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LHC WEP061 Oct 12-16 2009, Kobe, Japan International Conference on Large Experimental Physics Control Systems CER THE CONTROL SYSTEM FOR THE CRYOGENICS IN THE LHC TUNNEL [ FIRST EXPERIENCE AND IMPROVEMENTS ] P. Gomes, E. Blanco, J. Casas, C. Fluder, E. Fortescue, P. Le Roux, G. Penacoba, M. Pezzetti, M. Soubiran, A. Tovar, L. Zwalinski; CERN, Geneva, Switzerland Conclusions Database work is well advanced but not finished effort in maintaining old views, to minimise modifications to Specs Generator, if needed Also updating electrical and fieldbus diagrams their correctness is vital for maintenance and for efficient support to operation. Evolved towards simplicity in process control, databases, and generator of specifications Combined patches and eliminated original features intended for the machine start-up The control system is now more reliable & user friendly and adapted to regular operation Databases - rationalisation The scope of the original Layout data model was broadened with only minor modifications, it accommodates a wider range of objects and properties became possible a coherent treatment to physical and conceptual objects Grouping as much data as possible in the Layout & treating all types of instrumentation channels the same way The views for the controls specifications become less complex Not necessary to maintain distinct codes to retrieve each category of instrument Layout DB web interface can be used to easily browse data, and follow relationships between all types of instruments Operability - PCO structure Process logic is supervised by a hierarchy of Process Control Objects (PCO) Below master sector-PCO, 1 for ARC and 1 for LSS under these, there was originally 1 for each cryogenic cell Cells are usually operated together, because simultaneously fed from the QRL all individual cell PCOs replaced by only 4 associated to the different hydraulic circuits, which are common to all cells SECTOR PCO ARC PCO LSS PCO He Guard Circuit Beam Sreen Circuit Cooling/Filling Circuit 1.9K Circuit Safety - quench valves & DFB In case of damage of the magnets' helium enclosure, when the machine is filled to avoid or minimise helium release into the tunnel New logic for quench protection valves to automatically discharge into the QRL independently of their mechanical threshold being reached New & more detailed hard-wired vacuum-quality signals combined with cryogenic signals (like pressure measurement), can trigger the opening of corresponding quench valves New Thermal Switches & Pressures Switches notify operator (beep call) of potential degradation in DFBs operating conditions Abstract The Large Hadron Collider (LHC) was commissioned at CERN and started operation with beams in 2008 Several months of operation in nominal cryogenic conditions have triggered an optimisation of the process functional analysis In order to enhance safety, availability and operability of LHC cryogenics, a major rebuild of the logic and several hardware modifications were implemented The databases, containing instruments & controls information, are being rationalized; the automatic generator of specifications for the control software is being simplified ATLAS LHCb CMS dump beam1 beam2 cleaning cleaning ALICE RF P1 P8 P5 P6 P7 P3 magnets 23 x regular cell 107 m QRL A R C D S S D S S L L S S P2 P4 Controls Layout Layout 18 500 Physical Instruments Family properties 6 600 Cables 14 600 Electrical Components 7 500 Spare & Virtual Instruments MTF Equipment Data Thermometer Calibrations Level Gauge Calibrations Pressure Sens Calibrations Sensorbase cabling files for connecting & inspecting specification for manufacturing FIP crates specification for Control software configuration for Mobile Test Bench 8 600 Derived Instruments cool-down phases other modes Operability - phase sequencer Initially comprising 11 phases and all transitions & replicated at all levels of PCOs Cool-down sequence simplified to 2 phases kept only in the middle-level PCOs; removed from the other levels activated when sector-PCO in the new option-mode 'cool-down' The 3 non-cool-down phases (emptying, stand-by, warm-up) also defined as option-modes, but without any sequencer option mode 1 option mode 2 option mode 3 Stand-by Warm-up Emptying System stopped option mode 4 0 Safety Position T1 1 Cooldown+Filling T0 T2 2 Normal Operation T0 cool-down sequencer Controls Layout Layout 18 500 Physical Instruments Family properties 6 600 Cables 14 600 Electrical Components 7 500 Spare & Virtual Instruments MTF Equipment Data Thermometer Calibrations Level Gauge Calibrations Pressure Sens Calibrations Sensorbase cabling files for connecting & inspecting specification for manufacturing FIP crates specification for Control software configuration for Mobile Test Bench 8 600 Derived Instruments Thermbase Specifications Generator - simplification Extracts data from several DB views & from external spreadsheets applies a set of rules and calculations to derive parameter values, relationships and secondary objects Once the databases are completed and coherently structured a set of views will replicate each page of the specifications the maintenance of generator & database will be much simplified also a view with the PLC hardware configuration directly importable into S7 Complex Specifications Generator Controls Layout DB Main View FIP View Signals View ProfibusDP View ProfibusPA View Specifications (Excel Workbook) AI Page AO Page Analog Page DI Page DO Page OnOff Page Excel Various Pages Various Pages Various Pages Derived instrums Variables etc Specifications (Excel Workbook) AI Page AO Page Analog Page DI Page DO Page OnOff Page Controls Layout DB AI View AO View Analog View DI View DO View OnOff View Simplified Specifications Generator Architecture 27 km proton collider, 100 m underground, 8 sectors, each with: 2 long straight sections (LSS); a curved part (ARC) with 23 regular cells of 107 m 2 000 instruments distributed over 3 300 m; industrial field networks (Profibus & WorldFIP) 2 PLC Siemens S7-416-2DP, each running 250 control loops & 500 alarms and interlocks 8 Front End Computers: gateway FIP - PLC man-machine interface based on a SCADA built on PVSS control software conforms to the UNICOS framework of CERN TT CV PV/QV PT LT EH FT DI FIP DI Profi 9 599 2 662 700 897 474 2 429 2 521 1 291 physical derived spare virtual 18 575 8 624 5 702 1 820 electrical cables 14 657 6 656 in DB 56 034 in control sys 32 437 16 291 Availability - nominal conditions To limit magnet powering the availability in nominal conditions expected to improved by median filters on all sensors, to aoid spikes low-pass filter for input of the control loops new LT object with more accurate parameterisation control loops reviewd and optimised interlocks list fully reviewd down-time of Software production The modifications on PCO structure, sequencer, control loops, interlocks, and a new version of the UNICOS programming environment implied significant rebuild of logic templates used by the code generators generic functions with for objects families tools for automatic generation & automatic validation SCADA panels

