ler 94-003-00:on 940710,turbine runback occurred following ... · (luke ibtrer company (803)8313000...

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- _ . . . . . ._. - . - . .. || | . , ~' ' (luke Ibtrer Company (803)8313000 Catawba Neulear Swtion 4800 Concord Road H>rk. SC 2974.5 ' i 1 DUKEPOWER August 12, 1994 Document Control Desk U. S. Nuclear Regulatory Commission Washington, D.C. 20555 Subject: Catawba Nuclear Station Docket No. 50414 LER 414/94-003 Gentlemen: , Attached is Licensee Event Report 414/94-003 concerning MANUAL, REACTOR TRIP ON LOSS OF NORMAL FEEDWATER DUE TO SYSTEM PERFORMANCE. This report is being submitted three days past the 30 day NRC requirement. Late submittal was discussed with Catawba Senior Resident, R.J. Freudenberger, who finds this date for submittal to be acceptable. This event was considered to be of no significance with respect to the health and safety of the | public. Very truly yours, , Y 4, D. L. Rehn xc: Mr. S. D. Ebneter Marsh & McLennan Nuclear Regional Administrator, Region 11 1166 Avenue of the Americas U. S. Nuclear Regulatory Commission New York, NY 10036-2774 101 Marietta Street, NW, Suite 2900 Atlanta, GA 30323 Mr. R. E. Martin INPO Records Center U. S. Nuclear Regulatory Commission Suite 1500 Office of Nuclear Reactor Regulation 1100 Circle 75 Parkway Washington, D.C. 20555- Atlanta, GA 30339 - Mr. R. J. Freudenberger NRC Resident Inspector Catawba Nuclear Station 9408180156 940812 g2,,& %,m , ,,,, , PDR ADOCK 05000414 1 - _ .-. __ gh S PDR

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Page 1: LER 94-003-00:on 940710,turbine runback occurred following ... · (luke Ibtrer Company (803)8313000 Catawba Neulear Swtion 4800 Concord Road H>rk. SC 2974.5 ' i 1 DUKEPOWER August

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~' '(luke Ibtrer Company (803)8313000Catawba Neulear Swtion4800 Concord RoadH>rk. SC 2974.5 '

i 1 DUKEPOWER

August 12, 1994

Document Control DeskU. S. Nuclear Regulatory CommissionWashington, D.C. 20555

Subject: Catawba Nuclear StationDocket No. 50414LER 414/94-003

Gentlemen:,

Attached is Licensee Event Report 414/94-003 concerning MANUAL, REACTOR TRIP ONLOSS OF NORMAL FEEDWATER DUE TO SYSTEM PERFORMANCE.

This report is being submitted three days past the 30 day NRC requirement. Late submittal wasdiscussed with Catawba Senior Resident, R.J. Freudenberger, who finds this date for submittalto be acceptable.

This event was considered to be of no significance with respect to the health and safety of the |

public.

Very truly yours, ,

Y 4,

D. L. Rehn

xc: Mr. S. D. Ebneter Marsh & McLennan NuclearRegional Administrator, Region 11 1166 Avenue of the AmericasU. S. Nuclear Regulatory Commission New York, NY 10036-2774101 Marietta Street, NW, Suite 2900Atlanta, GA 30323

Mr. R. E. Martin INPO Records CenterU. S. Nuclear Regulatory Commission Suite 1500Office of Nuclear Reactor Regulation 1100 Circle 75 ParkwayWashington, D.C. 20555- Atlanta, GA 30339 -

Mr. R. J. FreudenbergerNRC Resident InspectorCatawba Nuclear Station

9408180156 940812 g2,,& .%,m , ,,,, ,PDR ADOCK 05000414 1

- _ .-. __

ghS PDR

Page 2: LER 94-003-00:on 940710,turbine runback occurred following ... · (luke Ibtrer Company (803)8313000 Catawba Neulear Swtion 4800 Concord Road H>rk. SC 2974.5 ' i 1 DUKEPOWER August

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NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMD NO. 3150-0104'

is ca EXPlRES 5/31/95

E 5itMATED HURDEN PE R DESPONSI COMPLY W'TH TH$

LICENSEE EVENT REPORT (LER) $$fr M E f L s $EMJi TSE,NJfjTO&^"OAND HECOROS M3NAGE MENT HRANCH tMNHH 7714 U.S. NUCtfAAREGULA!ORY COMUMON W ASHtNGTON, DC 2055$ 0001. AND TO jTHE PAP [FiW'.h REDUCTION PROJLCT {3150 0104L OFFICE OF |(See reverse for required number of dig.ts/ characters for each block) MANAGF YENT AND BUDGET, WASH +NGTON, DC 20503

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f ACitnY NAMt 0) DOCKET NUMBLH (2) PAGE (3)Catawba Nuclear Station, Unit 2 05000414 1OF/

Ti tti (4)

Manual Reactor Trip on Loss of Normal Feedwater Due to System Performance.

