first use of cesium formate lsobm as well perforating fluid (2002)
DESCRIPTION
Development and application of low-solid oil-based perforation fluid to maximize well productivityTRANSCRIPT
Development and application of a low-solid Development and application of a low-solid oil based perforation fluid to maximize well oil based perforation fluid to maximize well productivityproductivity
Anne-Mette Mathisen,Anne-Mette Mathisen,Eva Alterås, Morten StenhaugEva Alterås, Morten Stenhaug
Aberdeen 20. - 21.03.2002Aberdeen 20. - 21.03.2002
Outline of the presentationOutline of the presentation
The case
Field description
Well design
Revision of the perforation fluid
Investigation and development of new perforation fluids
Perforation of well A-23H - result and operational experience
Conclusion
The case....The case....
Some of the long horizontal wells in the Visund field has shown considerably lower well productivity than expected
Detailed work to understand the mechanisms which influenced the productivity of these wells, and to identify methods to improve productivity were initiated
Strategies for completion, perforation and completion fluid were given highest priority
The Visund Field The Visund Field North Sea, Norwegian sectorNorth Sea, Norwegian sector
Snorre A/B
VisundVigdis
Tordis
Bergen
Florø
Stavanger
The Visund DevelopmentThe Visund Development
Subsea development - water depth : 335 m
Semisubmersible production, drilling and living quarters platform
23 wells, 13 horizontal producers including 2 satellite wells
Platform located above subsea completed wells with flexible risersbetween the wellheads and the platform
Production strategy based on both water and gas injection
Capacities :
Oil production : 16000 Sm3/dGas production: 10 - 13 M Sm3/dWater production : 18000 Sm3/d
Visund developmentVisund development
The Visund ReservoirThe Visund Reservoir
Sandstone of the Jurassic Statfjord, Amundsen and Brent groups
Heavily segmented by faults with varying sealing properties
Saturated and undersaturated oil, with various composition and pressure within different reservoir segments
Medium to high initial reservoir pressure:
Pres : 430 - 460 barTres : 114 - 118 deg. C
Visund - Well location map
0 1 2 3 4 5Kilometer
N
B-2H
B-1AH
A-11H
A-9H
A-10AH
B-1H
BRENT N2
BRENT N1BRENT S1
STATFJORD/AMUNDSEN
A-1AH
A-7H
A-2HA-1BH
A-23H
A-5H
A-8HA-3H
A-5CHOil - Statfjord and Amundsen
Gas -Brent
Oil -BrentA-5AH
A-25H
A-5DH
Visund Nord
N3
Original Well designOriginal Well design
1000 - 2000 m horizontal section drilled with OBM
Perforated liner
12 spf, low debris, deep penetrating zinc charges
Overbalanced perforation in CaBr2/CaCl2-based kill pill
7" tubing, down hole pressure and temperature gauge
Immediate clean up
Welltype : Oil ProducerRKB Kværner subsea Xmas tree
0m
MSL 29mALL DEPTHS FROM RKB
Seabed @ 364m RKB7", 32#, Tubing
TRSCSSV TSM 7.5 @ 425m (top item) Perforation From (m MD) To (m MD) Length perf.(m)7" liner
30" shoe @ 451m 7" liner 7" liner
7 5/8", 39#, Tubing
18 5/8" shoe @ 1487m MD
13 3/8" shoe @ 3500m MD
Calculated TOC - 3900m MD
NaCl Brine 1.10 s.g. Pressure Gauge Carrier @ 4250m MD
SBRM Packer @ 4300m MD2 Way Seals
SABL-3 Packer @ 4350m MDNo Seals
Flexlock Liner Hanger w/ZXP Packer, TOL @ 4400m MD
Halliburton Communication Cplg. 10 3/4" shoe @ 4500m MD(shear pin)
TD @ 6470m MD
OCRE FBIV @ 4375m MD
General Completion Schematics
Well 34/8-A-23H
Well Sketch : 23 Oct 00
Geological cross-section along the wellpath, well 34/8-A-23 HGeological cross-section along the wellpath, well 34/8-A-23 H
-3050
-3000
-2950
-2900
-2850
-3050
-3000
-2950
-2900
-2850
3000 3500 4000 4500 5000
3000 3500 4000 4500 5000
Stat1_1
Stat1_2
Stat1_3
Stat1_4
Stat2_1
Stat2_2Stat2_3
Am1_1
Am1_2
0 100 200 300 400 500
Meter
TD @ 6147m MD
TD @ 6616m MDDown 1
Up 1
Down 2
Perforated intervals
Scope of work :
" Well productivity for the next producers to be significantly improved relative to previous wells"
Reevaluation of the completion strategy
Reevaluation of perforation strategy
Reevaluation of completion fluid strategy
Improvement of well productivityImprovement of well productivity
Criteria for selection of perforation fluidCriteria for selection of perforation fluid
Compatibility with formation rock
Compatibility with formation water
Compatibility with packer fluid
Particle content for fluid loss control
Cost
Criteria for selection of perforation fluidsCriteria for selection of perforation fluids
Reservoir pressure of 430 bar requires 1.65 s.g fluid density
Available brines with sufficient density:
CaCl2/CaBr2 < 1.71 s.g
KCOOH/CsCOOH < 2.20 s.g( ZnBr < 2.30 s.g )
