sree jayajothi cements private limited … cement... · sr.gm-engineering sr.gm-operations ... 5...
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Team Members:
R Venkateswarlu-Sr.DGM (Safety)
R.Laxmana Rao-DGM (Instrumentation)
E.Parameswara Rao-Dy.Manager (Process)
SREE JAYAJOTHI CEMENTS PRIVATE LIMITED
YANAKANDLA-KURNOOL-A.P
CII ENERGY EXCELLENCE AWARD-2017-18
➢ My Home Industries Pvt. Ltd. (MHIPL) was
established in the year 1998 with an installed
capacity of 0.2 MTPA, which has now risen to
10 MTPA.
➢ My Home Group have Various businesses like
Cement ,Construction, Real Estate, Power and
Education.
➢ MHIPL is a joint venture with CRH plc.
Ireland, an international leader in building
materials.
➢ SJCPL was taken Over by MHIPL in August
2013.
➢ SJCPL, YCW has Single line (capacity 3.2
MTPA) with state-of-the-art-Technology from
LNVT, the world’s leading suppliers of Cement
manufacturing equipment.
Company Profile
Location Capacity
SJCPL-Yanakandla Cement Works-Kurnool 3.2 MTPA
Mellacheruvu Cement Works- Kodad 3.3 MTPA
Vizag Grinding Unit- Yalamanchili 2.0 MTPA
Tuticorin Grinding Unit- Tamilnadu 1.5 MTPA
Total 10 MTPA
My Home Group Cement Businesses
Cement Process Flow Diagram
Management Systems
SJCPL Policies
Energy Review Methodology
Review of Energy Consumption with
respect to production in Daily
Production Meeting
Energy Committee Cell meeting for
Review of Energy Conservation
Projects
Setting of Annual Targets for
achieving National and International
Benchmark
Daily Monthly Yearly
Unit Head
Sr.GM-Engineering Sr.GM-Operations
HOD-Mech HOD-ProcessHOD-Elect Energy Manager HOD-Inst HOD-Mines HOD-QC HOD-Stores
Section
Incharges
Section
Incharges
Section
Incharges
Section
Incharges
Section
Incharges
Section
Incharges
Section
Incharges
Energy Management System Organization Structure
737.70
715.00
697.70695.10
692.58
670.00
680.00
690.00
700.00
710.00
720.00
730.00
740.00
750.00
2013-14 2014-15 2015-16 2016-17 2017-18
Sp.Thermal energy Consumption -Kcal/Kg Clinker
45 Kcal/Kg cl
6.2% Reduction
Energy Performance From last 5 Years
54.1
52.3252.06
51.16
49.77
47
48
49
50
51
52
53
54
55
2013-14 2014-15 2015-16 2016-17 2017-18
Electrical SEC: Up to Clinkerisation, Kwh/Ton of Clinker
4.33 Kwh/Ton of cl
8 % Reduction
Energy Performance From last 5 Years
78.8075.46
78.26 76.35 75.53
55.28 55.84
62.74 64.1267.44
0.00
10.00
20.00
30.00
40.00
50.00
60.00
70.00
80.00
90.00
2013-14 2014-15 2015-16 2016-17 2017-18
Electrical SEC : Total Plant ,Kwh/Ton of Cement
Kwh/ton of Cement % of OPC Production
Energy Performance From last 5 Years
1443.56 1428.73 1366.33
750.58 704.14610.34
0200400600800
1000120014001600
2015-16 2016-17 2017-18
Lakh Units Units cost Rs.Lakhs
46
48
50
52
54
56
Top 10 BestPlants
Top 3 BestPlants
SJCPL
54.08
49.17 49.77
Electrical SEC up to Clinkerisation
Kwh/Ton of Cl
60.00
65.00
70.00
75.00
80.00
Top 3 BestPlants
Top 10 BestPlants
SJCPL
66.20
70.76
75.53
Total Plant Electrical SEC
Kwh/Ton of Cement
680
685
690
695
700
705
Top 10 BestPlants
Top 3 BestPlants
SJCPL
703
690692
Thermal SEC -Kcal/Kg Clinker
National Benchmarking
Electrical Energy Bill
Ref :CII Energy Benchmarking for Cement Industry Version. 2.0, May 2015
Major Modification in 2014-15
S.No Project Description Reason for Modification
1 Precalciner height was extended downwardsTo Complete burn out of fuel and to
enhance the Production Capacity
2Entire Clinker Cooler was replaced with FLS CB Cooler with ABC
inlet
To increase the Heat Recuperation
efficiency and also to ensure better run
factor
3 Top Stage cyclone-1 was modified To improve the Collection efficiency
from 90-96%
4Low density Refractory bricks were lined in Cyclone-1 supplied by
M/s Skamol A/S, DK-7900 NykØbing, DenmarkTo reduce the Radiation losses
5
Preheater down comer duct was modified to the same diameter from
top of cyclone-1 to the preheater fan inlet to reduce the pressure
drop.