EVENT DATE (5) LER NUMBER (6i REPORT NUMBER (7) OTHER FACILITIES INVOLVED (8) IF AQU T V NAML DUCKLI NUMdl HT[ UUf NT4AL DE VGON

MON H DA( Y[ Aq YEAR MON 7 H DAY YEA" N/A 05000q

f ALJU f V N AML DOCGT NUMMR

07 10 94 94"

003~

00 08 12 94 05000

OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR O (Check one or more) (11)MODE (9) 1 20 402(b) 20.405(c) X 50.73(a)(2)(iv) 73 71(b)

POWER 20 405(a)fIHi) 50 36(c)(1) 50.73(a)(2)(v) 73.71(c)LEVEL (10) 100 20 405taH1Hd) 50 36(c)(2) 50.73(a)(2)(vii) OTHER

20 405taH1)(m) 50 73(a)(210) 50.73(a)(2)(vm)(A) PP *r'aAb**ct

20 405(aH1)0v) 50 73(aH2)(u) 50.73(a)(2)(voi)(B) r b A[20 405(a)(1)(v) 50.73(aH2)(m) 50.73(a)(2)(x)

LICENSEE CONTACT FOR THIS LER (12)NAvi TLLLPHONE NUYME H tinch.de Area Codet

D. P. Kimball, Safety Review Group Manager (803) 831-3743

COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)

N[OR ARLERE POR r ABLEcAuq timv cnum u sT MANuf am wR y

SUPPLEMENTAL REPORT EXPECTED (14) [ EXPECTED M*" DAY *tA"

vt S SUBMISSIONggcen cmw cwtcttD sonv.ssiaN DAir> X DATE (15)

ADSTRACT (Limit to 1400 spaces, i e., approomately 15 single-spaced typewntten 14nes) (16)

On July 10,1994, at 1347 hours with Unit 2 in Mode 1, Power Operation, at 100% power, a turbine runbackoccurred following manual trip of a malfunctioning Main Feedwater Pump (CFP). Following the runback, aloss of Main Feedwater (CF) occurred, caused by one of the Steam Generator's (S/G) 1.:vels reaching the"High41igh" level ESFAS Interlock Setpoint. This resulted in ESFAS actions to trip the M.lin Turbine (MT),trip both CFPs, and isolate CF. Tripping of both CFP initiated an ESFAS signal to start both Motor Driven JAuxiliary Feedwater Pumps. No automatic reactor trip signal was initiated because the unit was below theReactor Trip on Turbine Trip Interlock Setpoint. The reactor was manually tripped at 1355 hours from 65%power. The unit was stabili7.ed in Mode 3, Hot Standby, using " Reactor Trip Response" Emergency OperatingProcedure. The Root Cause of this event is attributed to the performance of the CF System following level

,

recovery from low S/G levels. The initial trip investigation did not reveal any anomalies in the response ofI

the S/G Level Control System. Following restart, additional information indicated the need for continuing ,

evaluation of the S/G Ixvel Control System performance. The performance of the S/G Level Control System !

transient response is a unit availability / reliability concern and not a nuclear safety issue. Corrective actionsinclude evaluation of secondary systems interactions and responsiveness of the S/G Level Control System |

including the CF Control Valves.