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  • LHC

    WEP061 Oct 12-16 2009, Kobe, Japan International Conference on Large Experimental Physics Control Systems

    CER

    THE CONTROL SYSTEM FOR THE CRYOGENICS IN THE LHC TUNNEL[ FIRST EXPERIENCE AND IMPROVEMENTS ]

    P. Gomes, E. Blanco, J. Casas, C. Fluder, E. Fortescue, P. Le Roux, G. Penacoba, M. Pezzetti, M. Soubiran, A. Tovar, L. Zwalinski; CERN, Geneva, Switzerland

    ConclusionsDatabase work is well advanced but not finished

    effort in maintaining old views, to minimise modifications to Specs Generator, if needed

    Also updating electrical and fieldbus diagrams

    their correctness is vital for maintenance and for efficient support to operation.

    Evolved towards simplicity

    in process control, databases, and generator of specifications

    Combined patches and eliminated original features intended for the machine start-up

    The control system is now more reliable & user friendly and adapted to regular operation

    Databases - rationalisationThe scope of the original Layout data model was broadened

    with only minor modifications, it accommodates a wider range of objects and properties

    became possible a coherent treatment to physical and conceptual objects

    Grouping as much data as possible in the Layout

    & treating all types of instrumentation channels the same way

    The views for the controls specifications become less complex

    Not necessary to maintain distinct codes to retrieve each category of instrument

    Layout DB web interface can be used to easily browse data,

    and follow relationships between all types of instruments

    Operability - PCO structureProcess logic is supervised by a hierarchy of Process Control Objects (PCO)

    Below master sector-PCO, 1 for ARC and 1 for LSS

    under these, there was originally 1 for each cryogenic cell

    Cells are usually operated together, because simultaneously fed from the QRL

    all individual cell PCOs replaced by only 4

    associated to the different hydraulic circuits, which are common to all cells

    SECTOR PCO

    ARC PCO LSS PCO

    He Guard Circuit

    Beam Sreen Circuit

    Cooling/Filling Circuit

    1.9KCircuit

    Safety - quench valves & DFBIn case of damage of the magnets' helium enclosure, when the machine is filled

    to avoid or minimise helium release into the tunnel

    New logic for quench protection valves

    to automatically discharge into the QRL

    independently of their mechanical threshold being reached

    New & more detailed hard-wired vacuum-quality signals

    combined with cryogenic signals (like pressure measurement),

    can trigger the opening of corresponding quench valves

    New Thermal Switches & Pressures Switches

    notify operator (beep call) of potential degradation in DFBs operating conditions

    AbstractThe Large Hadron Collider (LHC) was commissioned at CERN and started operation with beams in 2008

    Several months of operation in nominal cryogenic conditions have triggered an optimisation of the process functional analysis