Review of CaClReview of CaCl22/CaBr/CaBr22 as perforation fluidas perforation fluid
Compatibility with formation rockFormation damage tests showed 30 % reduction in permeability
Formates showed only 10 % impairment
Compatibility with formation waterRisk of CaCO3 precipitation due to high content of HCO3-
Formates entirely compatible
Compatibility with perforation chargesLow debris zinc charges used due to long horizontal perforation interval and the need for effective cleanup
Formation of ZnO powder during detonation in the vicinity of water
Possible formation of cement material due to further reaction with Ca-ions in the brine
Theory:
Zn + H2O => ZnO + H2
Zn + 2H2O => Zn(OH)2 + H2
Zn + CaCl2 + 2H2O => ZnCl2 + Ca(OH)2 + H2
xZn(OH)2 + yZnCl2 +zH2O => 2Zn(x+y)(OH)xCly(H20)z
Ref. SPE58758
Review of CaClReview of CaCl22/CaBr/CaBr22 as perforation fluidas perforation fluid
Review of CaCl2/CaBr2 as killpillReview of CaCl2/CaBr2 as killpill
In-house laboratory work verified the behavior of zincpowder in Ca-based brines.
Review of CaClReview of CaCl22/CaBr/CaBr22 as perforation fluidas perforation fluid
Perforation in oil based mud ???
Low content of water => reduced reaction with Zn-charges
Good fluid loss controlOil as continuos phases => reduced relative permeability effectsImproved clean up of the toe of the well due to low viscosity
Operational preferable due to high potential for time and cost saving
1.65 s.g OBM => extreme amounts of solids and potential for particle settling and plugging of perforation tunnels
High risk of reduced productivity
#2*@31 mm #4@whole length
Wel
lbor
e
Form
atio
n
#3@56mm
* Differential Pressure Transducer.
Investigations to qualify a new perforation fluidInvestigations to qualify a new perforation fluid
Study initiated with MI Norge to investigate the effect of different perforation fluids
Core flood tests to evaluate formation damage potential of water based andoil based perforation fluids and the impact of zinc perforation debris
Conventional brines (1.26 s.g NaCl, 1.38 s.g CaCl2, 1.55 s.g CaBr2, ), 1.55 s.g OBM and a new 1.65 s.g invert emulsion system with CsCOOH
Ref. SPE 73709MI Norge, SPE Formation damage Conference Lafayette, Feb. 2002
Investigations to qualify a new perforation fluidInvestigations to qualify a new perforation fluid
Core flooded with 1.26 s.g NaCl with perforation debris
Core flooded with 1.55 s.gOBM with perforation debris
Ref.: SPE73709
Investigations to qualify a new perforation fluidInvestigations to qualify a new perforation fluid
Conclusion from the core flood tests
Particle content in the perforation fluid effect the perforation clean up efficiency
Water based fluids show a chemical reaction with perforation debris that increase the fluid loss
Ref. SPE73709
Revised criteria for selection of perforation fluidRevised criteria for selection of perforation fluid
Low impairment of permeability
Entirely compatible with formation water
Low content of water to reduce reaction with perforation debris
Low content of particles to improve cleanup of perforation tunnels
Oil as continuos phase to reduce relative permeability effects
Low viscosity to increase cleanup efficiency at the toe of the well
Less emphasis on cost
New perforation fluid for well A-23HNew perforation fluid for well A-23H
Low solid oil based perforation fluid (LS OBM)
Density 1.65 s.g Oil to water ratio of 40/60
CsCOOH as internal phase
Minimum content of CaCO3 particles (60-90 g/l)
Particle size distribution optimized against permeability
Perforation of well A-23HPerforation of well A-23H
The well was perforated in June 2001 in the newly developed LS OBM-fluid and with a revised perforation strategy.
Operational problemsHigh losses to formation after perforation
Pumped additional kill pill based on CsCOOH-brine to cure losses
Investigations concluded that the circulation port failed during displacement and the upper part of the well was most likely perforated in clear brine
Same type of fluid based on CaCl2 used on Oseberg later on => no operational problems
Production of well A-23HProduction of well A-23H
Production controlled by maximum drawdown to reduce risk of sand production
Production rate after clean up: 7700 Sm3/D
Productivity 3-4 times higher than in previous comparable wells.
ConclusionConclusion
Improved productivity of well A-23H is the result of total consignment to the problem, where completion, perforation and fluid strategies are the most important items
Use of a new low solid oil based perforation fluid is regarded as being successful, and is an important contribution to improved well productivity