NnmOnu m m <

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REQUIRED NUMBER OF DIGITS / CHARACTERSFOR EACH BLOCK

BLOCK NUMBER OF 'NUMBER DIGITS / CHARACTERS

1 UP TO 46 FACILITY NAME

2 DO N W M3 IN ADDITION TO 05000

3 VARIES PAGE NUMBER

4 UP TO 76 TITLE

65 U^g pER BLOCK

7 TOTAL" ^"

6 LER NUMBER3 FOR SEQUENTIAL NUMBER

2 FOR REVISION NUMBER

7 ^2 PER BLOCK

UP TO 18 - FACILITY NAME

8 OTHER FACILITIES INVOLVED8 TOTAL - DOCKET NUMBER

3 IN ADDITION TO 05000

9 1 OPERATING MODE

10 3 POWER LEVEL

'l REQUIREMENTS OF 10 CFRCHECK BOX THAT APPLIES

UP TO 50 FOR NAME12 LICENSEE CONTACT

14 FOR TELEPHONE

CAUSE VARIES2 FOR SYSTEM

13 4 FOR COMPONENT EACH COMPONENT FAILURE4 FOR MANUFACTURER

NPRDS VARIES

'#CHECK BOX THAT APPLIES

15 D SUBMSSION DAM2 PER BLOCK

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. _ - _ _ - . . _ _ _ _ _ . _ _ _ _ _ _ _ _ _ __ _. _ _____ _ _ _ _ __ ._

Page 4: LER 94-003-00:on 940710,turbine runback occurred following ... · (luke Ibtrer Company (803)8313000 Catawba Neulear Swtion 4800 Concord Road H>rk. SC 2974.5 ' i 1 DUKEPOWER August

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%* '2C FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104

EXPlRES 5/31/95

ESTfMATED BURDEN PER RESPONSE TO COMDLY W"TH THl$

LICENSEE EVENT REPORT (LER) ZT@Sn%CZR0,Eo u,,5 W" T

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TEXT CONTINUATION AND REOOADS MANAGEMENT BRANCH {MNB8 Midi, V $ NUCLEAAAE 3dLA'OAV COMM StON. W ASHfNGTON, DC 20555 000', AND toTME F APE AWORA REDUCTION FAQJECT (3'S40'OA OFFCE OFMANAGEVEN? AND BJDGET, W ASHiNGTON. DC 20503

f ACILITY NAME O f DOCKET NUMBER (2) LE R NUMBER (4) PAGE (3)

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05000 414 2 OF 7Catawba Nuclear Station, Unit 2_

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BACKGROUND

The Main Turbine Control System [EIIS:JJJ(ITE) is designed to control the turbine [EIIS:TRB] |

under all load conditions. Incorporated into this design is the capability to " runback" the turbineload during selected abnormal conditions for the secondary side of the unit. One such conditionis the loss of a single Main Feedwater Pump [EIIS:P] with turbine load greater than 65%. The" runback" terminates at less than or equal to 65% turbine load based on turbine first stagepressure.

The Main Feedwater [EIIS:SJJ(CF) System consists of two Main Feedwater Pumps, piping[ Ells:PSPJ and valves [ Ells:V] necessary to deliver the Main Feedwater to the four SteamGenerators [ Ells:SGj(S/G) during normal plant operation.

The Steam Generator Level Control System [EIIS:JB](IFE) is designed to maintain aprogrammed level in each Steam Generator. Programmed level is a function of reactor[EIIS:RCT] power. For Unit 2 the program ramps narrow range level from 62% at 0% powerto 67% at 100% power. The system controls level by adjusting Main Feedwater Pump speedto maintain the Feedwater Control Valves [EIIS:LCVJ at the optimum throttling position for unit |

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load as the valves respond to level and/or steam flow changes, thus ensuring adequate feedwaterflow to maintain level. The system also functions to restore and maintain levels at acceptablevalues during normal transients, thus mitigating undesirable reactor and/or turbine trips. If,however, the levels in the Steam Generators reach the limits which either jeopardize the SteamGenerators' ability to act as a " heat sink" due to low-low level m threaten to damage equipmentdue to moisture carryover as a result of high-high level, then a signal is generated to either tripthe reactor via the REACTOR TRIP SYSTEM [EIIS:JDl(IPE) for Steam Generator water levelLow-Low g trip the Main Turbine, trip the Main Feedwater Pumps and initiate Main FeedwaterIsolation via the ENGINEERED SAFETY FEATURES ACTUATION SYSTEM [ Ells:JE](ISE)for Steam Generator water level Iligh-Iligh.