    In order to enhance safety, availability and operability of LHC cryogenics, a major rebuild of the logic and several hardware modifications were implemented

    The databases, containing instruments & controls information, are being rationalized; the automatic generator of specifications for the control software is being simplified

    ATLAS LHCb

    CMS

    dump

    beam1beam2

    cleaning

    cleaningALICE

    RF

    P1P8

    P5

    P6

    P7

    P3

    magnets

    23 x regular cell 107 m

    QRL

    ARCDSSDSSL

    LSS

    P2

    P4

    Controls Layout

    Layout

    18 500Physical

    Instruments

    Family properties

    6 600Cables

    14 600Electrical

    Components

    7 500Spare & Virtual

    Instruments

    MTF

    Equipment Data

    Thermometer Calibrations

    Level Gauge Calibrations

    Pressure SensCalibrations

    Sensorbase

    cabling files for connecting & inspecting

    specification for manufacturing FIP crates

    specification for Control software

    configuration for Mobile Test Bench

    8 600Derived

    Instruments

    cool-downphases

    othermodes

    Operability - phase sequencerInitially comprising 11 phases and all transitions & replicated at all levels of PCOs

    Cool-down sequence simplified to 2 phases

    kept only in the middle-level PCOs; removed from the other levels

    activated when sector-PCO in the new option-mode 'cool-down'

    The 3 non-cool-down phases (emptying, stand-by, warm-up)

    also defined as option-modes, but without any sequencer

    optionmode

    1

    optionmode

    2

    optionmode

    3

    Stand-by Warm-upEmptying

    Systemstopped

    optionmode

    4

    0 Safety Position

    T1

    1 Cooldown+Filling

    T0 T2

    2 Normal Operation

    T0

    cool-downsequencer

    Controls Layout

    Layout

    18 500Physical

    Instruments

    Family properties

    6 600Cables

    14 600Electrical

    Components

    7 500Spare & Virtual

    Instruments

    MTF

    Equipment Data

    Thermometer Calibrations

    Level Gauge Calibrations

    Pressure SensCalibrations

    Sensorbase

    cabling files for connecting & inspecting

    specification for manufacturing FIP crates

    specification for Control software

    configuration for Mobile Test Bench

    8 600Derived

    Instruments

    Thermbase

    Specifications Generator - simplificationExtracts data from several DB views & from external spreadsheets

    applies a set of rules and calculations

    to derive parameter values, relationships and secondary objects

    Once the databases are completed and coherently structured

    a set of views will replicate each page of the specifications

    the maintenance of generator & database will be much simplified

    also a view with the PLC hardware configuration directly importable into S7

    Complex Specifications Generator

    Controls Layout DB

    MainView

    FIPView

    SignalsView

    ProfibusDPView

    ProfibusPAView

    Specifications (Excel Workbook)

    AIPage

    AOPage

    AnalogPage

    DIPage

    DOPage

    OnOffPage

    Excel

    VariousPages

    VariousPages

    VariousPagesDerived instrums

    Variables

    etc

    Specifications (Excel Workbook)

    AIPage

    AOPage

    AnalogPage

    DIPage

    DOPage

    OnOffPage

    Controls Layout DB

    AIView

    AO View

    Analog View

    DI View

    DOView

    OnOffView

    Simplified Specifications Generator

    Architecture27 km proton collider, 100 m underground, 8 sectors, each with:

    2 long straight sections (LSS); a curved part (ARC) with 23 regular cells of 107 m

    2 000 instruments distributed over 3 300 m; industrial field networks (Profibus & WorldFIP)

    2 PLC Siemens S7-416-2DP, each running 250 control loops & 500 alarms and interlocks

    8 Front End Computers: gateway FIP - PLC

    man-machine interface based on a SCADA built on PVSS

    control software conforms to the UNICOS framework of CERN

    TT CV PV/QV PT LT EH FT DI FIP DI Profi

    9 599 2 662 700 897 474 2 429 2 521 1 291

    physical derived spare virtual

    18 575 8 624 5 702 1 820

    electrical cables

    14 657 6 656

    in DB

    56 034

    in control sys

    32 437

    16 291

    Availability - nominal conditionsTo limit magnet powering

    the availability in nominal conditions expected to improved by

    median filters on all sensors, to aoid spikes

    low-pass filter for input of the control loops

    new LT object with more accurate parameterisation

    control loops reviewd and optimised

    interlocks list fully reviewd

    down-time of

    Software productionThe modifications on PCO structure, sequencer, control loops, interlocks,

    and a new version of the UNICOS programming environment

    implied significant rebuild of

    logic templates used by the code generators

    generic functions with for objects families

    tools for automatic generation & automatic validation

    SCADA panels