To reduce the pressure drop from Top
cyclone to PH fan inlet
6 Replaced kiln inlet & outlet seal arrangement with lamella seal
To avoid false air entry and to improve
the life of tip castings.
7 Modified kiln inlet smoke chamber with introduction of “Trough”To reduce Hot meal entrainment in Kiln
exit gases
Pre-calciner Modification Cyclone-1 Modification
KILN OUTLET SHELL AND SEAL BEFORE MODIFICATION
KILN OUTLET SHELL AND SEAL AFTER MODIFICATION
Kiln Outlet Seals ModificationPrevious Cooler FLS CB Cooler
Major Modification in 2014-15
S.No Project type
EnCon
Projects
2015-16
EnCon
Projects
2016-17
EnCon
Projects
2017-18
Total Annual
Savings
(Rs. In Lakhs)
CO2
Mitigation-
MT/Year
1 Zero Investment 3 13 5 250.41 1813
2 Investment 5 9 4 516.96 15506
Total 8 22 9 767.37 17319
Energy Conservation Initiatives
Zero Investment Investment
EnCon Projects 2015-16
S.No Project Description
Annual Electrical Savings Lakh Kwh
Annual ThermalSavings
Annual Electrical Savings
Total Cost Savings
Lakh Units Rs. Lakhs MT of Fuel Rs. Lakhs Rs. Lakhs
1 a).Entire burner replacement with new FLS
Duoflex burner
b).Kiln outlet sealing arrangement with
lamella seal.
1.74 9.03 5139.4 272.39 281.42
2 Conversion of 15 no's of kiln shell cooling
fan motor from delta to star connection 3.26 16.96 0 0.00 16.96
3 25 nos. of 90 watts LED Lamps fitted
instead of 250 watts SV lamps0.16 0.84 0 0.00 0.84
4 Timer Based ON/OFF lighting programmed
for colony street lighting0.04 0.19 0 0.00 0.19
5 Conversion of motor from delta to star
connection of Packing plant bucket Elevator
for 4 nos.3.36 17.46 0 0.00 17.46
6 Provided ON/OFF inter lock system for
GGBS Bin aeration blower based on
controlled bin weight0.38 1.97 0 0.00 1.97
7 Replacement of Raw Mill fan inlet Venturi
duct to reduce pressure drop3.60 18.72 0 0.00 18.72
8 Replacement of Coal Mill fan inlet Venturi
duct to reduce pressure drop1.56 8.11 0 0.00 8.11
Zero Investment Investment
EnCon Projects 2016-17
S.No Project Description
Annual Electrical Savings Lakh Kwh
Annual ThermalSavings
Annual Electrical Savings
Total Cost Savings
Lakh Units Rs. Lakhs MT of Fuel Rs. Lakhs Rs. Lakhs
1Interlock Cooling tower fans operation
with cold well temperature0.18 0.96 0 0 0.96
2 Reduce False Air in Coal Mill Circuit 1.28 6.63 0 0 6.63
3 Reduce False Air in Raw Mill Circuit 1.22 6.35 0 0 6.35
4 Reduce false air across preheater 3.68 19.16 0 0 19.16
5Avoid venting air in Raw Mill Silo Aeration
Blowers0.26 1.35 0 0 1.35
6Reduce pressure drop across damper in
crusher bag filter fan by installing VFD0.57 2.95 0 0 2.95
7 Optimization of Slag Mill inlet pressure 1.28 6.66 0 0 6.66
8Avoid head loss across Venturi in Slag Mill
fan0.80 4.16 0 0 4.16
S.No Project Description
Annual Electrical Savings Lakh Kwh
Annual Thermal Savings
Annual Electrical Savings
Total Cost Savings
Lakh Units Rs. Lakhs MT of Fuel Rs. Lakhs Rs. Lakhs