The ENGINEERED SAFETY FEATURES ACTUATION SYSTEM senses selected plantparameters and compares them to predetermined limits. If a limit is exceeded, the system sendsactuation signals to those ENGINEERED SAFETY FEATURES components whose aggregatefunction best serves the requirements of the condition. One such condition is Steam GeneratorWater Level Iligh-liigh. For Unit 2 the limit is < /= 77.1 % of narrow range instrument span.The actuation signals generated are: Main Turbine Trip, Both Main Feedwater Pumps Trip, andMain Feedwater Isolation. Tripping of both Main Feedwater Pumps generates an actuation

N4C FORM 366A ($ On

_______ _ _ -- _ _ _ _ _ _ _ _ _ _ _ . . _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ __ __

Page 5: LER 94-003-00:on 940710,turbine runback occurred following ... · (luke Ibtrer Company (803)8313000 Catawba Neulear Swtion 4800 Concord Road H>rk. SC 2974.5 ' i 1 DUKEPOWER August

NRC F RM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104<5 ez

EXPIRES 5/31/95

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THE PAPCAWORK REDUCT60N PRMCT (3MC104, OFFICE OFt

MANAGEMENT AND BUDGE 7, WASHINGTON, DC 20503

f ACILITY NAMt 0) DOCKET NUMBE R (2) LEN NUMBER (t) PAGE (3)

bt GV f.M .AL REWStONNJMBE FI NUMBERCatawba Nuclear Station, Unit 2 05000414 3 OF 7 -

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signal to start both Motor [ Ells:MO] Driven Auxiliary Feedwater Pumps. The tripping of themain turbine will initiate a REACTOR TRIP SYSTEM signal if reactor power is above theReactor Trip on Turbine Trip (P-9) Interlock [EIIS:IEL] Setpoint.

liVENT DESCRIPTION

On July 10,1994, at 1347 hours with Unit 2 in Mode 1, Power Operation, at 100% power, anautomatic turbine runback occurred following the manual trip of 2A Main Feedwater Pump. 2AMain Feedwater Pump was tripped due to high thrust bearing temperatures. The thrust bearingtemperatures had been above normal and Engineering was in the process of having Operations" bias" the loading on 2A and 2B Main Feedwater Pumps when the outboard thrust bearingtemperature unexpectedly increased to 210 degrees. Abnormal Procedure, AP/2/A/5500/03, |

LOAD REJECTION, was entered and all applicable steps completed. The unit responded asdesigned during the runback. The runback terminated at a reactor power level of 76%.

At 1348 hours with Unit 2 at 76% power, the Balance of Plant Operator manually reducedturbine load an additiona! 100 MWE, due to all four Steam Generators' feedwater control valvesbeing fully open and the 2B Main Feedwater Pump's speed being higher than expected.Additionally, the 2B Main Feedwater Pump suction flow was greater than 20000 GPM.

At 1354 hours with Unit 2 at 65% power, the Operator at the Controls noted rapidly risinglevels in all four Steam Generators. The Main Feedwater Control Valves were observed to befully open. Steam Generator levels were at programmed level for the current reactor power andrising. 2A and 2C Steam Generators had the highest indicated levels. The Operator at theControls took manual control of 2CF-28 (2A Steam Generator Main Feedwater Control Valve)and began throttling it closed in order to control the rising level. 2CF-28 was placed back inautomatic and 2CF-46 (2C Steam Generator Main Feedwater Control Valve) was placed inmanual and throttled closed in order to control the rising level.

At 1354:45 hours with Unit 2 at 65% power and 2CF-46 in manual, 2C Steam GeneratorNarrow Range level reached the "High-Iligh" level (P-14) ESFAS Interlock Setpoint of </=77.1 %. The following ESFAS signals were initiated by P-14; a trip of the Main Turbine, tripof both Main Feedwater Pumps, and Main Feedwater Isolation. All components responded totheir respective ESFAS signals. The trip of the remaining Main Feedwater Pump satisfied thelogic for the ESFAS signal to start both Motor Driven Auxiliary Feedwater Pumps. Both pumpsresponded to the ESFAS signal.

