each of the machines within the

    investment casting area. Also, the company measured

    parts throughput (parts per hour) through the cell in

    order to identify whether the inefficiencies were due to

    the machinery or to the operations surrounding the

    machinery or both. As an example, OEE calculated for

    one machine was calculated at 75% however partsthroughput in the cell where the machine operated in

    was 43% less than the theoretical throughput for that

    cell. Further analysis of the cell indicated that the

    process surrounding the machine was at fault rather

    than the machine itself.

    One casting cell was measured as having a throughput

    at 36% of its theoretical value and an OEE value of

    30% for the wax making machine. A process mapping

    exercise confirmed that the wax making machine was

    the major cause of the low cell throughput and so thismachine became the focus of the remainder of the

    project.

    3.3 Analyse

    The OEE value was split down to its constituent

    parts namely; Availability, Performance and Quality.

    * 5S A systematic process of workplace cleaning and

    maintenance. Sort, Sanitize, Stabilize, Systematize, Sustain

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    The results of this analysis showed that machineavailability was lowest at 34% compared to

    performance at 94% and quality at 96%. This clearly

    indicated that machine breakdowns and major stoppage

    problems were the causal point for the poor OEEvalue. A Fault Tree Analysis (FTA) was therefore

    carried out by a team of engineers from within thecompany in order to ascertain the root cause(s) of high

    machinery failure. The FTA is shown in Fig 1 and lists

    the failure routes identified from the brainstorming

    session. Following the FTA, the engineering team

    progressed to creating Failure Modes and Effects and

    Criticality Analysis (FMECA) on each of the areasidentified from the failure routes on the FTA. The

    FMECA allowed the company to identify the potential

    causes of failure, assess its effect on the machine and

    process and also, and most importantly, allow for

    corrective actions to be identified. The engineering

    team did not follow normal FMECA convention at this

    stage and decided to employ individual FMECA sheets

    for each potential failure mode. The benefit this gavethe team was that each sheet could be given to the

    maintenance teams in turn in order to apply the

    corrective action specified in the documents. In order

    to prioritise the issuing of the FMECA sheets to the

    maintenance teams, a Pareto analysis was constructed

    of the Risk Priority Number (RPN) from each

    FMECA study with the higher ranked RPNs being

    tackled first.

    3.4 Improve

    Three levels of TPM were adopted in the

    company in order to improve the machines reliability.

    Level 1 was the introduction of shop floor autonomous

    maintenance teams. These teams applied basic

    maintenance practices including regular daily cleaningregimes as well as undertaking sensory maintenance

    tasks (smell, sound, sight, feel etc). However, prior to

    this level being undertaken, it was essential that major

    machinery and equipment was completely overhauled

    in order to revert the machinery to its original level of

    reliability. This was considered to be Level 2 in the

    TPM system and the work undertaken by the

    maintenance department. Level 3 involved the

    engineering department becoming more pro-active in

    the development of preventive maintenance practices

    including machine modification and enhancementstrategies that allow for easier maintenance etc. Level

    3 work also included the monitoring of maintenance

    FMECA An advanced planning technique aimed at

    systematically assessing all the potential failures of a machine and

    the potential impact (criticality) of the failure on a human and/or the

    system.

    RPN Risk Priority Number. A numerical method of analysing the

    failure mode and its effect on the system. RPN = Severity x

    Occurrence x Detection.

    activities and concentrating primarily on approachestowards increasing Mean Time Between Failures

    (MTBF) so that higher machine availability is

    achieved. The aim here is to systematically extend the

    mean time between failure so that the machinery can

    remain productive for longer thus providing greater

    return on machine performance. Table 1 shows thework undertaken at each level in the TPM system.