9 Avoid damper loss in Cement Mill Fan 2.44 12.71 0 0 12.71
10Reduce pressure drop across Clinker silo
top bag filter fan damper0.13 0.68 0.00 0.00 0.68
11Avoid head loss across Venturi in
Cement Mill fan4.63 24.07 0.00 0.00 24.07
12Avoid damper loss in coal mill bin venting
bag filter fan by installing VFD0.26 1.35 0.00 0.00 1.35
13Inlet Louver dampers of Cooler FD Fans
are removed5.23 27.20 0.00 0.00 27.20
14 Optimization of packing plant bag filters 0.71 3.71 0.00 0.00 3.71
15Raw Mill Cyclone RAL Motor connection
changed from Delta to star connection
(4No’s).
0.66 3.42 0.00 0.00 3.42
Zero Investment Investment
EnCon Projects 2016-17
EnCon Projects 2016-17
S.No Project Description
Annual Electrical Savings Lakh Kwh
Annual Thermal Savings
Annual Electrical Savings
Total Cost Savings
Lakh Units Rs. Lakhs MT of Fuel Rs. Lakhs Rs. Lakhs
16Replaced 55 Kw Laterite Belt conveyor
(221 BC-9)) motor with 37 KW motor 0.52 2.69 0.00 0.00 2.69
17Star / Delta panels are arranged for
Cement Mill Reject Bucket Elevator0.10 0.54 0.00 0.00 0.54
18Changed Raw mill Magnetic separator
Motor connection from delta to Star
connection
0.09 0.46 0.00 0.00 0.46
19
Changed 2 nos of Cement mill Magnetic
separator Motor connection from delta to
Star connection
0.22 1.16 0.00 0.00 1.16
20Installed HT Capacitor banks to improve
the Power Factor18.25 94.90 0.00 0.00 94.90
2190 W LED Fittings replaced in place of
250W SV LAMP Fittings (150 No’s) 0.88 4.56 0.00 0.00 4.56
22Introduced the high efficiency Transformer
for the cooler ESP field 1 & 22.34 12.17 0.00 0.00 12.17
Zero Investment Investment
Zero Investment Investment
EnCon Projects 2017-18
S.No Project Description
Annual Electrical Savings Lakh Kwh
Annual ThermalSavings
Annual Electrical Savings
Total Cost Savings
Lakh Units Rs. Lakhs MT of FuelRs. Lakhs
Rs. Lakhs
1Improved Coal Conveying phase density by
re-rooting the coal conveying line7.865 47.19 383 28.89 76.08
2Avoided Raw water pump running in Pump
House0.45 2.70 0 0 2.70
3 Optimization of Nitrogen compressor air 6.99 41.92 0 0 41.92
4Installation of VFD for Cement Mill Booster
fan 2.25 13.50 0 0 13.5
5Modification of Gypsum feeding belt
conveyor with Y-Chute0.21 1.26 0 0 1.26
6Installation of High Efficiency impeller for
Cooler ESP fan1.885 11.31 0 0.00 11.31
7Removal of Cooler fans Silencers for
reduction of pressure drop across silencers2.925 17.55 0 0.00 17.55
8
Installation of VFD drive for 511 BC3
Venting Bag Filter for reduction of damper
loss-Cement Mill Section
0.32 1.94 0 0 1.94
9Installation of LP Compressor for fly ash
unloading1.61 9.66 0 0 9.66
Innovative Projects
PROJECT-1
INSTALLATION OF Y-CHUTE FOR GYPSUM FEEDING
Project Description:
In our Cement Mill & Slag Mill section, we have 3 belts conveyors for
Gypsum feeding. At Gypsum Hopper top, spillages was happening daily
under the belt conveyor.so, every day Man Power were deploying for
spillage cleaning.