NAC FORM 366A (5 62:

Page 6: LER 94-003-00:on 940710,turbine runback occurred following ... · (luke Ibtrer Company (803)8313000 Catawba Neulear Swtion 4800 Concord Road H>rk. SC 2974.5 ' i 1 DUKEPOWER August

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NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB No. 3150-0104<s n EXPIRES 5/31/95

ESilMATED BURDEN PER HESPONSE TO COMPLY wtTH T HIS

LICENSEE EVENT REPORT (LER) '"s*T'ESit$s*al"RiMELTNOTS -OCT7'

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TEXT CONTINUATION Qas"yO" 8|7v@s7',!Mo"g[""'A'||;%8 "Ec 3,

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F ACILITY NAME p) DOCKET NUMBER (2) L1H NUMBER (4) PAGE(bbtOULNhAi HtV15CNANUMBER NUMBERCatawba Nuclear Station, Unit 2 05000 414 4 OF 7

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At 1355 hours with Unit 2 at 65 % power, a manual reactor trip was initiated. No automatic tripsignal was present or required. The unit was below the Reactor Trip on Turbine Trip Interlock(P-9) Setpoint of > /= 69%. The manual reactor trip was initiated as required by the " LOSSOF S/G FEED" Abnormal Procedure, AP/2/A/5500/06. Upon manually tripping the reactor,Emergency Procedure, EP/2/A/5000/E-0, Reactor Trip or Safety Injection, was entered, allappropriate steps perfonned and transition was made to EP/2/A/5000/ES-0.1, Reactor TripResponse. The Safety Parameters Display System (SPDS) was continuously monitored andEP/2/A/5000/F-0, Critical Safety Function Status Trees, was implemented. All Critical SafetyFunctions were fully satisfied. The unit was maintained in Mode 3, Hot Standby, until restartwas commenced using OP/2/A/6100/05, UNIT FAST RECOVERY.

CONCLUSION

This event occurred when the four S/G's levels became higher than expected following recoveryfrom loss of a single CFP with the unit initially at Rated Thermal Power. During the runback,the operating CFP speed increased and the CF Control Valves fully opened as expected inresponse to decreasing S/G levels. Upon level recovery, the IFE valve demand begandecreasing as S/G level approached programmed level. Three of the four CF Control Valvesbegan closing within twelve seconds of the demand change. The fourth CF Control Valve beganclosing twenty-five seconds after the demand change. Even the delay of twelve seconds was too :

long for the CF Control Valves to reduce flow quickly enough to slow the rise of S/G level. Itis concluded that the aggregate response of the IFE and the CF Control Valves in automatic was ,

|too slow to prevent level increase " overshoot" during the loss of CFP transient.

The operators' actions to reduce CF flow manually had no adverse effect on the ultimateoutcome. The exhibited rate of change of all four S/G levels Lnd the values of those levels show )that had the operators been able to " turn" level in the 2C S/G, then level in one or more of the jother three S/G would have reached the "lilGil-IIIGli LEVEL (P-14) SETPOINT", culminating

;

in the same event sequence.

Since the Root Cause for the levels in each S/G reaching or approaching the "HIGH-HIGHLEVEL (P-14) SETPOINT" has been determined to be performance of the S/G Level ControlSystem, the paragraphs below address areas of continuing evaluation.

1) Process instrument calibration in the S/G Level Control System; this is to determine ifconservative instrumentation tolerances exhibited a " stacking" effect resulting in more than turequired conservatism, such that operational margins are unnecessarily reduced.

NRC FORY3664{542;

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NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISslON APPROVED BY OMB NO. 3150 0104is sa

EXPIRES 5/31/95

ESTIMATED BJRDEN PER RE SPONSE TO COMPLY WTTH THIS

LICENSEE EVENT REPORT (LER) E$US%to'AnfflB RifsEE OZ'MC'""

TEXT CONTINUATION QS "$838 $7,^$$'Tja"8E"" '"s'sfo *>ci No$'c y

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2) S/G Level Control System signal generation; this is to ensure that the demand signals havesufficient response characteristics for transient conditions while still maintaining steady statestability.

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3) CF Control Valve operation; this is to ensure timely response to transient conditions whilestill maintaining steady state stability.

4) CF Control Valve throttling position; this is to restore the valves to their " optimum"throttling position.

5) Reassessment of the Auxiliary Feedwater (CA) System piping modification; this is to ensurethat the effects, if any, of the larger diameter piping are addressed for CF transients.

Subsequent to this event, a Work Order was issued to check the pneumatic controls for the CFControl Valves to ensure proper Instrument Air [EIIS:LDJ(VI) System alignment, fittingtightness and adjustment screw locknut tightness.

A review of the Operating Experience Program (OEP) database for the previous 24 months prior jto this event revealed that no reactor trip Licensee Event Reports (LERs) had the same cause j

code. A review of LERs for events other than reactor trips revealed that for the same time'

frame, none had the same cause code. Therefore, this is not a recurring problem.