    Table 1 TPM Levels and Work Definition

    Levels of TPM Operation and Typical Activities

    Level 1 Level 2 Level 3

    Basic Cleaning Machine

    overhaul

    Machine

    redesign

    Machine care

    plans

    Major

    Maintenance

    MTBF analysis

    & extension

    Sensorymaintenance

    Level 1Monitoring

    Level 2Monitoring

    3.5 Control

    The work undertaken by the pilot TPM work wasmeasured for its effectiveness before being rolled out

    through the company. Machine maintenance schedules

    and plans were formalized and attached to each

    machine. All operators were trained to undertake the

    maintenance schedules and to report any issues to the

    maintenance teams. As a control mechanism, it is the

    responsibility of the maintenance department to

    monitor the work of the operators and to rectify any

    issues raised by the shop floor personnel.

    The engineering department in turn monitored theoutputs from the maintenance department in order to

    identify recurring failures and issues that could be

    redesigned in order to prevent future failures. Theengineering team provided the technical and financial

    support to the maintenance department in order to

    facilitate the high level maintenance activities

    undertaken at the level 2 stage. Fig 2 shows the

    autonomous team approach at each of the TPM levels

    in the organization and how each level integrate with

    each other.

    Fig 2 Autonomous Team Structure

    TPM Autonomous teams

    11

    22

    33

    44

    OperatorsOperators

    Team LeaderTeam Leader

    11

    22

    33

    44

    11

    22

    33

    44

    MaintenanceMaintenance

    Team LeaderTeam Leader

    EngineersEngineers

    Team LeaderTeam Leader

    Complexity of maintenance function- +

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    4. Evaluation

    As part of the companys approach to improving

    their Quality, Cost and Delivery targets, i t was decided

    to measure the QCD [6] outputs as a direct result of theTPM project. Table 2 shows the improvements made

    in each QCD area.

    In this case, the benefits gained from undertaking theTPM project may be considered idealistic when

    comparing the large benefits gained from a relatively

    small initial financial outlay. However, the costs

    incurred in continuously controlling the input variables

    and factors means that the monitoring costs can be

    large and greater than first expected. This in turn can

    affect the true savings achieved from the project. The

    issue of cost analysis and control is as a key

    consideration and its correct analysis and interpretation

    is key to providing credibility to the TPM strategywithin the company.

    5. Conclusions

    A TPM pilot study was undertaken in order toimprove the Quality, Cost and Delivery measures

    of the company. In all measures, the TPM project

    achieved significant improvements.

    This relatively simple application of TPM using astructured DMAIC technique should allow for

    increased use of the methodology for tackling

    many maintenance issues. Likewise, the results

    can also provide the stimulus for the widerapplication of the technique to create process

    improvements at relatively lower costs.

    The application of the TPM approach to the waxmachine area at Wall Colmonoy achieved savings

    in excess of 200,000 for an initial outlay of less

    than 4,000 in experimental and project costs.

    The development of the TPM approach developeda culture towards continuous improvement and the

    systematic implementation of the system

    throughout the organisation.

    The application of the TPM approach allowed thecompany to develop advanced systems mapping

    and analysis techniques and to become generally

    more technical in their approach to problem

    solving .

    Acknowledgements

    The authors would like to express their

    appreciation to the following organisations for their

    support during the development of the project and the

    writing of this paper: Wall Colmonoy, I*PROMS,

    Cardiff University Innovative Manufacturing Research

    Centre.

    References

    [1] Jostes R S, Helms M M. Total Productive

    Maintenance and Its Link to Total Quality

    Management. Work Study Journal. (1994), 43,7.[2] Breyfogle, F.W. Implementing Six Sigma,

    Smarter Solutions - Using Statistical Methods,

    (1999).John Wiley & Sons Inc.

    [3] Blanchard,B S.An enhanced approach for

    implementing total productive maintenance in the

    manufacturing environment, Journal of Quality in

    Maintenance Engineering.(1997), 3,2.

    [4] Jens,O, Riis J, Luxhj T, Thorsteinsson U. A

    situational maintenance model

    International Journal of Quality & ReliabilityManagement; (1997).14, 4.[5] Raouf A, Ben-Daya M. Total maintenance

    management: a systematic approach,Journal of Quality in Maintenance Engineering;

    (1995) 1,1.

    [6] Achieving Best Practice in Your Business

    QCD Measuring Manufacturing Performance.