Action Taken:
After Brain Storming, On view of Energy Conservation and to avoid
spillages, our team has decided to install a In-house designed Y-Chute for
Gypsum Feeding at top of the hopper in place of reversible belt.
Benefits:
Annual Power Saving :0.21 Lakh Kwh
Annual Cost Saving :Rs.1.26 Lakhs
Investment :Zero
Pay Back :Immediate
Before
After
Before After
PROJECT-1
INSTALLATION OF Y-CHUTE FOR GYPSUM FEEDING
PROJECT-2
INSTALLATION OF SOLAR LIGHTING SYSTEM IN MINES AREA
Project Description:
Earlier Mobile lighting Diesel generator was used for lighting purpose in
our new Limestone Mining area. Diesel generator consumes more HSD oil
at around 493 Lts/Month (5.75 KL/Yr.). On Energy Conservation View and
environmental protection View our team has decided to replace the Mobile
lighting Diesel generator with Solar Lighting System.
Action Taken:
Our team has installed a Solar Lighting System in place of Mobile Lighting
Diesel Generator at New Limestone Mining area.
Benefits:
Annual GHG Reduction :17.25 MT of CO2
Annual HSD Saving :5.75 KL
Annual Cost Saving :Rs.3.74 Lakhs
Investment for Solar Panels :Rs.2.85 Lakhs
Pay Back :9 Months
Mobile Lighting DG Set
Solar Lighting System
PROJECT-3
REMOVAL OF VENTURIES FOR ALL PROCESS FANS
Project Description :
Installed Raw Mill (LM 56.4+4 ), Cement Mill (LM56.3+3), Slag Mill (LM46.2+2) & Coal Mill
(LM28.2+2) for raw materials Grinding. All mill fan inlet ducts are designed with Venturies for
online flow indication. It was identified and measured that Venturi pressure drop was 15-25 mmwg.
Reviewing the Venturies Pressure drop, management decided to remove the venturies for all
process fan inlet ducts.
Action Taken :
All venturies were removed and hooked up with In- house fabricated same diameter duct at all
process fans inlet ducting to avoid pressure drop across venturies.
Benefits:
Area Annual Electrical
Saving - Lakh Units
Annual Cost Saving
Rs. Lakhs
Investment
Rs. Lakhs
Pay Back-
Months
Coal Mill 1.56 8.11 2 3
Slag Mill 0.8 4.16 2.2 6
Raw Mill 3.6 18.72 12.5 8
Cement Mill 4.63 24.07 6.76 3
Coal Mill Slag Mill
Raw Mill Cement Mill
Before
BeforeBefore
BeforeAfter After
After After
PROJECT-3
REMOVAL OF VENTURIES FOR ALL PROCESS FANS
EnCon PROJECT-1
REPLACEMENT OF PRESENT BURNER WITH DUOFLEX BURNER
Project Description:
Previous burner was designed for lower capacity and
consumes more primary air at around 13-14%. It was decided
to reduce the Primary air consumption for reduction of STEC
by installing the FLS Duoflex burner.
Action Taken:
With management’s approval ,Existing burner was replaced
with New Duoflex Burner to reduce Primary air consumption
for reduction in STEC
Benefits:
Primary Air percentage reduced from 13% to 8%
Sp.Heat Consumption reduced by 3 Kcal/Kg Clinker
Project Description :
Earlier high pressure compressor (6 bar ) was used for fly ash unloading
by regulating the pressure from 6.0 bar to 3.0 bar. It was decided to install
a dedicated Low Pressure compressor for pumping the flyash into
Concrete silo to reduce the Power consumption and safety concerns.
Action Taken :
With management’s approval, LP compressor was installed dedicatedly for
flyash tankers unloading and pumping into the concrete silo.