!

CORRECTIVE ACTIONS '

IMMEDIATE

The reactor was manually tripped and EP/2/A/5000/E-0, REACTOR TRIP OR SAFETYINJECTION, was entered with transition to EP/2/A/5000/l'.S-0.1, REACTOR TRIPRESPONSE, to stabilize the unit in Mode 3, Ilot Standby.

SUBSEQUENT

1) PT/0/A/4150/02, TRANSIENT INVESTIGATION, was completed and based on review oftransient data retrieved on July 10, 1994, the unit was restarted using OP/2/A/6100/05,UNIT FAST RECOVERY. No items affecting unit startup were identified.

NRO FOAM 386A (s 82)

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. .

.

5HC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104is e EXPIRES 5/31/95

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F ACIUTV NAME 0) DOCRET NUMBt.H (2) LER NUMBER (t) PAGE (3)

YEAR i

NUMBE R NUMBER !Catawba Nuclear Station, Unit 2 05000 414 6OF794 - 003 - 00

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2) Work Order #94058318 01 was issued on 08/03/94 to conduct a visual inspection of thepneumatic controls for the Main Feedwater Control Valves to ensure the physical integrityof the pneumatic fittings, the proper Instrument Air System alignment, and the tightness oflocking devices on the adjustment screws. No conditions were found to exist that wouldaffect valve operation. This Work Order was completed on 08/04/94.

PLANNED

1) Electrical / Systems Equipment Engineering evaluate process instrument calibration in the S/GLevel Control System to determine if conservative instrumentation tolerances exhibit a" stacking" effect such that more than required conservatism exist.

2) Electrical / Systems Equipment Engineering evaluate S/G Level Contro: System signalgeneration to ensure that the demand signals have sufficient response characteristics fortransient conditions while still maintaining steady state stability.

3) Instrument and Electrical Department evaluate CF Control Valve operation to ensure timelyresponse to transient conditions while still maintaining steady state stability.

4) Electrical / Systems Equipment Engineering evaluate the current CF Control Valve throttling ;

position and restore the valves to their " optimum" throttling position.

5) Mechanical Systems Engineering reassess the CA piping modification to verify that anyeffects on CF transients have been considered and accounted for.

6) Catawba Safety Review Group will evaluate the need to supplement this report uponcompletion of the above five PLANNED CORRECTIVE ACTIONS.

1

SAFETY ANALYSIS

This event was initiated by a turbine runback as a result of a loss of a single CFP at RatedThermal Power. The turbine trip on "IIIGII-IIIGII" S/G level occurred as a result of excessive i

feedwater flow following recovery from the runback. This event is bounded by the Safety !

Analysis documented in FSAR Section 15.1.2, FEEDWATER SYSTEM MALFUNCTIONCAUSING AN INCREASE lN FEEDWATER FLOW.

NRC FORM 36EA (5 92)

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..

NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104is s2

EXPIRES 5/31/95

ESilMA'ED BURDEN PER RESPONSE TO COMPLY WfTH TH:S#NcORM A TION COLLECTION REQUEST 50 0 HRS. F ORW ARDLICENSEE EVENT REPORT (LER) COvMENTS nEGARo,NG euRatN EST unE Yo nE i~FORMo cn

TEXT CONTINUATION ^' "' C "'8 "'N^ S"'"' "*'ANC" **S8 ""' U S ""C*'"REGULATORf COMV:SS:ON, W ASHtNOTON DC 20$$5 000'1. AND TOTHE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OFMANAGEMEN' AND BUDGET. WASMtNGTON, DO 20503

F ACILITY NAME (1) DOCKET NUMBER (2) f LE R NUMBLR st) PAGE (3)bE fWt.N iia. RLV@ON

NJMBER NUMBERCatawba Nuclear Station, Unit 2 05000 414 7OF794

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The operator's action to manually trip the reactor, pre-empted the occurrence of the " LOW-LOW" S/G level reactor trip assumed in the FSAR and therefore mitigated the consequences ofthe automatic trip.

After a review of this event, it was determined that all systems responded as designed to shutdown the reactor and maintain it in a safe condition. There was no unusual release ofradioactive material.

The health and safety of the public were not affected by this event.

1

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NRC FORM 366A [5 92)