    Department of Trade and Industry Brochure,

    www.dti.gov.uk.(2002).

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    Fig1

    AnFT

    A

    ofthepossiblefactorsinfluencingmachineperformance

    Auto

    WaxMachine1

    OEE=35,5

    %

    SCRAP

    BREAKDOWN

    Partsinoil

    Dipping

    Parts

    c

    hipping

    Parts

    sticking

    Air

    entrapment

    Fla

    shing

    Tool

    jamming

    Wiperarm

    creeping

    down

    Injection

    system

    Hydraulic

    pipes

    bursting

    No

    regulators

    Noset

    variables

    Wax

    Temp

    Back

    plates

    arentcold

    Water

    coolingnot

    working

    Leak

    cooling

    Par

    tsfalling

    one

    achother

    F

    lushing

    systemnot

    w

    orking

    Pumps

    notworking

    S

    ystem

    b

    locking

    Water

    contaminated

    Tool

    Sprue

    T

    emp

    Control

    Wipernot

    long

    enough

    Patterns

    notcool

    Nozzle

    design

    Suckingin

    air

    Nozzle

    temp

    Spread

    of

    stirring

    Seal

    worn

    Part

    springing

    Plate

    cooling

    Hold

    time

    Air

    entrapment

    Wear

    onthe

    tool

    Brass

    bush

    wearing

    Surface

    Finish

    Sprue

    stuck

    Ejector

    pinsnaps

    Nowax

    Blockage

    Waxblocked

    infeedfrom

    tank

    Blockage

    atnozzle

    Stirrer

    notlong

    enough

    Debris

    intank

    Temp

    control

    Poor

    hou

    sekeeping

    Pouring

    system

    Nozzle

    des

    ign

    Temp

    control

    at

    nozzle

    Water

    heating

    Handling

    problem

    Tool

    condition

    Storage

    Dust

    Sealsin

    system

    Oilin

    water

    AND

    OR

    LEGEND

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    Table 2 Quality, Cost Delivery The Seven Measures

    ie

    60-30

    30

    5%1%

    1% - 5%

    5%

    Improvement =

    ie

    Increase

    Increase

    i.e.

    Increase

    Number of planned deliveries - Number of not on time

    deliveries

    30,000 per employee

    30,000

    50,000 - 30,000Improvement =

    Number of employees

    30%

    (Gross) Value Added

    per Person

    Basic Measure: / person Example of Improvement Measure

    Previous StateOutput value - Input value New State 50,000 per employee

    96% - 80%

    80%

    66% effective

    66% - 30%

    Value of (Raw material + WIP + Finished Goods)

    Improvement =

    Overall Equipment

    Effectiveness

    Basic Measure: % Example of Improvement Measure

    Previous S tate 30% e ffective

    i.e. Availability % x Perfomance % x Quality % New State

    Improvement =

    90%

    Increase in Stock

    Turns

    Basic Measure: Number of turns Example of Improvement Measure

    Previous S tate 4 S tock Turns

    Sales turnover of product New State 5 Stock Turns

    99% delivered on Time

    Improvement = 99% - 90%

    50,000 - 30,000=67%

    30,000

    On Time Delivery

    Improvement

    Basic Measure: % delivered correctly and on t ime Example of Improvement Measure

    Previous State 90% del ivered on Time

    New State

    Number of not on time deliveries

    People Productivity

    Improvement

    Improved Space

    Utilisation

    Basic Measure: per m2 Example of improvement measure

    Previous S tate 30,000 per m2

    Sales turnover of model area New State 50,000 per m2

    Number of square metres of area

    Scrap / Defect

    Reduction

    Basic Measure: % Example of Improvement Measure

    Previous StateQuantity of defective units New State

    Total quantity of units supplied Improvement =

    Basic Measure: Units per direct operator hour Example of Improvement Measure

    Previous S tate 30 Uni ts per Hour

    Number if good units made New State 60 units per Hour

    Number of direct operator hoursImprovement = 50%

    i.e a 80%

    reduction indefects (reported

    as a positive

    number

    =10%

    =20%

    =120%

    =67%