Benefits:
Annual Power Saving = 1.61 Lakh Kwh
Annual Cost saving = 9.7 Lakhs
Investment = Rs.25.6 Lakhs
Pay back = 2.6 Years
Before-6.0 bar After-3.0 bar
EnCon PROJECT-2
INSTALLATION OF LP COMPRESSOR FOR FLY ASH UNLOADING
Utilization of Renewable Energy
0
2
4
6
8
10
12
14
16
18
20
2014-15 2015-16 2016-17 2017-18
0 0
11.65
18.15
Lakh Kwh
Installed in August-2016
Utilization of Waste Oils instead of HSD Oil
➢ Petro Polymer Fuel & Pyrolysis Oils are used for Kiln Light up and
Hot air Generator Light Up.
➢ Pyrolysis Oil is generated from Tyres waste
➢ PPF is generated from Plastic Waste
➢ 1MT of HSD oil releases the 3 MT of CO2 Gases.
➢ By using this PPF & Pyrolysis oil, the Carbon emissions are also reduced.
25
31.31
0
5
10
15
20
25
30
35
2016-17 2017-18
Pyrolysis Oil-KL
75
94
0
20
40
60
80
100
2016-17 2017-18
Co2 emissions reduction-MT/Yr
Green House Gases Mitigation
830
840
850
860
870
880
890
900
910
920
930
2014-15 2015-16 2016-17 2017-18
922.60
911.57904.13
864.71
Kg CO2/MT Clinker
Good
Green House Gases Mitigation
Year
Scope 1 emissions Scope 2 emissions Scope 3 emissions Total
Kg CO2/MT
Clinker
Kg CO2/MT
Clinker
Kg CO2/MT
Clinker
Kg CO2/MT
Clinker
2014-15 835.67 86.41 0.52 922.60
2015-16 825.16 85.46 0.95 911.57
2016-17 822.17 81.03 0.93 904.13
2017-18 786.80 77.04 0.87 864.71
Scope-1 Cement Process-Calcination , Fuel burning in Kiln and HAG
Scope-2 Electricity Consumption form Grid
Scope-3 Raw Material Transport
PAT CYCLE-2 status
1059
1005
995
960
980
1000
1020
1040
1060
1080
Base Line
2014-15
Target
PAT Cycle-2
Achieved
2017-18
GTG SEC- (Kcal/Kg Eq.of Cement)
S.No Project Description Investment Rs.Lakhs
1 Installation of 7 MW Waste Heat recovery System 7500
2 Installation of 10Mwp Solar Power Plant (Phase-2) 8000
3 Improving the TSR 1% to 3 % by installing the AFR System 150
4 Installation of Pfister pumps for pulverized coal pumping system 400
5Optimize the pressure drop across preheater from cyclone 4 to
cyclone 280
6 Installation of High efficiency impeller for Cement mill fan 35.20
7 Installation of High efficiency impeller for Raw Mill Bag House fan 33.74
8 Replacement of all conventional lights with LED lights 42.25
Road Map for Achieving National & International
Benchmarking (2018-19)
0
2000
4000
6000
8000
10000
12000
14000
16000
18000
20000
15000
18898
11639
9098
Saplings
Green Belt Development
Water Conservation Methods
Mines Pit
STP -300 KL
Rain Water Harvesting Pits
Capacity-1.36 Lakh m3
Online AAQS
Water Sprinkling at Mines Roads Vanam Manam Program Plantation on 44th World Environment Day
Environmental Activities
Employees involvement & Awareness on Energy Conservation
Water & Energy Conservation Pledge on Every Saturday Energy Cell Meeting
Training Programs on Energy Conservation for Employees & Employee’s spouse
Employees involvement & Awareness on Energy Conservation
Awareness Program for Promotion of Blended Cements for reduction of Green House Gases
for Cement dealers, Marketing & Sales department
National Energy Conservation Day-2017 Celebrations
44th World Environment Day-2017 Celebrations
Employees involvement & Awareness on Energy Conservation
INDIA’ S MOST PROMISING BRAND 2015 AWARD
By World Consulting & Research Corporation, LONDON
Awards & Accolades
Awards & Accolades
SEEM National Energy Management Award-2016 SEEM National Energy Management Award-2017
APEX India Excellence Award-2017NCCBM Best Energy Practices Award-2016